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34-105-23205

Well Details

Well ID: 34-105-23205
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Country: United States
State: Ohio
County: Meigs
Municipality: Scipio Township
Operator Name: M & R INVESTMENTS OHIO LLC
Well Pad ID:
Farm/Lease Name: RHONDA STOCKWELL
License Status: Final Restoration
License Date: 2019-02-19
Spud Date: 1984-10-16
Spud Drilling Contractor: HAROLD B BRETT
Final Drill Date: 1984-10-17
Well Total Depth: 925.00 ft
Configuration: Vertical
Latitude: 39.110000
Longitude: -82.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-07-25 152 ROYAL PETROLEUM PROP INC GeoDate 7/25/84
Oil and Gas 1984-07-25 Issued Date 7/25/84 Expired Date 1/21/85 Acres 0010000 Tool Type RTA Proposed Formation CW RN/KEENER Proposed Depth 00925 Proposed Drill Depth 00925
Original Spud 1984-10-16 CHG PTD/FORM 10-13-84
Completed 1984-10-17 CHG PTD/FORM 10-13-84
Reached Total Depth 1984-10-17 CHG PTD/FORM 10-13-84
Completion Report Received 1984-11-05 CHG PTD/FORM 10-13-84
CO 1986-06-19 152 ROYAL PETROLEUM PROP INC GeoDate 6/19/86
Unknown 1986-06-19 Issued Date 6/19/86 Expired Date 6/19/87 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
CO 1996-01-02 4350 CENTURY WELL SERVICE GeoDate 6/19/86
Change of Owner 2007-10-03 Operator changed from 4350, CENTURY WELL SERVICE to 7033, BROAD STREET ENERGY COMPANY
Change of Owner 2008-02-14 Operator changed from 7033, BROAD STREET ENERGY COMPANY to 8312, BROAD STREET SERV LLC
Change of Owner 2015-07-16 Operator changed from 8312, BROAD STREET SERV LLC to 8685, M & R INVESTMENTS OHIO LLC
APP 2019-02-19 Proposed Formations:KEENER, Issued Date:2/19/2019, Expired Date:2/18/2021 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2019-02-26 CHG PTD/FORM 10-13-84
Construction Permit Expires 2021-02-18 CHG PTD/FORM 10-13-84

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 0 0
0 0
0 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NONE

