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34-089-25274

Well Details

Well ID: 34-089-25274
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Country: United States
State: Ohio
County: Licking
Municipality: Perry Township
Operator Name: MORAN RONALD F
Well Pad ID:
Farm/Lease Name: STEVENS
License Status: Final Restoration
License Date: 2019-01-18
Spud Date: 1987-01-16
Spud Drilling Contractor: R & J DRILLING
Final Drill Date: 1987-02-14
Well Total Depth: 2846.00 ft
Configuration: Vertical
Latitude: 40.150000
Longitude: -82.220000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1986-12-31 Issued Date 12/31/86 Expired Date 12/31/87 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02846 Proposed Drill Depth 02846
Original Spud 1987-01-16 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE. GMM UPDATED PLUG SATUS PER PLUG REPORT
Completed 1987-02-14 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE. GMM UPDATED PLUG SATUS PER PLUG REPORT
Reached Total Depth 1987-02-14 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE. GMM UPDATED PLUG SATUS PER PLUG REPORT
CO 1987-02-20 496 CENTRAL ENERGY CO INC GeoDate 12/31/86
Completion Report Received 1987-05-01 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE. GMM UPDATED PLUG SATUS PER PLUG REPORT
Change of Owner 2003-12-17 Operator changed from 496, CENTRAL ENERGY CO INC to 565, MORAN RONALD F
APP 2019-01-18 Proposed Formations:CLINTON SAND, Issued Date:1/18/2019, Expired Date:1/17/2021 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2019-04-10 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE. GMM UPDATED PLUG SATUS PER PLUG REPORT
Record Last Modified 2019-06-05 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE. GMM UPDATED PLUG SATUS PER PLUG REPORT
Construction Permit Expires 2021-01-17 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE. GMM UPDATED PLUG SATUS PER PLUG REPORT

