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34-089-23374

Well Details

Well ID: 34-089-23374
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Country: United States
State: Ohio
County: Licking
Municipality: Perry Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: BARRICK DALE L
License Status: Producing
License Date: 1977-05-02
Spud Date: 1979-07-31
Spud Drilling Contractor:
Final Drill Date: 1979-09-07
Well Total Depth: 2955.00 ft
Configuration: Vertical
Latitude: 40.130000
Longitude: -82.200000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-05-02 79 OXFORD OIL CO GeoDate 5/2/77
Unknown 1977-05-02 Issued Date 5/2/77 Expired Date 5/2/78 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Construction Permit Expires 1978-05-02 RI & RL 6-27-79
Original Spud 1979-07-31 RI & RL 6-27-79
Completed 1979-09-07 RI & RL 6-27-79
Reached Total Depth 1979-09-07 RI & RL 6-27-79
Change of Owner 2014-02-06 Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC
Change of Owner 2016-08-02 Operator changed from 9216, ECLIPSE RESOURCES-OHIO LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2016-08-04 RI & RL 6-27-79

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2888 2933 26
2888 2933 26
2888 2933 26

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 3200 Bbl 25000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OXFORD OIL 1298.00 705.00 0
1985 OXFORD OIL 0.00 611.00 365
1986 OXFORD OIL 1716.00 531.00 365
1987 OXFORD OIL 1697.00 441.00 365
1988 OXFORD OIL 1428.00 349.00 365
1989 OXFORD OIL 1076.00 356.00 365
1990 OXFORD OIL 863.00 282.00 365
1991 OXFORD OIL 15.00 414.00 365
1992 OXFORD OIL 778.00 258.00 365
1993 OXFORD OIL 774.00 179.00 365
1994 OXFORD OIL 803.00 203.00 365
1995 OXFORD OIL 696.00 132.00 365
1996 OXFORD OIL 725.00 165.00 366
1997 OXFORD OIL 593.00 27.00 365
1998 OXFORD OIL 496.00 103.00 365
1999 OXFORD OIL 564.00 143.00 365
2000 OXFORD OIL 490.00 124.00 0
2001 OXFORD OIL 123.00 91.00 365
2002 OXFORD OIL 17.00 117.00 365
2003 OXFORD OIL 0.00 108.00 365
2004 OXFORD OIL 0.00 108.00 365
2005 OXFORD OIL 0.00 84.00 365
2006 OXFORD OIL 0.00 99.00 365
2007 OXFORD OIL 0.00 84.00 365
2008 OXFORD OIL 0.00 53.00 365
2009 OXFORD OIL 0.00 84.00 0
2010 OXFORD OIL 0.00 60.00 365
2011 OXFORD OIL 0.00 49.00 0
2012 OXFORD OIL 0.00 49.00 0
2013 ECLIPSE RESOURCES-OHIO LLC 0.00 50.00 365
2014 ECLIPSE RESOURCES-OHIO LLC 0.00 57.00 365
2015 ECLIPSE RESOURCES-OHIO LLC 0.00 39.00 365
2016 ECLIPSE RESOURCES-OHIO LLC 0.00 0.00 365
2017 M & R INVESTMENTS OHIO LLC 0.00 14.00 365
2018 M & R INVESTMENTS OHIO LLC 0.00 51.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OXFORD OIL Brine 0 0
1985 OXFORD OIL Brine 384 365
1986 OXFORD OIL Brine 492 365
1987 OXFORD OIL Brine 486 365
1988 OXFORD OIL Brine 0 365
1989 OXFORD OIL Brine 142 365
1990 OXFORD OIL Brine 288 365
1991 OXFORD OIL Brine 321 365
1992 OXFORD OIL Brine 258 365
1993 OXFORD OIL Brine 256 365
1994 OXFORD OIL Brine 252 365
1995 OXFORD OIL Brine 164 365
1996 OXFORD OIL Brine 184 366
1997 OXFORD OIL Brine 204 365
1998 OXFORD OIL Brine 129 365
1999 OXFORD OIL Brine 179 365
2000 OXFORD OIL Brine 130
2001 OXFORD OIL Brine 124 365
2002 OXFORD OIL Brine 184 365
2003 OXFORD OIL Brine 164 365
2004 OXFORD OIL Brine 136 365
2005 OXFORD OIL Brine 149 365
2006 OXFORD OIL Brine 147 365
2007 OXFORD OIL Brine 129 365
2008 OXFORD OIL Brine 88
2009 OXFORD OIL Brine 118
2010 OXFORD OIL Brine 94 365
2011 OXFORD OIL Brine 108
2012 OXFORD OIL Brine 86
2013 ECLIPSE RESOURCES-OHIO LLC Brine 105 365
2014 ECLIPSE RESOURCES-OHIO LLC Brine 91 365
2015 ECLIPSE RESOURCES-OHIO LLC Brine 0 365
2016 M & R INVESTMENTS OHIO LLC Brine 0 365
2017 M & R INVESTMENTS OHIO LLC Brine 0 365
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1603866020 2019-3-26 0:00: PW No Violations 0.70
-1914868296 2016-9-21 0:00: PW No Violations
-1951058413 2020-5-6 0:00:0 PW No Violations 0.50
0391134017 2015-01-28 Production Wells No Violations This inspection was conducted as a production well status check. The well was equipped with a pumping unit and motor. Identification was posted at the well. The tank battery consists of (2) 100 barrel tanks inside an earthen dike. Identification was posted at the tank battery. No violations. Time of inspection: 1:59 PM. Weather: 22 degrees F, Sunny 3 snow
0765660449 2019-04-23 Production Wells No Violations My inspection revealed that identification has been posted at the well. The violation has been resolved. Time of inspection: 10:35 AM. Weather: 72 degrees F, Sunny
