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Well ID: 34-103-24409 | Loading map...
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Country: United States | |
State: Ohio | |
County: Medina | |
Municipality: Granger Township | |
Operator Name: RANDELL OIL CO | |
Well Pad ID: | |
Farm/Lease Name: GRANGER | |
License Status: Producing | |
License Date: 1987-09-09 | |
Spud Date: 1987-10-03 | |
Spud Drilling Contractor: EDCO DRLG | |
Final Drill Date: 1987-10-07 | |
Well Total Depth: 3695.00 ft | |
Configuration: Vertical | |
Latitude: 41.180000 | |
Longitude: -81.740000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1987-06-19 | Issued Date 6/19/87 Expired Date 6/18/88 Acres 0020000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1987-09-09 | 289 ALL STATES OIL & PROD GeoDate 9/9/87 |
Oil and Gas | 1987-09-09 | Issued Date 6/19/87 Expired Date 6/18/88 Acres 0020000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 03695 Proposed Drill Depth 03695 |
Original Spud | 1987-10-02 | RL 9-12-87 |
Completed | 1987-10-07 | RL 9-12-87 |
Reached Total Depth | 1987-10-07 | RL 9-12-87 |
CO | 1987-11-25 | 289 ALL STATES OIL & PROD GeoDate 6/19/87 |
Construction Permit Expires | 1988-06-18 | RL 9-12-87 |
Completion Report Received | 1988-07-13 | RL 9-12-87 |
Change of Owner | 1999-03-30 | Operator changed from 289, ALL STATES OIL & PROD to 2409, RANDELL OIL CO |
Record Last Modified | 2017-02-15 | RL 9-12-87 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3510 | 3590 | 0 |
3510 | 3590 | 0 | |
2006-09-11 | 3540 | 3588 | 22 |
3540 | 3588 | 22 | |
3510 | 3590 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 0 | 0 | SLICK WATER FRAC |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | ALL STATES OIL & PRODUCING CO | 0.00 | 165.00 | 90 |
1988 | ALL STATES OIL & PRODUCING CO | 19991.00 | 2373.00 | 365 |
1990 | ALL STATES OIL & PRODUCING CO | 8068.00 | 878.00 | 365 |
1991 | ALL STATES OIL & PRODUCING CO | 7272.00 | 458.00 | 365 |
1993 | ALL STATES OIL & PRODUCING CO | 2908.00 | 83.00 | 365 |
1994 | ALL STATES OIL & PRODUCING CO | 2142.00 | 135.00 | 365 |
1995 | ALL STATES OIL & PRODUCING CO | 1769.00 | 405.00 | 365 |
1996 | ALL STATES OIL & PRODUCING CO | 1822.00 | 109.00 | 365 |
1997 | ALL STATES OIL & PRODUCING CO | 1656.00 | 290.00 | 365 |
1998 | ALL STATES OIL & PRODUCING CO | 174097.00 | 151.00 | 0 |
1999 | RANDELL OIL CO | 1733.00 | 75.00 | 270 |
2000 | RANDELL OIL CO | 1945.00 | 113.00 | 360 |
2001 | RANDELL OIL CO | 1269.00 | 115.00 | 365 |
2002 | RANDELL OIL CO | 813.00 | 76.00 | 365 |
2003 | RANDELL OIL CO | 1010.00 | 75.00 | 365 |
2004 | RANDELL OIL CO | 607.00 | 90.00 | 365 |
2005 | RANDELL OIL CO | 820.00 | 35.00 | 365 |
2006 | RANDELL OIL CO | 732.00 | 73.00 | 365 |
2007 | RANDELL OIL CO | 456.00 | 36.00 | 365 |
2008 | RANDELL OIL CO | 0.00 | 48.00 | 365 |
2009 | RANDELL OIL CO | 25.00 | 30.00 | 365 |
2011 | RANDELL OIL CO | 79.00 | 26.00 | 0 |
2012 | RANDELL OIL CO | 0.00 | 18.00 | 366 |
2013 | RANDELL OIL CO | 0.00 | 23.00 | 365 |
2014 | RANDELL OIL CO | 0.00 | 0.00 | 0 |
2015 | RANDELL OIL CO | 0.00 | 30.00 | 365 |
2016 | RANDELL OIL CO | 0.00 | 24.00 | 365 |
2017 | RANDELL OIL CO | 0.00 | 28.00 | 365 |
2018 | RANDELL OIL CO | 0.00 | 36.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | ALL STATES OIL & PRODUCING CO | Brine | 0 | 90 |
1988 | ALL STATES OIL & PRODUCING CO | Brine | 750 | 365 |
1990 | ALL STATES OIL & PRODUCING CO | Brine | 263 | 365 |
1991 | ALL STATES OIL & PRODUCING CO | Brine | 137 | 365 |
1993 | ALL STATES OIL & PRODUCING CO | Brine | 10 | 365 |
1994 | ALL STATES OIL & PRODUCING CO | Brine | 20 | 365 |
1995 | ALL STATES OIL & PRODUCING CO | Brine | 10 | 365 |
1996 | ALL STATES OIL & PRODUCING CO | Brine | 0 | 365 |
1997 | ALL STATES OIL & PRODUCING CO | Brine | 3 | 365 |
1998 | ALL STATES OIL & PRODUCING CO | Brine | 0 | |
1999 | RANDELL OIL CO | Brine | 28 | 270 |
2000 | RANDELL OIL CO | Brine | 19 | 360 |
2001 | RANDELL OIL CO | Brine | 35 | 365 |
2002 | RANDELL OIL CO | Brine | 30 | 365 |
2003 | RANDELL OIL CO | Brine | 35 | 365 |
2004 | RANDELL OIL CO | Brine | 0 | 365 |
2005 | RANDELL OIL CO | Brine | 0 | 365 |
2006 | RANDELL OIL CO | Brine | 33 | 365 |
2007 | RANDELL OIL CO | Brine | 0 | 365 |
2008 | RANDELL OIL CO | Brine | 294 | 365 |
2009 | RANDELL OIL CO | Brine | 30 | 365 |
2011 | RANDELL OIL CO | Brine | 0 | |
2012 | RANDELL OIL CO | Brine | 0 | 366 |
2013 | RANDELL OIL CO | Brine | 0 | 365 |
2014 | RANDELL OIL CO | Brine | 0 | 0 |
2015 | RANDELL OIL CO | Brine | 0 | 365 |
2016 | RANDELL OIL CO | Brine | 0 | 365 |
2017 | RANDELL OIL CO | Brine | 35 | 365 |
