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Well ID: 34-099-20366 | Loading map...
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Country: United States | |
State: Ohio | |
County: Mahoning | |
Municipality: Goshen Township | |
Operator Name: DORFMAN PRODUCTION COMPANY | |
Well Pad ID: | |
Farm/Lease Name: LUNGOCIU UNIT | |
License Status: Producing | |
License Date: 1973-10-04 | |
Spud Date: 1973-10-25 | |
Spud Drilling Contractor: | |
Final Drill Date: 1973-11-16 | |
Well Total Depth: 5427.00 ft | |
Configuration: Vertical | |
Latitude: 40.940000 | |
Longitude: -80.940000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1973-10-04 | 182 BELDEN & BLAKE CO GeoDate 10/4/73 |
Original Spud | 1973-10-25 | IP. A.F. 17 BOPD 9 1ST WK.) |
Completed | 1973-11-16 | IP. A.F. 17 BOPD 9 1ST WK.) |
Reached Total Depth | 1973-11-16 | IP. A.F. 17 BOPD 9 1ST WK.) |
Change of Owner | 2002-08-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
Change of Owner | 2002-08-20 | Operator changed from 1966, PETROX INC to 180, DORFMAN PRODUCTION COMPANY |
Record Last Modified | 2013-10-03 | IP. A.F. 17 BOPD 9 1ST WK.) |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5249 | 5279 | 0 |
5249 | 5279 | 0 | |
5249 | 5279 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 126000 Gal | 70000 | |||
ACID | 15 | 500 Gal | 0 | @ 1850 PSI, MAX. @ 3200 PSI, AVG. RATE46 BPM |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | WITCO CORP | 1113.00 | 530.00 | 365 |
1985 | WITCO CORP | 796.00 | 434.00 | 365 |
1986 | WITCO CORP | 967.00 | 433.00 | 365 |
1987 | BELDEN & BLAKE CORPORATION | 555.00 | 383.00 | 365 |
2001 | BELDEN & BLAKE CORPORATION | 163.00 | 0.00 | 229 |
2002 | BELDEN & BLAKE CORPORATION | 358.00 | 0.00 | 114 |
2003 | DORFMAN PRODUCTION COMPANY | 907.00 | 368.00 | 365 |
2004 | DORFMAN PRODUCTION COMPANY | 890.00 | 273.00 | 365 |
2005 | DORFMAN PRODUCTION COMPANY | 1117.00 | 238.00 | 365 |
2006 | DORFMAN PRODUCTION COMPANY | 842.00 | 193.00 | 365 |
2007 | DORFMAN PRODUCTION COMPANY | 951.00 | 259.00 | 365 |
2008 | DORFMAN PRODUCTION COMPANY | 1167.00 | 233.00 | 365 |
2009 | DORFMAN PRODUCTION COMPANY | 1126.00 | 231.00 | 365 |
2010 | DORFMAN PRODUCTION COMPANY | 1040.00 | 221.00 | 365 |
2011 | DORFMAN PRODUCTION COMPANY | 1167.00 | 209.00 | 365 |
2012 | DORFMAN PRODUCTION COMPANY | 981.00 | 198.00 | 366 |
2013 | DORFMAN PRODUCTION COMPANY | 1054.00 | 317.00 | 365 |
2014 | DORFMAN PRODUCTION COMPANY | 1275.00 | 288.00 | 365 |
2015 | DORFMAN PRODUCTION COMPANY | 1254.00 | 232.00 | 365 |
2016 | DORFMAN PRODUCTION COMPANY | 1245.00 | 192.00 | 365 |
2017 | DORFMAN PRODUCTION COMPANY | 1219.00 | 209.00 | 365 |
2018 | DORFMAN PRODUCTION COMPANY | 1308.00 | 181.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-108288297 | 2007-12-5 0:00: | PW | No Violations | |
-585727698 | 2016-10-13 0:00 | PW | No Violations | 2.00 |
001216i439 | 2002-04-25 | Production Wells | Violations Noted | The well is shut in and cannot be run at this time. Plug or produce the idle well. The lease name is Lungociu Unit #4. |
001216i599 | 2002-05-29 | Production Wells | Violations Noted | Well remains idle. Case pends. |
0089077679 | 2002-08-28 | Production Wells | No Violations | Well is now in production. Recommend case be resolved. |
0108288297 | 2007-12-05 | Production Wells | No Violations | I preformed a random field inspection. GPSd the tank battery and the wellhead. ID signs were posted. The tank battery was in good shape. I found no violations at this time. |
0503863827 | 2004-05-24 | Production Wells | No Violations | The tank battery was destroyed by fire and explosion caused by a lightning strike. The tank battery had been shared with permits: 318, 363 and 367 and consisted of 2-210 bbl storage tanks, 2-separators, 1-100 bbl salt water tank and a dike. |
0585727698 | 2016-10-13 | Production Wells | No Violations | I performed a follow up inspection on this location. I walked the length of the ditch from the impacted area to the siphoning dams. I did not notice any collected oil or residue in the water. I called Paul Shaw Field Forman for Dorfman Production to let him know that they could remove the dams. I instructed them to release the water slow as not to create a large flow of water and cause a flow of sediment down stream. |
1216i439 | 2002-4-25 0:00: | PW | No Violations | 0.50 |
1216i599 | 2002-5-29 0:00: | PW | No Violations | 0.50 |
1477057933 | 2016-10-13 | Production Wells | No Violations | I performed a follow up inspection on this location. I walked the Garfield Ditch that was impacted by the oil release 5 barrels (pipeline) that occurred on 7/21/2016. There is no noticeable oil or sheen at the siphon dams. I talked to Terry Whitehair North Region Emergence Response Coordinator about my findings and he was in agreement to call Dorfman Production and have them to remove the dams. |
503863827 | 2004-5-24 0:00: | PW | No Violations | 0.50 |
89077679 | 2002-8-28 0:00: | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
001216i439 | US-OH-105771 | 2002-04-25 | Well shall be plugged | |
001216i599 | US-OH-105798 | 2002-05-29 | Well shall be plugged |
For data sources see[9]