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34-103-24684

Well Details

Well ID: 34-103-24684
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Country: United States
State: Ohio
County: Medina
Municipality: Chatham Township
Operator Name: MS PRODUCING LLC
Well Pad ID:
Farm/Lease Name: MANTZ
License Status: Producing
License Date: 2007-04-06
Spud Date: 1993-07-09
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1993-07-17
Well Total Depth: 5010.00 ft
Configuration: Vertical
Latitude: 41.080000
Longitude: -82.060000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1993-06-25 Issued Date 6/26/93 Expired Date 6/26/94 Acres 0040000 Tool Type RTF Proposed Formation TRENTON thru PCAM Proposed Depth 05010 Proposed Drill Depth 05010
Original Spud 1993-07-10
Completed 1993-07-17
Reached Total Depth 1993-07-17
CO 1993-08-06 4479 FAIRWAY LTD INC GeoDate 6/25/93
Completion Report Received 1993-09-27
Change of Owner 1998-09-09 Operator changed from 4479, FAIRWAY LTD INC to 5905, RUSTIC RESOURCES, INC.
Change of Owner 2000-08-02 Operator changed from 5905, RUSTIC RESOURCES, INC. to 5660, S & S ENERGY CORPORATION
APP 2005-03-17 Proposed Formations:TREMPEALEAU, Issued Date:3/17/2005, Expired Date:3/17/2006 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2007-04-06 Proposed Formations:TREMPEALEAU, Issued Date:4/6/2007, Expired Date:4/5/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2008-04-05
Change of Owner 2017-01-12 Operator changed from 5660, S & S ENERGY CORPORATION to 9842, MS PRODUCING LLC
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4669 0
4669 0
2006-09-11 4786 4794 35
4786 4794 35
4669 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 20 500 Gal 0 2500 GAL 20% ACID
ACID 20 2000 Gal 0 LT.WT./3% CC
Not Treated 0 330 Gal 0 SUPER FLUSH 2# SKS. CALSEAL

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 FAIRWAY LTD INC 581.00 1272.00 132
1995 FAIRWAY LTD INC 36.00 0.00 0
1998 RUSTIC RESOURCES, INC. 206.00 0.00 30
1999 RUSTIC RESOURCES, INC. 1270.00 533.00 365
2000 S & S ENERGY CORP 161.00 0.00 60
2001 S & S ENERGY CORP 765.00 160.00 364
2002 S & S ENERGY CORP 154.00 121.00 365
2003 S & S ENERGY CORP 66.00 0.00 365
2004 S & S ENERGY CORP 0.00 0.00 0
2005 S & S ENERGY CORP 0.00 0.00 0
2006 S & S ENERGY CORP 0.00 0.00 0
2007 S & S ENERGY CORP 0.00 0.00 0
2008 S & S ENERGY CORP 0.00 0.00 0
2009 S & S ENERGY CORP 0.00 0.00 0
2011 S & S ENERGY CORP 0.00 0.00 0
2012 S & S ENERGY CORP 0.00 0.00 0
2013 S & S ENERGY CORP 0.00 0.00 0
2014 S & S ENERGY CORP 0.00 0.00 0
2015 S & S ENERGY CORP 0.00 0.00 0
2016 S & S ENERGY CORP 0.00 0.00 0
2017 MS PRODUCING LLC 0.00 0.00 0
2018 MS PRODUCING LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 FAIRWAY LTD INC Brine 337 132
1995 FAIRWAY LTD INC Brine 0 0
1998 RUSTIC RESOURCES, INC. Brine 65 30
1999 RUSTIC RESOURCES, INC. Brine 2104 365
2000 S & S ENERGY CORP Brine 85 60
2001 S & S ENERGY CORP Brine 1086 364
2002 S & S ENERGY CORP Brine 629 365
2003 S & S ENERGY CORP Brine 604 365
2004 S & S ENERGY CORP Brine 110 0
2005 S & S ENERGY CORP Brine 0 0
2006 S & S ENERGY CORP Brine 0 0
2007 S & S ENERGY CORP Brine 0 0
2008 S & S ENERGY CORP Brine 0 0
2009 S & S ENERGY CORP Brine 0 0
2011 S & S ENERGY CORP Brine 0 0
2012 S & S ENERGY CORP Brine 0 0
2013 S & S ENERGY CORP Brine 0 0
2014 S & S ENERGY CORP Brine 0 0
2015 S & S ENERGY CORP Brine 0 0
2016 S & S ENERGY CORP Brine 0 0
2017 MS PRODUCING LLC Brine 0 0
2018 MS PRODUCING LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1031652873 2015-4-14 0:00: PW No Violations
0000010412 Preliminary Restoration No Violations PASSED Y WITNESSED 12/1/93 INSPECTOR HAROLD MORAVY DATE 12/0119/93 DATA FROM OLD VAX INFO
0437733533 2014-08-05 Production Wells Violations Noted Inspected production well on 08/05/2014. The tank battery consists of 2-100 bbl steel tanks and 1-1,600 gal plastic tank located within an earthen dike. Well identification is posted at the tank battery, but the permit number is too faded to read and needs to be updated. The well is equipped with a wellhead with a stuffing box with a rod sticking up through it. Research into the production history of the well showed that the well has not produced since 2003 or met the minimum production requirements since 2002, therefore the well must be plugged.
1031652873 2015-04-14 Production Wells No Violations Inspected production well on 04/14/2014 to follow-up on a previously-issued compliance notice. The tank battery consists of 2-100 bbl steel tank, 1-1,600 gal plastic tank, and 1-vertical separator located within an overgrown earthen dike. The separator has separated from the piping and fallen over onto the ground. Well identification is posted at the tank battery, but it is too faded to read. The well is equipped with a wellhead with a stuffing box and rod sticking up through it; the pump jack has been removed. 2014 production data showed that the well did not produce any oil or gas. Jason with S&S indicated that he has been continuing to repair lines and work on wells in the area with the intention of putting them back into production. Will continue working with S&S to get the wells turned back on.
10412 PL No Violations
437733533 2014-8-5 0:00:0 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0437733533 US-OH-124713 2014-08-08 Well shall be plugged

For data sources see[9]

References