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34-099-20836

Well Details

Well ID: 34-099-20836
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Country: United States
State: Ohio
County: Mahoning
Municipality: Beaver Township
Operator Name: GAS ACQUISITION COMPANY LTD
Well Pad ID:
Farm/Lease Name: YENCIK UNIT
License Status: Final Restoration
License Date: 2005-06-08
Spud Date: 1976-10-21
Spud Drilling Contractor:
Final Drill Date: 1976-10-30
Well Total Depth: 5769.00 ft
Configuration: Vertical
Latitude: 40.950000
Longitude: -80.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-10-19 2143 CARLESS RESOURCES INC GeoDate 10/19/76
Original Spud 1976-10-21 LANDOWNER WAIVER ON FINAL RESTORATION SUBMITTED 4/23/07. IP.A.F. 1.5MMCFG
Completed 1976-10-30 LANDOWNER WAIVER ON FINAL RESTORATION SUBMITTED 4/23/07. IP.A.F. 1.5MMCFG
Reached Total Depth 1976-10-30 LANDOWNER WAIVER ON FINAL RESTORATION SUBMITTED 4/23/07. IP.A.F. 1.5MMCFG
Change of Owner 1998-07-02 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2003-10-15 Operator changed from 1388, NORTH COAST ENERGY INC to 6805, GAS ACQUISITION COMPANY LTD
APP 2005-06-08 Proposed Formations:CLINTON, Issued Date:6/8/2005, Expired Date:6/8/2006 6:00:00 AM, Drilling unit acres:153.723, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2006-04-21 LANDOWNER WAIVER ON FINAL RESTORATION SUBMITTED 4/23/07. IP.A.F. 1.5MMCFG
Construction Permit Expires 2006-06-08 LANDOWNER WAIVER ON FINAL RESTORATION SUBMITTED 4/23/07. IP.A.F. 1.5MMCFG
Record Last Modified 2013-03-14 LANDOWNER WAIVER ON FINAL RESTORATION SUBMITTED 4/23/07. IP.A.F. 1.5MMCFG

