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Well ID: 34-093-60473 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: FJD PROPERTIES LLC | |
Well Pad ID: | |
Farm/Lease Name: FJD PROPERTIES LLC (WINCKLES) | |
License Status: Final Restoration | |
License Date: 2014-01-17 | |
Spud Date: 1941-10-09 | |
Spud Drilling Contractor: | |
Final Drill Date: 1941-11-06 | |
Well Total Depth: 2478.00 ft | |
Configuration: Vertical | |
Latitude: 41.390000 | |
Longitude: -82.030000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1941-10-09 | UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052. |
Completed | 1941-11-06 | UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052. |
Reached Total Depth | 1941-11-06 | UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052. |
Correction to Well | 2007-09-28 | UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052. |
Change of Owner | 2014-01-13 | Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM |
APP | 2014-01-17 | Proposed Formations:SHALE, Issued Date:1/17/2014, Expired Date:1/17/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2014-02-12 | Operator changed from 40004, COTTRELL AARON to 40005, FJD PROPERTIES LLC |
Change of Owner | 2014-02-12 | Operator changed from 8318, ORPHAN WELL PROGRAM to 40004, COTTRELL AARON |
Plugged by Orphan Well Program | 2014-03-07 | Plugged by Orphan Well Program |
Plugged/Abandoned | 2014-03-07 | UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052. |
Construction Permit Expires | 2016-01-17 | UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052. |
Record Last Modified | 2017-02-10 | UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052. |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1170796367 | 2008-8-6 0:00:0 | OR | No Violations | 1.00 |
-1193531815 | 2014-2-18 0:00: | PB | No Violations | |
-1739275544 | 2014-2-19 0:00: | OR | No Violations | |
-1981808815 | 2015-12-31 0:00 | FR | No Violations | 2.00 |
-2011015490 | 2014-3-4 0:00:0 | OR | No Violations | 8.00 |
-253263923 | 2014-2-6 0:00:0 | OR | No Violations | |
-464544559 | 2014-3-3 0:00:0 | OR | No Violations | |
-46932437 | 2014-2-13 0:00: | OR | No Violations | |
-638603913 | 2014-2-11 0:00: | PB | No Violations | |
-64861059 | 2014-2-12 0:00: | PB | No Violations | |
-849949934 | 2014-2-12 0:00: | OR | No Violations | |
-964372000 | 2014-2-10 0:00: | PB | No Violations | |
0046932437 | 2014-02-13 | Orphan | No Violations | A follow-up inspection was conducted on 02/13/2014 for contract compliance.
1. Excavating continues and contractor is placing the excavated clay material in the northwest stockpile. 2. Sewer line was removed and the water is continuing to flow from the gravel base of the sewer ditch.
Note: Keeping Mark Bruce (ODNR Communication Department) apprised of progress at the site. END |
0064861059 | 2014-02-12 | Plug / Plug Back | No Violations | Visited location on 02/12/2014 with Norburt Lowder to check on status of excavation operations and discuss plan forward. At time of visit, Whipstock Drilling was excavating at approximately 15 below ground level. |
0253263923 | 2014-02-06 | Orphan | No Violations | Shut down due to subzero weather. |
0464544559 | 2014-03-03 | Orphan | No Violations | A follow-up inspection was conducted on 03/03/2014 for contract compliance.
1.Equipment freezing up due to the subzero weather. 2. Started to clean out at 13:00 hrs, working on the obstruction at 60 using a 4.3750 tri cone bit. At first the circulating fluid was clear but then it turned to a blackish color. Drilled down to 76. 3. Circulating out large pieces of Red Bedford Shale, due to fresh water that is being used to circulate. 4. Shut down for the day at 16:00 hrs. END |
0638603913 | 2014-02-11 | Plug / Plug Back | No Violations | Visited location on 02/11/2014 with Norburt Lowder to check on status of excavation. Whipstock Drilling is continuining to excavate down to wellhead. At the time of the visit, they were at approximately 12 down from ground level. |
0849949934 | 2014-02-12 | Orphan | No Violations | A follow-up inspection was conducted on 02/12/2014 for contract compliance.
