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Well ID: 34-105-21664 | Loading map...
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Country: United States | |
State: Ohio | |
County: Meigs | |
Municipality: Bedford Township | |
Operator Name: SMITH RONALD DBA CHIPCO | |
Well Pad ID: | |
Farm/Lease Name: ARNOLD WALTER D | |
License Status: Producing | |
License Date: 1976-10-07 | |
Spud Date: 1900-01-01 | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.110000 | |
Longitude: -82.070000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-10-07 | 435 HARDIN HANLEY E GeoDate 10/7/76 |
Change of Owner | 2011-05-20 | Operator changed from 435, HARDIN HANLEY E to 7640, SMITH RONALD DBA CHIPCO |
Change of Owner | 2011-10-24 | Operator changed from 7640, SMITH RONALD DBA CHIPCO to 6295, KNOX ENERGY INC. |
Change of Owner | 2017-01-25 | Operator changed from 6295, KNOX ENERGY INC. to 7640, SMITH RONALD DBA CHIPCO |
Record Last Modified | 2017-01-25 | GL=909.08 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | HARDIN HANLEY E | 446.00 | 193.00 | 365 |
1992 | NATLAND ENERGY CORP | 301.00 | 0.00 | 365 |
1993 | HARDIN HANLEY E | 189.00 | 132.00 | 365 |
1994 | HARDIN HANLEY E | 299.00 | 196.00 | 365 |
1995 | HARDIN HANLEY E | 284.00 | 182.00 | 365 |
2011 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2012 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2013 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2014 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2015 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2016 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2017 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | HARDIN HANLEY E | Brine | 0 | 365 |
1992 | HARDIN HANLEY E | Brine | 0 | 365 |
1993 | HARDIN HANLEY E | Brine | 0 | 365 |
1994 | HARDIN HANLEY E | Brine | 0 | 365 |
1995 | HARDIN HANLEY E | Brine | 0 | 365 |
2011 | KNOX ENERGY INC. | Brine | 0 | 0 |
2012 | KNOX ENERGY INC. | Brine | 0 | 0 |
2013 | KNOX ENERGY INC. | Brine | 0 | 0 |
2014 | KNOX ENERGY INC. | Brine | 0 | 0 |
2015 | KNOX ENERGY INC. | Brine | 0 | 0 |
2016 | KNOX ENERGY INC. | Brine | 0 | 0 |
2017 | KNOX ENERGY INC. | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1013810417 | 2016-2-22 0:00: | AM | No Violations | 0.40 |
-187467150 | 2016-2-16 0:00: | PW | No Violations | 1.50 |
0187467150 | 2016-02-16 | Production Wells | No Violations | Inspection of this well found the unit off center. The polish rod was all the way past the horsehead on the right meaning the left side of the unit would need raised. The valves were also in the closed position. This well did not pump into the other wells tank at the bottom of the driveway. The lead line was going over the hill. The only tank down there was a ratty old blue tank. I left a card with the land owner at his gate. |
1013810417 | 2016-02-22 | Administrative Inspection | No Violations | I called Bill Mitton with Knox energy earlier this morning asking about his plans for the three Williams wells, I left a message stating that with my number. Bill called me back around 1:42 pm and stated that those wells freeze up very bad in the winter so they just shut them in. The other well needs the pump pulled and the unit reset. It also needs a new leadline hooked up to the tank battery with the other two wells at the bottom of the driveway. He stated that he would get them all going hopefully by the middle of April. |
For data sources see[7]