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34-105-22357

Well Details

Well ID: 34-105-22357
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Country: United States
State: Ohio
County: Meigs
Municipality: Bedford Township
Operator Name: SMITH RONALD DBA CHIPCO
Well Pad ID:
Farm/Lease Name: WILLIAMS
License Status: Producing
License Date: 1981-12-31
Spud Date: 1982-04-20
Spud Drilling Contractor: SWANK-ULLMAN
Final Drill Date: 1982-04-22
Well Total Depth: 1900.00 ft
Configuration: Vertical
Latitude: 39.110000
Longitude: -82.060000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-12-31 1336 AKRON OIL CORP GeoDate 12/31/81
Oil and Gas 1981-12-31 Issued Date 12/31/81 Expired Date 12/31/82 Acres 0000000 Tool Type Proposed Formation Proposed Depth Proposed Drill Depth
Original Spud 1982-04-20 PERMIT EXPIRED.
Completed 1982-04-22 PERMIT EXPIRED.
Reached Total Depth 1982-04-22 PERMIT EXPIRED.
Construction Permit Expires 1982-12-31 PERMIT EXPIRED.
Change of Owner 1984-02-02 Change Owner From 435 HANLEY HARDIN to 1336 AKRON OIL CORPORATION: 2-2-1984
Change of Owner 2003-06-16 Operator changed from 1336, AKRON OIL CORP to 6295, KNOX ENERGY INC.
Change of Owner 2017-01-25 Operator changed from 6295, KNOX ENERGY INC. to 7640, SMITH RONALD DBA CHIPCO
Record Last Modified 2017-02-15 PERMIT EXPIRED.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-12-02 1786 1792 10
1786 1792 10
1786 1792 10

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 53000 Gal 25000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 AKRON OIL CORP 0.00 0.00 0
1985 AKRON OIL CORP 0.00 0.00 0
1986 AKRON OIL CORP 0.00 0.00 365
1987 AKRON OIL CORP 498.00 197.00 180
1988 AKRON OIL CORP 395.00 68.00 365
1989 AKRON OIL CORP 390.00 97.00 365
2003 KNOX ENERGY INC. 0.00 0.00 365
2004 KNOX ENERGY INC. 0.00 0.00 366
2005 KNOX ENERGY INC. 0.00 0.00 365
2006 KNOX ENERGY INC. 0.00 0.00 39
2007 KNOX ENERGY INC. 518.00 153.00 365
2008 KNOX ENERGY INC. 764.00 78.00 365
2009 KNOX ENERGY INC. 489.00 39.00 365
2010 KNOX ENERGY INC. 22.00 50.00 365
2011 KNOX ENERGY INC. 35.00 32.00 365
2012 KNOX ENERGY INC. 111.00 32.00 366
2013 KNOX ENERGY INC. 46.00 9.00 365
2014 KNOX ENERGY INC. 43.00 27.00 365
2015 KNOX ENERGY INC. 0.00 0.00 0
2016 KNOX ENERGY INC. 0.00 0.00 0
2017 KNOX ENERGY INC. 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 AKRON OIL CORP Brine 0 0
1985 AKRON OIL CORP Brine 0 0
1986 AKRON OIL CORP Brine 0 365
1987 AKRON OIL CORP Brine 210 180
1988 AKRON OIL CORP Brine 70 365
1989 AKRON OIL CORP Brine 113 365
2003 KNOX ENERGY INC. Brine 0 365
2004 KNOX ENERGY INC. Brine 0 366
2005 KNOX ENERGY INC. Brine 0 365
2006 KNOX ENERGY INC. Brine 0 39
2007 KNOX ENERGY INC. Brine 12 365
2008 KNOX ENERGY INC. Brine 10 365
2009 KNOX ENERGY INC. Brine 0 365
2010 KNOX ENERGY INC. Brine 70 365
2011 KNOX ENERGY INC. Brine 85 365
2012 KNOX ENERGY INC. Brine 89 366
2013 KNOX ENERGY INC. Brine 30 365
2014 KNOX ENERGY INC. Brine 53 365
2015 KNOX ENERGY INC. Brine 0 0
2016 KNOX ENERGY INC. Brine 0 0
2017 KNOX ENERGY INC. Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-293784619 2016-2-16 0:00: PW No Violations 2.00
0293784619 2016-02-16 Production Wells No Violations Inspection of this well found that it hadnt been pumped in recent weeks. The bearing cap on top of the walking beam was broken and disapled the pump jack. I will call Knos and get them moving on this well.
1331040555 2002-12-10 Production Wells No Violations An inspection of the well revealed the well to be Idle and incapable of producing, well is equipped with tubing, rods, pump jack, and production tanks. It appears no house gas is being used from well.

For data sources see[9]

References