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2798 2846 0
2798 2846 0
2798 2846 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1800 Bbl 23000 FRAC W/1800 BW & 23M# SAND
ACID 15 100 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 MORAN RONALD F 302.00 948.00 365
1988 MORAN RONALD F 168.00 512.00 365
1989 MORAN RONALD F 144.00 287.00 365
1990 MORAN RONALD F 0.00 147.00 365
1991 MORAN RONALD F 29.00 119.00 365
1995 MORAN RONALD F 0.00 0.00 0
1996 MORAN RONALD F 0.00 0.00 0
1997 MORAN RONALD F 0.00 0.00 365
1998 MORAN RONALD F 0.00 0.00 365
1999 MORAN RONALD F 0.00 0.00 365
2000 MORAN RONALD F 0.00 0.00 365
2001 MORAN RONALD F 0.00 0.00 0
2002 MORAN RONALD F 0.00 0.00 0
2003 MORAN RONALD F 0.00 0.00 0
2004 MORAN RONALD F 0.00 0.00 0
2005 MORAN RONALD F 0.00 0.00 365
2012 MORAN RONALD F 0.00 0.00 366
2013 MORAN RONALD F 0.00 0.00 365
2014 MORAN RONALD F 0.00 0.00 365
2015 MORAN RONALD F 0.00 0.00 365
2016 MORAN RONALD F 0.00 0.00 366
2017 MORAN RONALD F 0.00 0.00 365
2018 MORAN RONALD F 0.00 32.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 MORAN RONALD F Brine 440 365
1988 MORAN RONALD F Brine 60 365
1989 MORAN RONALD F Brine 40 365
1990 MORAN RONALD F Brine 80 365
1991 MORAN RONALD F Brine 0 365
1995 MORAN RONALD F Brine 0 0
1996 MORAN RONALD F Brine 0 0
1997 MORAN RONALD F Brine 0 365
1998 MORAN RONALD F Brine 0 365
1999 MORAN RONALD F Brine 0 365
2000 MORAN RONALD F Brine 0 365
2001 MORAN RONALD F Brine 0 0
2002 MORAN RONALD F Brine 0 0
2003 MORAN RONALD F Brine 0 0
2004 MORAN RONALD F Brine 0 0
2005 MORAN RONALD F Brine 0 365
2012 MORAN RONALD F Brine 0 366
2013 MORAN RONALD F Brine 37 365
2014 MORAN RONALD F Brine 120 365
2015 MORAN RONALD F Brine 160 365
2016 MORAN RONALD F Brine 280 366
2017 MORAN RONALD F Brine 232 365
2018 MORAN RONALD F Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1491577734 2019-3-26 0:00: PB No Violations 1.90
-1666039439 2019-4-10 0:00: PB No Violations 0.30
-424348466 2019-4-23 0:00: PB No Violations 0.20
-657080117 2019-3-15 0:00: PB No Violations 1.30
-876574898 2019-6-18 0:00: FR No Violations 0.10
000PL13537 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0424348466 2019-04-23 Plug / Plug Back No Violations My inspection revealed that the casing was still open. The clay plug has not settled. I called Randi Moran during the inspection. Randi said he would put a plate on the casing this week and bury the well. Time of inspection: 10:50 AM. Weather: 72 degrees F, Cloudy
0657080117 2019-03-15 Plug / Plug Back No Violations My inspection revealed that Randi Moran has put his service rig on this well to have it plugged. During the inspection Randi was pulling tubing. I observed a pile of clay next to the well. Randi said he would start washing in clay on 3/18/2019. Time of inspection: 9:45 AM. Weather: 47 degrees F, Overcast
0688223380 2017-03-21 Production Wells No Violations This inspection was conducted as a status check. The well was equipped with a pumping unit and motor. It was pumping during inspection. The tank battery consists of (2) 100 barrel tanks, (1) 500 gallon plastic brine tank, and separator. Identification was observed at the well and tank battery. No violations. Time of inspection: 1:35 PM. Weather: 54*F, Sunny
0762463716 2019-04-03 Plug / Plug Back No Violations My inspection revealed that the well will need to be topped off with clay. I observed fluid in the well approximately 10 feet down. No personnel were present during my inspection. Time of inspection: 2:15 PM. Weather: 60 degrees F, Sunny
1197553669 2019-8-20 0:00: FR No Violations 0.30
1291107606 2019-05-06 Final Restoration No Violations My inspection revealed that the casing has been buried and the well location graded. I observed that the tank battery location and well location contained a significant amount of gravel. I contacted Ron Moran at 11:30 AM and advised him that the gravel needs to be removed. Mr. Moran agreed and said he would take care of it. Time of inspection: 10:40 AM.
1491577734 2019-03-26 Plug / Plug Back No Violations I arrived to the well to witness plugging operations today. Randi Moran ran tools in the well to tag the cement plug. It was revealed that the plug dropped approximately 300 feet. The top of the plug was tagged at approximately 800 feet. A plug job was set up for 3:00 PM to set another plug across the Berea. Time of inspection: 9:50 AM.
1553004909 2019-03-18 Plug / Plug Back No Violations I witnessed Randi Moran wash in 150 shovels of clay in the well. Randi said he would rip the 4.5 inch pipe the following morning. Refer to plug report for details. Time of inspection: 2:20 PM.
1553526579 2019-03-25 Plug / Plug Back No Violations I witnessed plugging operations on this well today. In accordance with 1501:9-11-08 (A)(2) a cement plug was set across the Berea. Cemenco pumped 60 sacks of Class A cement through tubing for a 200 foot plug. Refer to plug report for details. Time of inspection: 8:25 AM. Weather: 41 degrees F, Rain
1568204647 2019-9-11 0:00: FR No Violations 0.20
1666039439 2019-04-10 Plug / Plug Back No Violations During my inspection I observed clay at the surface. Randi Moran was removing the lead line during the inspection. The tank battery has been removed as well as all the production equipment. Randi said he would weld a plate onto the casing. The well has been plugged. Time of inspection: 1:45 PM. Weather: 59 degrees F, Mostly sunny
1676549052 2019-7-15 0:00: FR No Violations 0.20
1935387185 2018-11-26 Production Wells No Violations My inspection revealed that the well was equipped with a pumping unit and motor. The well produces into a shared tank battery with API permit number 5273. The tank battery consists of (2) 100 barrel tanks, a plastic brine tank, and separator. During the inspection the landowner Mr. Brad Stevens arrived. Mr. Stevens told me that the well has not produced in over 3 years. The polish rod was dull and did not indicate recent signs of production. According to RBDMS records the last year for reported commercial production was 1991. The well owner/operator shall submit a written plugging schedule to Brandon Mitchell at 5880 Memory Road Zanesville, Ohio 43701-9553 within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. I contacted well owner Ron Moran at 11:38 AM and advised him of my findings. Time of inspection: 10:45 AM. Weather: 38 degrees F, Overcast
2007790963 2019-03-26 Plug / Plug Back No Violations I witnessed plugging operations on this well today. Randi Moran ran 650 feet of 2.38 inch tubing in the well. Cemenco pumped 60 sacks of Class A cement through tubing for a 200 foot plug. Time of inspection: 2:55 PM. Weather: 47 degrees F, Sunny
2144585258 2019-03-19 Plug / Plug Back No Violations I witnessed plugging operations on this well today. Refer to plug report for details. Time of inspection: 9:45 AM.
688223380 2017-3-21 0:00: PW No Violations
762463716 2019-4-3 0:00:0 PB No Violations 0.30
PL13537 PL No Violations

For data sources see[9]

References