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5602 5668 21
5602 5668 21
5602 5668 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 9200 Gal 77000
ACID 0 900 Gal 0
N2 0 227 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RSC ENERGY CORP 7274.00 0.00 0
1985 CARLESS RESOURCES INC 6754.00 0.00 365
1986 CARLESS RESOURCES INC 6284.00 0.00 365
1987 CARLESS RESOURCES INC 4731.00 0.00 364
1988 CARLESS RESOURCES INC 6349.00 0.00 365
1989 CARLESS RESOURCES INC 2745.00 0.00 360
1990 CARLESS RESOURCES INC 6287.00 0.00 365
1991 CARLESS RESOURCES INC 5885.00 0.00 365
1992 CARLESS RESOURCES INC 4553.00 0.00 365
1993 CARLESS RESOURCES INC 3791.00 0.00 365
1994 CARLESS RESOURCES INC 2286.00 0.00 365
1995 CARLESS RESOURCES INC 3065.00 0.00 365
1996 CARLESS RESOURCES INC 2271.00 0.00 365
1997 CARLESS RESOURCES INC 2488.00 0.00 365
1998 EXCO - NORTH COAST ENERGY INC 328.00 0.00 365
1999 EXCO - NORTH COAST ENERGY INC 527.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 1083.00 0.00 365
2001 EXCO - NORTH COAST ENERGY INC 638.00 0.00 365
2002 EXCO - NORTH COAST ENERGY INC 337.00 0.00 365
2003 EXCO - NORTH COAST ENERGY INC 235.00 0.00 280
2005 GAS ACQUISITION COMPANY LTD 89.00 0.00 365
2006 GAS ACQUISITION COMPANY LTD 0.00 0.00 0
2007 GAS ACQUISITION COMPANY LTD 0.00 0.00 0
2008 GAS ACQUISITION COMPANY LTD 0.00 0.00 0
2009 GAS ACQUISITION COMPANY LTD 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RSC ENERGY CORP Brine 0 0
1985 CARLESS RESOURCES INC Brine 25 365
1986 CARLESS RESOURCES INC Brine 242 365
1987 CARLESS RESOURCES INC Brine 81 364
1988 CARLESS RESOURCES INC Brine 86 365
1989 CARLESS RESOURCES INC Brine 0 360
1990 CARLESS RESOURCES INC Brine 836 365
1991 CARLESS RESOURCES INC Brine 102 365
1992 CARLESS RESOURCES INC Brine 0 365
1993 CARLESS RESOURCES INC Brine 75 365
1994 CARLESS RESOURCES INC Brine 0 365
1995 CARLESS RESOURCES INC Brine 0 365
1996 CARLESS RESOURCES INC Brine 0 365
1997 CARLESS RESOURCES INC Brine 0 365
1998 EXCO - NORTH COAST ENERGY INC Brine 0 365
1999 EXCO - NORTH COAST ENERGY INC Brine 365
2000 EXCO - NORTH COAST ENERGY INC Brine 0 365
2001 EXCO - NORTH COAST ENERGY INC Brine 0 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 0 280
2005 GAS ACQUISITION COMPANY LTD Brine 0 365
2006 GAS ACQUISITION COMPANY LTD Brine 0 0
2007 GAS ACQUISITION COMPANY LTD Brine 0 0
2008 GAS ACQUISITION COMPANY LTD Brine 0 0
2009 GAS ACQUISITION COMPANY LTD Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1167609125 2003-9-3 0:00:0 PW No Violations 0.50
-1250469233 2006-4-21 0:00: PB No Violations 9.50
-1552898893 2003-9-3 0:00:0 PW No Violations 0.50
-289148498 2003-9-3 0:00:0 PW No Violations 0.50
0080673789 2003-04-22 Production Wells Violations Noted The tank battery consists of 1-100 bbl storage tank that has a brine leak around the salt water discharge line at the tank bottom. Repair or replace the tank. There is a buried concrete salt water tank and a separator. There is also 4- joints of tubing and an old cable on the well site that needs to be removed. Met with Nelson at North Coast Energy and discussed the violation.
0289148498 2003-09-03 Production Wells No Violations The tank has been repaired. Recommend case be resolved.
1145879430 2006-04-20 Plug / Plug Back No Violations Arrived on site for the setting of the bottom plug. Trouble getting the packer to release. Once released the bottom plug was set through the tubing. It was not decided until later that there would be no more plugs set this date.
1167609125 2003-09-03 Production Wells No Violations Debris removed. Leak stopped. Recommend case be resolved.
1176838080 2007-04-17 Final Restoration No Violations Good vegetation is growing at well and tank battery. Lease road is for farmer into fields. Visual inspection shows all piping is gone. A landowner waiver will be attached to final restoration. This well and tank battery has passed final restoration.
1250469233 2006-04-21 Plug / Plug Back No Violations Arrived for the completion of the plug job. Ripped the pipe. Pulled up and set the Big Lime plug. The well did not circulate. Pulled up out of the cement and attempted to circulate the well using 70 bbls of fresh water and 2 sacks of cotton seed hulls. The well did not circulate. Pulled up to 822 where the next plug was to be set. Mixed 400# of gel and 225# cotton seed hull in 10 bbls of fresh water and discplaced with 60 bbls of fresh water. Broke circulation. Mixed and displaced the 8 5/8 plug. Pulled up and set the final plug. The cement stayed up and there was no leakage.
1552898893 2003-09-03 Production Wells No Violations Leak repaired, tubing removed. Recommend case be resolved.
80673789 2003-4-22 0:00: PW No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0080673789 US-OH-129167 2003-04-23 Well operation causing pollution and contamination

For data sources see[9]

References