1. A replacement pump arrived and was placed close to the vault so the water can be pumped from it. Once the waterwas pumped out of the well vault and the casing was exposed, the gas leakage from the well diminished. No gas was detected in excavation, however elevated gas readings were detected in the vault. 2. Whipstock completed excavation down to the sewer line (approximately
3. The sewer contractors arrived to determine if the lines needed to be removed or worked around it. They decided to remove it.
END |
0964372000 | 2014-02-10 | Plug / Plug Back | No Violations | Visited location on 02/10/2014 with Norburt Lowder to check-on status of excavation operations. Whipstock Drilling excavating at approximately 6 below ground level to reach wellhead. |
0972176465 | 2014-02-15 | Orphan | No Violations |
RECORD OF CONVERSATION ON 02/15/2014 Phone call received from Chris Corso (Whipstock) advising me they collar. He also noted that marks were present on the casing that appeared to be from the teeth of a large track hoe bucket. No work will be done on Sunday 02/16/2014. END |
1157642099 | 2006-09-07 | Orphan | No Violations | Case # I&O 06-004, Met with Chris Teater to locate leaking gas well on housing development property at 37000 Center Ridge Rd. in North Ridgeville. Located a concrete column 23 underground with gas bubbling thru center of concrete column at 100% lel.. There is casing inside concrete but not sure of diameter. From photos it is 5 casing and it is bent over in bottom of 60 corregated plastic pipe over well . Construction company located gas leaking during removal of trees. Concrete around well will have to be chipped away to determine casing size. No houses are around well location at this time but construction to begin in October 2006. Sun, 70 degrees. |
1170796367 | 2008-08-06 | Orphan | No Violations | I&O case # 06-004 Chris Teeter. Requested by Mike McCormac to inspect well site for orphan well program. Well is in a new development and houses are getting closer to well site since last materix evaluation. Well has increased in gas leakage to 100 % lel 5 above well. My recommendation would be to plug the well this fall, to eliminate costs, due to hazards near a house. Nearest home now is 500 in diameter. I am submitting a new matrix to Mike McCormac. Dry, sun, 85 degrees. |
1193531815 | 2014-02-18 | Plug / Plug Back | No Violations | Visited location 0n 02/18/2014 to check-on status of excavation operations and assist with filming of ODNR video with Norburt Lowder. |
1306816129 | 2014-03-26 | Final Restoration | No Violations | A follow-up inspection was conducted on 03/26/2014 for contract compliance.
1) This well is located in the next phase of a housing development of K. Hovnanian Homes. This well is on the south side of Tailfeather Drive, in the block of address 1088 to 1091. There is no paved street in this area yet. The housing contractor has installed the water and sewer main lines and several lateral lines. |
1340797127 | 2012-06-22 | Orphan | No Violations | On this inspection, I was uUnable to locate the well site. |
1391692683 | 2014-02-03 | Orphan | No Violations | Inspection on 02/03/2014 was conducted for contract compliance.
1. The snow was removed from the area to be excavated. Corso, Whipstock Superintendent, to put orange flagging on each fence post and KEEP OUT 3. Excavating was started around well vault (black culvert). The projected excavation will be 4. All excavated material will be stockpiled at the perimeter of the site. The first stockpile will be located in the southwest corner. Note: a. The Sewer line, which had been installed by the developer of the complex, is located approximately 10-15 to the south of the well vault and at a depth of 18. the north of well, will need to be removed to continue excavating. END |
1392649672 | 2014-02-10 | Orphan | No Violations |
A follow-up inspection; 02/10/2014 was conducted for contract compliance. 1.Whipstock is still excavating and stockpiling this material at the northwest corner of the location. This material will be used to backfill the excavation. 2.Water is entering the excavation from the gravel fill at the base of the sewer line. A dewatering ditch was excavated along southern edge of the excavation to direct the water to the sump which is located in the southwest corner of the excavation. END |
1392779866 | 2014-02-13 | Orphan | No Violations | Crews from Whipstock are in the process of excavating the existing overburden to allow access to the damaged remaining casing of the well. Work is ongoing and work at the wellhead will not take place until later in the week. |
1393248892 | 2014-02-05 | Orphan | No Violations | Shut down due to sudzero weather. |
1393337156 | 2014-02-07 | Orphan | No Violations | No on site inspection done on 02/07/2014.
