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Well ID: 34-089-24839 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Perry Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: WRIGHT GEORGE | |
License Status: Producing | |
License Date: 1983-10-13 | |
Spud Date: 1983-11-15 | |
Spud Drilling Contractor: JAMES MORAN DRLG | |
Final Drill Date: 1983-12-10 | |
Well Total Depth: 2948.00 ft | |
Configuration: Vertical | |
Latitude: 40.120000 | |
Longitude: -82.270000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-10-13 | Issued Date 10/13/83 Expired Date 4/10/84 Acres 0020600 Tool Type CT Proposed Formation CLINTON Proposed Depth 02948 Proposed Drill Depth 02948 |
Original Spud | 1983-11-15 | FDT=SHALE BELOW CL. CHANGED STATUS OF WELL FROM FR TO PR PER EMAIL FROM B. MITCHELL *SEE EMAIL IN FILE DATED 6/19/2018 ON 6/20/2018 CM. |
Completed | 1983-12-10 | FDT=SHALE BELOW CL. CHANGED STATUS OF WELL FROM FR TO PR PER EMAIL FROM B. MITCHELL *SEE EMAIL IN FILE DATED 6/19/2018 ON 6/20/2018 CM. |
Reached Total Depth | 1983-12-10 | FDT=SHALE BELOW CL. CHANGED STATUS OF WELL FROM FR TO PR PER EMAIL FROM B. MITCHELL *SEE EMAIL IN FILE DATED 6/19/2018 ON 6/20/2018 CM. |
CO | 1983-12-20 | 447 DUGAN HARRY OIL CO GeoDate 10/13/83 |
Completion Report Received | 1984-01-06 | FDT=SHALE BELOW CL. CHANGED STATUS OF WELL FROM FR TO PR PER EMAIL FROM B. MITCHELL *SEE EMAIL IN FILE DATED 6/19/2018 ON 6/20/2018 CM. |
Construction Permit Expires | 1984-04-10 | FDT=SHALE BELOW CL. CHANGED STATUS OF WELL FROM FR TO PR PER EMAIL FROM B. MITCHELL *SEE EMAIL IN FILE DATED 6/19/2018 ON 6/20/2018 CM. |
Change of Owner | 2018-06-22 | Operator changed from 447, DUGAN HARRY OIL CO to 1634, NORTHWOOD ENERGY CORP |
Record Last Modified | 2018-06-22 | FDT=SHALE BELOW CL. CHANGED STATUS OF WELL FROM FR TO PR PER EMAIL FROM B. MITCHELL *SEE EMAIL IN FILE DATED 6/19/2018 ON 6/20/2018 CM. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 2888 | 2934 | 0 |
2888 | 2934 | 0 | |
2888 | 2934 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1700 Bbl | 42000 | FRAC;H2O,SAND,ACID |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | DUGAN HARRY OIL CO | 309.00 | 163.00 | 365 |
1991 | DUGAN HARRY OIL CO | 162.00 | 137.00 | 365 |
1992 | DUGAN HARRY OIL CO | 0.00 | 97.00 | 365 |
1993 | DUGAN HARRY OIL CO | 0.00 | 73.00 | 365 |
1994 | H I SMITH OIL & GAS INC | 0.00 | 0.00 | 0 |
1996 | H I SMITH OIL & GAS INC | 2000.00 | 0.00 | 260 |
1997 | H I SMITH OIL & GAS INC | 1318.00 | 0.00 | 260 |
1998 | H I SMITH OIL & GAS INC | 1321.00 | 0.00 | 260 |
1999 | H I SMITH OIL & GAS INC | 300.00 | 63.00 | 365 |
2000 | H I SMITH OIL & GAS INC | 916.00 | 0.00 | 365 |
2001 | H I SMITH OIL & GAS INC | 383.00 | 63.00 | 365 |
2002 | H I SMITH OIL & GAS INC | 260.00 | 47.00 | 365 |
2003 | H I SMITH OIL & GAS INC | 1503.00 | 0.00 | 365 |
2004 | H I SMITH OIL & GAS INC | 1335.00 | 0.00 | 365 |
2005 | H I SMITH OIL & GAS INC | 1016.00 | 0.00 | 365 |
2006 | H I SMITH OIL & GAS INC | 66.00 | 0.00 | 365 |
2007 | EQUITY OIL & GAS FUNDS INC | 415.00 | 65.00 | 365 |
2008 | H I SMITH OIL & GAS INC | 20.00 | 0.00 | 0 |
2010 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2011 | NORTHWOOD ENERGY CORP | 0.00 | 61.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 0.00 | 22.00 | 366 |
2013 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2014 | NORTHWOOD ENERGY CORP | 0.00 | 34.00 | 365 |
2015 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2016 | NORTHWOOD ENERGY CORP | 0.00 | 32.00 | 365 |
2017 | NORTHWOOD ENERGY CORP | 0.00 | 25.00 | 365 |
2018 | NORTHWOOD ENERGY CORP | 0.00 | 20.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-321459635 | 2012-9-14 0:00: | PW | No Violations | |
0000DP4672 | Final Restoration | No Violations | Final Restoration done information from Data Point | |
0321459635 | 2012-09-14 | Production Wells | No Violations | The Division received a landowner request to provide assistance with the identification of approximately seventeen (17) well locations on the property. The landowners son, Mr. James Wright, stated they are paying taxes on all wells, but own only the wells equipped with pump jacks. An inspection of this Clinton well conducted with Mr. Wright revealed that the well was idle and showed no signs of recent production. Mr. Wright stated they do not own this well, but remembered that someone installed the pumping unit approximately 10 years ago. The well consisted of rods, tubing, casing with a wellhead and a pumping unit with no engine. According to Mr. Wright, the tank battery is located on their adjacent property. The valve was open on the pumping tee side of the well, but RBDMS records showed no commercial production since 1993. The well did not produce house gas and was also inaccurately listed as FR under Owner No. 447, Harry Dugan Oil Co. Mr. Wright stated that they have an oil and gas lease with Northwood Energy and believed they may have acquired this well. The well location will be researched and verified with Central Office. |
1529334348 | 2018-06-18 | Production Wells | No Violations | My inspection revealed that the well was equipped with a pumping unit. It was covered in brush and vegetation in which the only counterweights of the pumping unit were visible. This well produces into a shared tank battery with API permit number 4748. I spoke with Mr. Bill Arnholt of Northwood Energy on 6/15/2018 regarding this well. Mr. Arnholt claims this well belongs to Northwood Energy. The well is currently registered to Harry Dugan Oil Co. I believe when Northwood Energy took ownership of this well the API number 4776 was incorrectly used for the transfer as it has the same well name of George Wright #2. The George Wright #2 (API number 4776) is registered to Northwood Energy but I was told that it is owned by Derrick Petroleum. This well will need to be registered to Northwood Energy and API number 4776 shall be registered to Derrick Petroleum. I left a voicemail message for Bill Arnholt at 11:52 AM requesting to meet him at the George Wright tank battery. Time of inspection: 10:00 AM. Weather: 83 degrees F, Sunny |
DP4672 | FR | No Violations |
For data sources see[9]