If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-089-25833 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.22,"lon":-82.5,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Burlington Township | |
Operator Name: KNOX ENERGY INC. | |
Well Pad ID: | |
Farm/Lease Name: LIGGETT W | |
License Status: Producing | |
License Date: 2006-11-14 | |
Spud Date: 2007-01-09 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2007-01-15 | |
Well Total Depth: 2353.00 ft | |
Configuration: Vertical | |
Latitude: 40.220000 | |
Longitude: -82.500000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2006-11-14 | Proposed Formations:OHIO SHALE THRU CLINTON, Issued Date:11/14/2006, Expired Date:11/14/2007 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2007-01-15 | |
Reached Total Depth | 2007-01-15 | |
Completion Report Received | 2007-07-09 | |
Construction Permit Expires | 2007-11-14 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2007-10-29 | 2186 | 2210 | 49 |
2186 | 2210 | 49 | |
2186 | 2210 | 49 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 46000 Gal | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | KNOX ENERGY INC. | 15465.00 | 0.00 | 259 |
2008 | KNOX ENERGY INC. | 28939.00 | 0.00 | 365 |
2009 | KNOX ENERGY INC. | 15851.00 | 61.00 | 365 |
2010 | KNOX ENERGY INC. | 18884.00 | 0.00 | 365 |
2011 | KNOX ENERGY INC. | 17914.00 | 0.00 | 365 |
2012 | KNOX ENERGY INC. | 17052.00 | 0.00 | 366 |
2013 | KNOX ENERGY INC. | 12633.00 | 0.00 | 365 |
2014 | KNOX ENERGY INC. | 9506.00 | 0.00 | 365 |
2015 | KNOX ENERGY INC. | 8519.00 | 0.00 | 365 |
2016 | KNOX ENERGY INC. | 8437.00 | 0.00 | 365 |
2017 | KNOX ENERGY INC. | 6865.00 | 0.00 | 365 |
2018 | KNOX ENERGY INC. | 4748.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | KNOX ENERGY INC. | Brine | 60 | 259 |
2008 | KNOX ENERGY INC. | Brine | 30 | 365 |
2009 | KNOX ENERGY INC. | Brine | 0 | 365 |
2010 | KNOX ENERGY INC. | Brine | 0 | 365 |
2011 | KNOX ENERGY INC. | Brine | 0 | 365 |
2012 | KNOX ENERGY INC. | Brine | 0 | 366 |
2013 | KNOX ENERGY INC. | Brine | 0 | 365 |
2014 | KNOX ENERGY INC. | Brine | 0 | 365 |
2015 | KNOX ENERGY INC. | Brine | 0 | 365 |
2016 | KNOX ENERGY INC. | Brine | 0 | 365 |
2017 | KNOX ENERGY INC. | Brine | 0 | 365 |
2018 | KNOX ENERGY INC. | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2130266097 | 2007-5-4 0:00:0 | PL | No Violations | |
-305078062 | 2007-1-11 0:00: | DD | No Violations | |
0305078062 | 2007-01-11 | Drill / Deepen / Reopen | No Violations | Went to well site to inspect the cementing of the surface casing. The job was postponed due to the 8 inch being plugged up. They pulled the eight inch, will re-drill, and will call me when ready to cement. |
1051569497 | 2007-01-12 | Drill / Deepen / Reopen | No Violations | This mornings surface cement job was called off due to water flow and sand plugging up the surface casing as they were running it. They pulled the 8 inch and drilled it out again. At 4:30 pm they had there surface casing in the ground and ready to cement. Formation Cementing set the casing with 251 sacks of cement. There was good cement returns to the surface. |
1201025296 | 2007-12-11 | Preliminary Restoration | No Violations | |
2085271039 | 2007-08-08 | Preliminary Restoration | No Violations | The inspection revealed that the well is located in an agricultural field. The area has been properly graded and soy beans are growing. The tank battery consists of a 200 barrel tank and a separator contained in an earthen dike. There is proper display of identification at the tank battery. Preliminary Restoration passed. |
2130266097 | 2007-05-04 | Preliminary Restoration | No Violations | nspection reveled that all pits have been filled. The area has been properly graded. The tank battery consists of a separator and a 100 barrel tank in a gravel lined dike. There is a pumping unit on the well and the well is in production. There is no identification posted at the wellhead or the tank battery. |
For data sources see[9]