Shut down due to subzero weather. |
1394469632 | 2014-03-10 | Orphan | No Violations | Plugging and abandonment operations are being completed. Cementing was completed on Friday 3/7/14. The cement is firm and set at a nominal 24 inches below the top of the casing collar. Whipstock crews indicated that the plan is to cut the casing off at 4 feet below the existing grade and install a short section of black, corrugated drain pipe around the well once the cap is welded on with ID#. I inspected both the cement in the casing and samples of the cement retained in cups. Both look firm and solid. No gas detected via meter. I collected a GPS location data as well as triangulation measurements from selected locations for future reference. |
1395242127 | 2014-02-20 | Orphan | No Violations |
A follow-up inspection was conducted on 02/20/2014 for contract compliance. 1. Sewer Contractors on site reinstalling the sewer line.
END |
1513686661 | 2014-02-04 | Orphan | No Violations |
A follow-up inspection was conducted on 02/04/2014 for contract compliance.
2. The water line on the north side of the excavation, that was installed by the developer was exposed.Whipstock contacted the developer to shut water off. east and west sides of the excavation. Note: When Whipstock was excavating in the area of the sewer line, which was previously installed by the developer, they encountered black material that appeared to be high in organic matter (corn stalks, vegtation, tree limbs and roots). Whipstock segregated this material and stockpiled it in the southwest corner of the location. This material will not be used as back fill. END |
1541231752 | 2014-03-20 | Plug / Plug Back | No Violations | Visited well on 03/20/2014 to determine the status of the location at the request of Norburt Lowder. All rig-related equipment has been removed, and the location has been rough-graded. A 12 plastic culvert pipe is around the well, sticking out of the ground ~2. The water level within the pipe is down ~4 from the top of the pipe. Occasional bubbles were noted in the water in the pipe. |
1608252901 | 2014-03-05 | Plug / Plug Back | No Violations | Visited location on 03/05/2014 to observe plugging operations with Norburt Lowder. Whipstock Drilling had run in the hole with tubing to circulate out old oil in the hole. Will tag bottom with tubing and then prepare to plug out the well. |
1739275544 | 2014-02-19 | Orphan | No Violations |
A follow-up inspection was conducted on 02/19/2014 for contract compliance. 1. Plugging equipment removed from site. 2. Excavation was backfilled and compacted in 8-10 lifts. 3. Site is ready for the Sewer Contractor to reinstall the sewer lines.
END. |
1894238965 | 2014-02-11 | Orphan | No Violations | A follow-up inspection was conducted on 02/11/2014 for contract compliance.
1. Pump problems due to sub-zero weather. 2. Whipstock continues to excavate and this material is being stockpiled at the northwest perimeter. Note: Cody Bruce, of FJD/Hovnanian Homes, arrived on site. He inquired about how the excavation will be backfilled. I advised him to contact Gene Chini, Orphan Well Manager, with any questions. |
1981808815 | 2015-12-31 | Final Restoration | No Violations | Collecting photographic evidence of final restoration. Final restoration is approved. |
2011015490 | 2014-03-04 | Orphan | No Violations | A follow-up inspection on 03/04/2014 was conducted for contract compliance.
1.Due subzero weather the equipment lines are freezing up. 2. Whipstock order 2 load saltwater from Cargill to add to circulating half tank to keep water from freezing. The salt water will help keep the Red Bedford from caving in on the drill stem. 3. Started to drill out with same bit 4.8750 on 2.3750 tubing at approximately 96.6 4. During drill out, at a depth of approximately 100, the well started to unload. The contractor slowed their pump down to keep well under control, letting the well flow into half tank. The initial flow back produced approximately 100 gallons of a thick black oil and then changed to black water with a strong petroleum odor. I notified Asst Fire Chief Bement (cell 440-653-6362) of the odor and that he might get complaints from the area. 5. I advised Whipstock crew to put a trap over half tank to keep the odor in. 6.The crew ran tubing to 225 and shut down for the day. END |
2139366242 | 2014-03-07 | Orphan | No Violations | I conducted this follow-up inspection on 03/07/2014 for contract compliance.
1.Confirmed that the half tank, to be used to contain flow back from the plugging, was delivered. 2. Tubing was run for first plug (1334 to 850) will cement with 110 sacks of Class A cement. 3. Gel will be from 850 to 400. 4. Cement plug from 400 to surface with 160 sacks of Class A cement. END |
972176465 | 2014-2-15 0:00: | OR | No Violations |
For data sources see[3]