1217754488 2017-02-21 Production Wells No Violations I returned to this well today to meet with Dale Smith and Eddie Moss from M&R Investments. They have determined where the leak was coming from then used shovels to dig down and clamp the 2 inch steel flow line. The flow line was buried 3 foot under the ground. There was a pinhole in the steel line that caused the leak of the oil. The crew shoveled up all the contaminated soil they could find into trash bags. They will put down an oil absorbent and check back to see if anymore oil comes to the surface. It looks like an estimated 5-10 gallons leaked from the flow line. The company did not want to use any equipment in the yard because they did not want to tear up the landowners yard. I will return to the location to check on it myself in a couple of days.
1487681722 2017-02-19 Production Wells No Violations I received a phone call on 2/18/2017 at 7:09 pm from Emergency Supervisor Terry Whitehair reporting a flow line leak on the Barrick Walcutt # 2 well owned and operated by M&R Investments. Terry gave me the information on the well and asked if I could get eyes on the situation tomorrow morning. So today 2/19/2017 I went out to the well to do a field inspection on it. I found the flow line has leaked about 8-10 feet away from the road going down hill not towards the road. The flow line is under a bunch of little trees and brush. It has traveled down into the landowners yard in some spots. It is underground so we can not really determine how much there is at this point. I talked with Ethan the pumper from M&R Investments while I was on location. He came out to the well the night it was reported and cleaned up what he could. I then talked with Tim Altier and he informed me they would be coming back out Monday morning to work on it. I will come back out on location to check on the progress of the clean up.
1488209198 2017-02-23 Production Wells No Violations I returned to this well today to do a follow-up inspection on the flow line leak. At this point in the cleanup I only found a couple more spots of contamination come up from the rain. I contacted Eddie Moss from M&R to let him know they would need cleaned up. He stated he would have it done on the following day.
1488809180 2017-03-06 Production Wells No Violations I returned to this well today to do a follow-up inspection on it. Eddie Moss and his crew have been back out on location to put down topsoil along with seed and mulch. The contamination has all been removed at this point. The area is now cleaned up and reclaimed.
1490109744 2017-03-21 Production Wells No Violations This inspection was conducted as a status check. Top soil and straw was applied to the contaminated areas. Clean up has been completed. Time of inspection: 11:15 AM. Weather: 46*F, Sunny
1572672691 2017-02-20 Administrative Inspection No Violations I was contacted today by Eddie Moss from M&R Investments about the situation at this well. Mr. Moss wanted to know if I could meet him out on location tomorrow morning to go over the clean up of this well. I told him that would be fine and we agreed to meet at 9 am.
1603866020 2019-03-26 Production Wells No Violations This inspection was conducted in regards to a complaint from the landowner Mr. Mark Emde. Mr. Emde claims that this well has not produced for over two years and would like for the well to be plugged. The well was equipped with a pumping unit and motor. The well was shut-in at the time of the inspection. M & R Investments has reported 17 barrels of oil for 2017. The production report for 2018 was not available at the time of inspection. I told Mr. Emde that I would contact the company about his concern. This well produces into a shared tank battery with API permit numbers 3373, 3664, 3775, and 3776. Proper identification was displayed at the tank battery but I did not observe identification at the well. The well owner shall post identification at the well within 10 days. I spoke with Dale Smith on 3/28/2019 regarding my inspection. He advised me that they may set a tank near the well in order to produce it. Mr. Smith told me the current flow line is in too poor of condition to produce through it. I advised Mr. Smith that the well needs identification. Time of inspection: 1:30 PM. Weather: 41 degrees F, Sunny
1914868296 2016-09-21 Production Wells No Violations Met with landowner Mr. Mark Emde regarding questions and concerns about the well/company. No violations. Identification at the wellhead was not complete. The company will be advised to make identification complete. Mr. Emde informed me of an oil leak that occurred on his property last year. The Division was not notified of any leak at this property. Mr. Emde showed me the area where the leak happened. No issues visible at that spot. Time of inspection: 4:50 PM.
1935113495 2017-02-27 Production Wells No Violations I was on location to follow up on this well today. Everything looked good on location today. I contacted Eddie Moss from M&R to let him know they could bring in topsoil to put down with grass seed and straw. He stated they would get on it and get it done.
391134017 2015-1-28 0:00: PW No Violations
765660449 2019-4-23 0:00: PW No Violations 0.20

For data sources see[9]

References