2018 | RANDELL OIL CO | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-43906668 | 2014-4-24 0:00: | PW | No Violations | |
-519152554 | 2018-5-23 0:00: | PW | No Violations | |
000PL11353 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0043906668 | 2014-04-24 | Production Wells | Violations Noted | Inspected production well on 04/24/2014. The tank battery consists of 2-100 bbl steel tanks and a vertical separator located within an earthen dike. The tank battery is used by multiple wells; identification is posted for all wells utilizing it. The well is equipped with a pump jack with an electric motor located within an earthen dike. No well identification is posted at the wellhead. Research into the production history of the well showed that no production has been turned in to ODNR since 2012. Randell Oil was notified of the identification issue and will address it as soon as possible. |
0519152554 | 2018-05-23 | Production Wells | No Violations | I met onsite with Randel Oil Company representative, Randy Duncan, to set date and time for the clean-up operation. Originally planned to start on Thursday, 5/31. However, the Contractor is delayed until the 6/4. The site will be contained and monitored until then. |
1529941961 | 2018-05-22 | Production Wells | Violations Noted | I conducted this compliance inspection due to a phone call from John Smith, a Columbia Gas Field Operation Leader. He stated that during a service check of their line along Snowberry Lane they detected a possible line leak and dug an exploratory excavation to determine the source. I found they had excavated a 2 foot by 3-foot hole, approximatley 3-feet deep to find the suspected leak. The excavation start to fill with fluid that was coming from a layer of gravel under the base of the asphalt covering Snowberry Lane. This fluid consisted of water and what appeared to be crude oil. Columbia Gas ceased excavating and oil absorbent pads placed in the excavation. I called Randy Duncan to inform him of the incident and he stated that his pumper is on his way to evaluate the situation. I set up a meeting with Mr. Duncan for tomorrow morning. |
1530296100 | 2018-06-04 | Production Wells | No Violations | I conducted a follow-up inspection to oversee the clean-up contractor on site. The contractor started to excavate in same area as the prior excavation completed by Columbia Gas. They excavated to a depth of approximatley 5 feet where they encountered water and crude oil entering the excavation from a gravel zone. A water truck that was on site removed this fluid from the excavation. At a depth of approximately 4.5 feet, a 4-inch diameter steel pipe was exposed. The contractor thought that this may be a sleeve for the flow line. The contractor excavated and exposed both ends of the flow line and pumped fresh water from well to the tank battery. Prior to flushing the flow line, the contractor cut a hole in the side of the 4-inch diameter pipe to see if there was any communication between 2-7/8-inch flow line and 4-inch pipe during the flushing process. They pumped approximately 25 barrels of fresh water through the flow line, with no communication with the sleeve. The fluid in the excavation cleared up and no more crude oil was seen seeping out of the gravel layer. Fred Romeo from ODNR Emergency Response section was on site to oversee the backfilling and grading the excavation to ground level. The excavated area will be seeded at end of the month. |
1531835151 | 2018-07-17 | Production Wells | No Violations | Conducted a follow-up inspection on reclamation of site after oil seep was removed. The area disturbed in front of address 1505 has been graded and vegetation reestablished and the area to right of driveway of address 1500 that was disturbed during the line repair back in January of 2018 was regraded and top soil replaced and reseeded.
Case closed. |
1576763167 | 2018-05-31 | Production Wells | No Violations | I conducted an inspection to check on the contractors progress on the clean-up. OUPS has marked the utilities, the excavation that was done by Columbia Gas is fenced and additional oil absorbents pads have been placed on the fluid to absorb any assocoated crude oil. The site will be contained untill the contractor can start on the 4th. |
PL11353 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0043906668 | US-OH-124726 | 2014-05-05 | Statement of annual production not filed | |
1529941961 | US-OH-114670 | 2018-07-16 | 9-1-07 | Well operation causing pollution and contamination |
For data sources see[9]