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Well ID: 34-089-24693 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Hanover Township | |
Operator Name: H & D DRILLING CO INC | |
Well Pad ID: | |
Farm/Lease Name: THE TWENTIENTH CENTURY CLUB ETAL | |
License Status: Final Restoration | |
License Date: 2010-06-01 | |
Spud Date: 1983-03-12 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 1983-07-12 | |
Well Total Depth: 2955.00 ft | |
Configuration: Vertical | |
Latitude: 40.060000 | |
Longitude: -82.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-03-14 | Issued Date 3/14/83 Expired Date 9/10/83 Acres 0145700 Tool Type CT Proposed Formation CLINTON Proposed Depth 02955 Proposed Drill Depth 02955 |
Original Spud | 1983-03-15 | IPN. OIL = 1/2 BBL. |
Completed | 1983-07-12 | IPN. OIL = 1/2 BBL. |
Reached Total Depth | 1983-07-12 | IPN. OIL = 1/2 BBL. |
CO | 1983-07-15 | 401 H & D DRILLING CO INC GeoDate 3/14/83 |
Completion Report Received | 1983-10-21 | IPN. OIL = 1/2 BBL. |
APP | 2010-06-01 | Proposed Formations:CLINTON, Issued Date:6/1/2010, Expired Date:6/1/2011 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2011-04-19 | IPN. OIL = 1/2 BBL. |
Construction Permit Expires | 2011-06-01 | IPN. OIL = 1/2 BBL. |
Record Last Modified | 2017-02-15 | IPN. OIL = 1/2 BBL. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 2903 | 2930 | 0 |
2903 | 2930 | 0 | |
2903 | 2930 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1200 Bbl | 40000 | FRAC,WATER & SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2005 | H & D DRILLING CO INC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2005 | H & D DRILLING CO INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1813985659 | 2011-4-11 0:00: | PB | No Violations | 1.50 |
-678755016 | 2011-4-14 0:00: | PB | No Violations | 1.00 |
000PL13814 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0678755016 | 2011-04-14 | Plug / Plug Back | No Violations | An inspection revealed no plugging activity at this time. |
1176601659 | 2011-04-12 | Plug / Plug Back | No Violations | Witnessed pre-cast concrete plug placed on 7 seat and washing of fireclay into wellbore to cover Berea formation. |
1302278292 | 2011-04-08 | Plug / Plug Back | No Violations | I witnessed plugging operations today. Mark Donaker with H&D Drilling is plugging this Clinton well. The first portion of the bottom hole plug was set with 2 tons of fireclay before of the 4 inch production casing was ripped. |
1441895989 | 2014-04-08 | Final Restoration | No Violations | This inspection was conducted as a final restoration status check. The well has been plugged and equipment removed. Inspection meets ORC 1509.072 requirements. |
1813985659 | 2011-04-11 | Plug / Plug Back | No Violations | An inspection revealed 4.5 casing being pulled from the wellbore. |
PL13814 | PL | No Violations |
For data sources see[9]