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Well ID: 34-099-20401 | Loading map...
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Country: United States | |
State: Ohio | |
County: Mahoning | |
Municipality: Milton Township | |
Operator Name: ERIC PETROLEUM CORP | |
Well Pad ID: | |
Farm/Lease Name: HULY RAY ETAL | |
License Status: Producing | |
License Date: 1973-11-12 | |
Spud Date: 1974-06-09 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-11-08 | |
Well Total Depth: 4760.00 ft | |
Configuration: Vertical | |
Latitude: 41.120000 | |
Longitude: -80.940000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1973-11-12 | 834 PATRICK PETROLEUM CORP GeoDate 11/12/73 |
Original Spud | 1974-06-09 | |
Completed | 1974-11-08 | |
Reached Total Depth | 1974-11-08 | |
Change of Owner | 2010-12-20 | Operator changed from 2936, CHESAPEAKE APPALACHIA LLC to 5054, ERIC PETROLEUM CORP. LAST PR WELL UNDER PATRICK PETROLEUM WHICH IS CANCELED. SUPPORTING DOCUMENTATION IN ERIC PET FILE. 12/20/10. |
Change of Owner | 2010-12-20 | Operator changed from 834, PATRICK PETROLEUM CORP to 2936, CHESAPEAKE APPALACHIA LLC |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4676 | 4758 | 17 |
4676 | 4758 | 17 | |
4676 | 4758 | 17 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 201 Mscf | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | COLUMBIA GAS TRANSMISSION LLC | 3683.00 | 0.00 | 0 |
1985 | COLUMBIA GAS TRANSMISSION LLC | 5762.00 | 72.00 | 362 |
1986 | COLUMBIA GAS TRANSMISSION LLC | 3786.00 | 0.00 | 269 |
1987 | COLUMBIA GAS TRANSMISSION LLC | 3843.00 | 16.00 | 215 |
1988 | COLUMBIA GAS TRANSMISSION LLC | 1425.00 | 19.00 | 365 |
1989 | CHESAPEAKE APPALACHIA LLC | 1503.00 | 56.00 | 56 |
1992 | CHESAPEAKE APPALACHIA LLC | 6848.00 | 49.00 | 365 |
1993 | CHESAPEAKE APPALACHIA LLC | 5233.00 | 69.00 | 365 |
1994 | CHESAPEAKE APPALACHIA LLC | 5218.00 | 27.00 | 362 |
1995 | CHESAPEAKE APPALACHIA LLC | 4924.00 | 32.00 | 368 |
1996 | CHESAPEAKE APPALACHIA LLC | 5199.00 | 0.00 | 342 |
1997 | CHESAPEAKE APPALACHIA LLC | 3449.00 | 0.00 | 364 |
1998 | CHESAPEAKE APPALACHIA LLC | 3640.00 | 0.00 | 363 |
1999 | CHESAPEAKE APPALACHIA LLC | 4280.00 | 0.00 | 364 |
2000 | CHESAPEAKE APPALACHIA LLC | 3727.00 | 0.00 | 365 |
2001 | CHESAPEAKE APPALACHIA LLC | 4958.00 | 0.00 | 364 |
2002 | CHESAPEAKE APPALACHIA LLC | 5080.00 | 0.00 | 368 |
2003 | CHESAPEAKE APPALACHIA LLC | 4356.00 | 0.00 | 366 |
2005 | CHESAPEAKE APPALACHIA LLC | 2926.00 | 0.00 | 365 |
2006 | CHESAPEAKE APPALACHIA LLC | 3017.00 | 0.00 | 365 |
2007 | CHESAPEAKE APPALACHIA LLC | 3526.00 | 41.00 | 347 |
2008 | CHESAPEAKE APPALACHIA LLC | 2353.00 | 306.00 | 365 |
2009 | CHESAPEAKE APPALACHIA LLC | 2628.00 | 0.00 | 365 |
2010 | ERIC PETROLEUM CORP | 0.00 | 0.00 | 365 |
2011 | ERIC PETROLEUM CORP | 3184.00 | 0.00 | 365 |
2012 | ERIC PETROLEUM CORP | 2730.00 | 34.00 | 366 |
2013 | ERIC PETROLEUM CORP | 3277.00 | 0.00 | 365 |
2014 | ERIC PETROLEUM CORP | 3089.00 | 0.00 | 365 |
2015 | ERIC PETROLEUM CORP | 1602.00 | 0.00 | 365 |
2016 | ERIC PETROLEUM CORP | 965.00 | 0.00 | 365 |
2017 | ERIC PETROLEUM CORP | 2967.00 | 0.00 | 365 |
2018 | ERIC PETROLEUM CORP | 2619.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2120760674 | 2015-10-7 0:00: | PW | No Violations | 1.00 |
0000015508 | Final Restoration | No Violations | PASSED Y WITNESSED 9/18/95 INSPECTOR KEITH WHITE DATE 09/1819/95 DATA FROM OLD VAX INFO | |
0004272348 | 2012-03-01 | Production Wells | Violations Noted | On the day of my inspection I met Rick Huffman of Eric Petroleum at the well site in order to witness the repair of the well head. Thompsons Well Service replaced the top joint of 2-3/8 tubing, as well as replacing the Demco valve, the rabbit catcher, and the ball valves. Thompsons then swabbed the excess fluid from the well. The gas leak is stopped and the well is now within compliance. The repairs satisfy ORC 1509.20 and OAC 1501.9-9-05(A)1. |
0469349334 | 2010-06-15 | Production Wells | No Violations | I performed a random field inspection. I GPSd both the tank battery and the wellhead. I continued to walk around both the wellhead and the tank battery. This inspection satisfies 1501:9-9-05. There were no violations at this time. |
