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34-105-21664

Well Details

Well ID: 34-105-21664
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Country: United States
State: Ohio
County: Meigs
Municipality: Bedford Township
Operator Name: SMITH RONALD DBA CHIPCO
Well Pad ID:
Farm/Lease Name: ARNOLD WALTER D
License Status: Producing
License Date: 1976-10-07
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.110000
Longitude: -82.070000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-10-07 435 HARDIN HANLEY E GeoDate 10/7/76
Change of Owner 2011-05-20 Operator changed from 435, HARDIN HANLEY E to 7640, SMITH RONALD DBA CHIPCO
Change of Owner 2011-10-24 Operator changed from 7640, SMITH RONALD DBA CHIPCO to 6295, KNOX ENERGY INC.
Change of Owner 2017-01-25 Operator changed from 6295, KNOX ENERGY INC. to 7640, SMITH RONALD DBA CHIPCO
Record Last Modified 2017-01-25 GL=909.08

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 HARDIN HANLEY E 446.00 193.00 365
1992 NATLAND ENERGY CORP 301.00 0.00 365
1993 HARDIN HANLEY E 189.00 132.00 365
1994 HARDIN HANLEY E 299.00 196.00 365
1995 HARDIN HANLEY E 284.00 182.00 365
2011 KNOX ENERGY INC. 0.00 0.00 0
2012 KNOX ENERGY INC. 0.00 0.00 0
2013 KNOX ENERGY INC. 0.00 0.00 0
2014 KNOX ENERGY INC. 0.00 0.00 0
2015 KNOX ENERGY INC. 0.00 0.00 0
2016 KNOX ENERGY INC. 0.00 0.00 0
2017 KNOX ENERGY INC. 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 HARDIN HANLEY E Brine 0 365
1992 HARDIN HANLEY E Brine 0 365
1993 HARDIN HANLEY E Brine 0 365
1994 HARDIN HANLEY E Brine 0 365
1995 HARDIN HANLEY E Brine 0 365
2011 KNOX ENERGY INC. Brine 0 0
2012 KNOX ENERGY INC. Brine 0 0
2013 KNOX ENERGY INC. Brine 0 0
2014 KNOX ENERGY INC. Brine 0 0
2015 KNOX ENERGY INC. Brine 0 0
2016 KNOX ENERGY INC. Brine 0 0
2017 KNOX ENERGY INC. Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1013810417 2016-2-22 0:00: AM No Violations 0.40
-187467150 2016-2-16 0:00: PW No Violations 1.50
0187467150 2016-02-16 Production Wells No Violations Inspection of this well found the unit off center. The polish rod was all the way past the horsehead on the right meaning the left side of the unit would need raised. The valves were also in the closed position. This well did not pump into the other wells tank at the bottom of the driveway. The lead line was going over the hill. The only tank down there was a ratty old blue tank. I left a card with the land owner at his gate.
1013810417 2016-02-22 Administrative Inspection No Violations I called Bill Mitton with Knox energy earlier this morning asking about his plans for the three Williams wells, I left a message stating that with my number. Bill called me back around 1:42 pm and stated that those wells freeze up very bad in the winter so they just shut them in. The other well needs the pump pulled and the unit reset. It also needs a new leadline hooked up to the tank battery with the other two wells at the bottom of the driveway. He stated that he would get them all going hopefully by the middle of April.

For data sources see[7]

References