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34-091-20074

Well Details

Well ID: 34-091-20074
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Country: United States
State: Ohio
County: Logan
Municipality: Stokes Township
Operator Name: CHATHAM ASSOCIATES
Well Pad ID:
Farm/Lease Name: WARNECKE MELETUS
License Status: Historical Production Well
License Date: 1965-09-08
Spud Date: 1965-09-08
Spud Drilling Contractor:
Final Drill Date: 1965-09-20
Well Total Depth: 1500.00 ft
Configuration: Vertical
Latitude: 40.520000
Longitude: -83.910000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1965-09-08 IN ORPHAN WELL DATABASE, BUT INCOMPLETE. WELL IS OWNED BY STREAM GLOBAL INVESTMENTS LLC, AS OF 10/28/2004, UNREGISTERED OWNER. I&O CASE # 1991 04 119.
Completed 1965-09-20 IN ORPHAN WELL DATABASE, BUT INCOMPLETE. WELL IS OWNED BY STREAM GLOBAL INVESTMENTS LLC, AS OF 10/28/2004, UNREGISTERED OWNER. I&O CASE # 1991 04 119.
Reached Total Depth 1965-09-20 IN ORPHAN WELL DATABASE, BUT INCOMPLETE. WELL IS OWNED BY STREAM GLOBAL INVESTMENTS LLC, AS OF 10/28/2004, UNREGISTERED OWNER. I&O CASE # 1991 04 119.
Completion Report Received 1965-09-23 IN ORPHAN WELL DATABASE, BUT INCOMPLETE. WELL IS OWNED BY STREAM GLOBAL INVESTMENTS LLC, AS OF 10/28/2004, UNREGISTERED OWNER. I&O CASE # 1991 04 119.
CO 1982-11-01 Owner change from ROUNDHEAD GAS CO., INC to 1635 CHATHAM ASSOCIATES
Record Last Modified 2017-02-15 IN ORPHAN WELL DATABASE, BUT INCOMPLETE. WELL IS OWNED BY STREAM GLOBAL INVESTMENTS LLC, AS OF 10/28/2004, UNREGISTERED OWNER. I&O CASE # 1991 04 119.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1410 1500 0
1410 1500 0
1410 1500 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 1200 Lbs 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2082316155 2017-7-18 0:00: PW No Violations
1526486385 2018-05-16 Production Wells No Violations Received a phone call from Mr. Warnecke about orphan well on mothers property. Researched and inspected well and well is currently registered to Chatham Associates. There is currently Chiefs Order # 2018-116 on this well and also on all the other wells owned by Chatham Associates. Explained to Mr. Warnecke that well is not capable of production at the present time and also it is illegal to operate the well at the present time. He would like to either have the well plugged or be able to use it again for domestic purposes.
2082316155 2017-07-18 Production Wells No Violations Well construction of this well consist of an 8.25 inch conductor casing and a 6.625 inch surface casing extending approximately 20 inches above ground. The well does not have any rods and tubing and the 6.625 inch surface casing is reduced to 2 inch with a closed manual valve . There is numerous regulators and valves around wellhead and a 2 inch production line possibly leading to storage tank. The storage tank is approximately a 30 Bbl. rusted steel tank with a large hole cut into top. There is approximately 12 inches of water and an oily substance in bottom of tank. Cannot verify who is actually the owner of this well at the present time with the images provided. No leakage observed around well or tank area.

For data sources see[5]

References