0559500637 | 2018-12-18 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-0401. Inspector John Fleming was present during the inspection. RBDMS indicated reported production was current. Access remained drivable and stable. The 8.625 well head was above grade and open to atmosphere. The 4.5 production casing was equipped with a plunger lift assembly. Production valves were in the open position. No leaks were observed. The tank battery consisted of one (1) horizontal separator, one (1) 140 bbl production tank and one (1) 1100 gallon poly brine tank. The separator remained in good repair and contained a current 7 day chart. A stable earthen dike that was free of fluid was present around the tank. The tank remained in good repair and contained correct identification. The sign was peeling from the tank but remained legible. Valves were closed and plugged. The poly brine tank remained in good repair. Valves were closed and plugged. No violations were observed during this inspection. |
1258116518 | 2007-06-12 | Production Wells | No Violations | I performed a random field inspection. GPSs tank battery and wellhead. I found no violations at this time. |
1329415453 | 2012-02-16 | Production Wells | Violations Noted | I received notification from landowner that well was still leaking gas into the atmosphere. At 09:00 on the day of the inspection I contacted Rick Huffman (330-904-2576) of Eric Petroleum, who agreed to dispatch pumper immediately to blow well down again. I conducted a field inspection of the well at 13:15, and found that the well was still leaking gas from around a metal clamp patch on the 2-3/8 tubing, just above the 4-1/2 well head. This issue has been ongoing since 01/11/2012. |
1454341623 | 2016-01-27 | Production Wells | No Violations | DOGRM Inspector Kevin Perry and myself performed a status check on the above location. The well is equipped with 1.5 tubing and one horizontal separator the well is set up to operate intermittent. There is one 100 barrel tank. There is a very small gas leak around the 1.5 tubing. I called Rick Huffman Field Supervisor and told him about the landowners concerns he said he would get it corrected . ID signs are posted. |
1454508513 | 2016-02-02 | Production Wells | No Violations | I was notified by Rick Huffman that the leak at the wellhead had been fixed. Upon my inspection I could not detect a leak at the wellhead. There is on noted violation at this time. |
15508 | FR | No Violations | ||
1633592366 | 2012-01-11 | Production Wells | No Violations | I received complaint call that this well was leaking gas into the atmosphere. I met the pumper for Eric Petroleum at the well location. There was a leak in the 2.375 tubing just above the 4.5 well head. I witnessed the well being completely blown down into the stock tank. There was zero pressure on the well. Eric Petroleum is to have a service rig on site by 01/20/2012 to replace the top joint of 4.5 casing and 2.375 tubing as needed. Proper identifcation is posted. The tank battery dike in good condition, free of debris, with no spills or leaks around stock tank. There is no evidence of impact around well head. Eric Petroleum will notify me upon completion of the well service for a follow up inspection. |
2120760674 | 2015-10-07 | Production Wells | No Violations | I performed a status check on the above location. There is one 100 barrel tanks and one 35 barrel tank and one horizontal separator. The well is equipped with 2 tubing. ID signs are posted. No noted violations at this time. |
4272348 | 2012-3-1 0:00:0 | PW | No Violations | |
469349334 | 2010-6-15 0:00: | PW | No Violations | |
559500637 | 2018-12-18 0:00 | PW | No Violations | 0.30 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0004272348 | US-OH-124549 | 2013-04-03 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1329415453 | US-OH-109429 | 2012-02-16 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]