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 ROYAL PETROLEUM PROP INC 0.00 0.00 0
1999 CENTURY WELL SERVICE 0.00 0.00 365
2000 CENTURY WELL SERVICE 0.00 0.00 365
2001 CENTURY WELL SERVICE 0.00 0.00 365
2002 CENTURY WELL SERVICE 0.00 0.00 365
2003 CENTURY WELL SERVICE 0.00 0.00 365
2004 CENTURY WELL SERVICE 0.00 0.00 365
2005 CENTURY WELL SERVICE 0.00 0.00 365
2006 CENTURY WELL SERVICE 0.00 0.00 365
2007 BROAD STREET SERV LLC 0.00 0.00 365
2008 BROAD STREET SERV LLC 0.00 0.00 0
2009 BROAD STREET SERV LLC 0.00 0.00 0
2011 BROAD STREET SERV LLC 0.00 0.00 0
2012 BROAD STREET SERV LLC 0.00 0.00 0
2013 BROAD STREET SERV LLC 0.00 0.00 0
2014 BROAD STREET SERV LLC 0.00 0.00 0
2015 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2016 M & R INVESTMENTS OHIO LLC 10.00 0.00 0
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 ROYAL PETROLEUM PROP INC Brine 0 0
1999 CENTURY WELL SERVICE Brine 0 365
2000 CENTURY WELL SERVICE Brine 0 365
2001 CENTURY WELL SERVICE Brine 0 365
2002 CENTURY WELL SERVICE Brine 0 365
2003 CENTURY WELL SERVICE Brine 0 365
2004 CENTURY WELL SERVICE Brine 0 365
2005 CENTURY WELL SERVICE Brine 0 365
2006 CENTURY WELL SERVICE Brine 0 365
2007 BROAD STREET SERV LLC Brine 0 365
2008 BROAD STREET SERV LLC Brine 0 0
2009 BROAD STREET SERV LLC Brine 0 0
2011 BROAD STREET SERV LLC Brine 0 0
2012 BROAD STREET SERV LLC Brine 0 0
2013 BROAD STREET SERV LLC Brine 0 0
2014 BROAD STREET SERV LLC Brine 0 0
2015 M & R INVESTMENTS OHIO LLC Brine 0 0
2016 M & R INVESTMENTS OHIO LLC Brine 0 0
2017 M & R INVESTMENTS OHIO LLC Brine 0 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1015806889 2016-3-31 0:00: PW No Violations 1.00
-1037609506 2019-5-7 0:00:0 PB No Violations 2.30
-1360664397 2017-11-24 0:00 PW No Violations 0.50
-1662624799 2011-3-6 0:00:0 PW No Violations
-1798707396 2019-5-9 0:00:0 PB No Violations 9.00
-2008523458 2007-4-30 0:00: PW No Violations
-2043379166 2015-11-23 0:00 PW No Violations 2.70
-521047623 2019-4-17 0:00: PB No Violations 1.30
-80195644 2017-6-6 0:00:0 PW No Violations 1.20
-898538925 2014-4-21 0:00: PW No Violations 1.50
-931335527 2011-3-7 0:00:0 PW No Violations
000PL10736 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0080195644 2017-06-06 Production Wells No Violations Well was found to be in the same idle state as in previous inspections. The well is leaning off of 90 degrees about 10-15 degrees. It would appear as though a slip was pushing the casing over. Pictures were taken.
0428837895 2019-05-08 Plug / Plug Back No Violations Unlimited Energy Services took 5 hours gathering 1.5 inch diameter tubing and getting the tubing back to the well. They attempted to run the 1.5 inch tubing but could not because the 7 inch surface casing is bent approximately 18 feet below the surface. The are obtaining 1.5 outside diameter tubing that should allow them to get past the bend in the surface casing.
0521047623 2019-04-17 Plug / Plug Back No Violations I walked this proposed access road for the future plugging of this well. There was one creek crossing. The creek is unnamed. I informed Mr. Mick Goodwin with Unlimited Energy Serives that he would be required to use a culvert to cross this unnamed creek. The well consisted of 7 inch diameter casing with a swage. Records indicate the well is 800 feet deep. The access road construction will begging on 4.18.19.
0728598503 2018-05-31 Production Wells No Violations This well was originally issued a violation for being idle and not capable of production, this is in O.R.C. 1509.12B. There is no path to the wellhead. The casing in this well is leaning downhill slightly, like the casing is bent from a slip. The well has no flowlines attached and is not capable of production. The last time I spoke with Jody Jasper he stated that these Stockwell wells were on the short list to be plugged. I called Jody Jasper the field supervisor for M&R Investments at 10:31 A.M. and left a message about the follow-ups for these wells.
0898538925 2014-04-21 Production Wells No Violations Compliance Notice Follow-up: The well is still idle and there are no production lines or equipment hooked up to the wellhead. There has been no resolution to any of the issues.
0931335527 2011-03-07 Production Wells No Violations Accompanied Meigs Inspector Josh Garland on the inspection. A blank Royal Petroleum Identification was on the ground near the wellhead. Well is not connected to production equipment or production lines. No equipment or lines were observed on the well site. Well is equipped with 6 5/8 casing with wellhead annulus has 2 valve. 4.5 casing with 4 by 2 swedge, 2 tee with 2 ball valve, 2 nipple with 2 by 3/4 reducing coupling, a 3/4 nipple, a3/4 bullheaded tee with a 3/4 ball valve on each end. All valves are shut. No leaks observed during inspection. Took photos and GPS of the well.
1015806889 2016-03-31 Production Wells No Violations Well is still in violation. No plugging plans submitted. No lines connected to well, valves closed. Pictures taken.
1037609506 2019-05-07 Plug / Plug Back No Violations Unlimited Energy Services repaired the lease road and was able to bring a wire line truck back to the well. They tagged bottom at 912 feet. The 4.5 inch casing cannot be removed due to the 7 inch casing being bent about 18 feet below grade. They used collar busters to shoot the 4.5 inch casing at 900 feet, 450 feet and 250 feet.
1265674433 2016-01-12 Production Wells No Violations Plugging plan not yet received.
1309246503 2020-4-9 0:00:0 FR No Violations 0.50
1360664397 2017-11-24 Production Wells No Violations I found this well in the exact same condition as previously reported. I took new pictures of the well. This well had no identification. The casing was about 7 degrees slanted from 90 degree vertical. All the valves on this well were in the closed position.
1421410557 2018-04-16 Production Wells No Violations This well was issued a notice for being idle and not capable of production. The well is still in a state of idleness and is not capable of production. There are no flowline connected to the well. I spoke with Jody Jasper at 2:20 pm about this well the next day. He said that he will bring this well and the others I spoke with him about up in a meeting with his boss later this week.
1448302661 2015-11-23 Production Wells No Violations Close previous violation and issue
1556821591 2019-05-02 Plug / Plug Back No Violations Unlimited Energy Services pulled 913 feet of 1 inch diameter tubing from the well. They attempted to run 4.5 inch tools into the well bore to check total depth. The surface casing and the production casing were bent approximately 5 below the surface of the ground. They excavated to see if they could find out where the pipe was bent. They could not dig deep enough to locate the bend in the casing.
1662624799 2011-03-06 Production Wells Violations Noted Upon Inspection well was found to have no ID and to be idle with no production records for previous two years. 1501:9-9-05 (A)(10) All producing leases shall be legibly identified in a conspicuous place on or near the well-head or the storage tanks as to owner, lease name, well number, permit number where available, county, and an emergency telephone number. If multiple wells are being produced into the common tanks each well-head shall be identified as to owner, permit number where available, well number and lease name. Well shall be in production, plugged or placed in temporary inactive status. Production records shall be filled, and well shall be properly identified.
1794458889 2019-05-01 Plug / Plug Back No Violations My inspection revealed this well consisted of 8.62 inch diameter casing with 4.5 inch diameter production casing. The 8.62 inch diameter casing is bent at approximately 10 degree angle. Once the swage on the 4.5 inch diameter production casing was removed. This revealed 1 inch diameter pipe. The crew did not have tools to remove 1 inch diameter pipe and they will have to locate 1 inch tools before they can begin plugging the well.
1798707396 2019-05-09 Plug / Plug Back No Violations Unlimited Energy Services ran 870 feet of 1 inch diameter tubing. They pumped 8 barrels of fresh water to obtain circulation. They starting mixing cement at 4:45 PM and pumped 8 barrels of cement. They pulled 20 joints of 1 inch diameter tubing and pumped additional cement until the cement came back to surface.
1809659866 2015-08-17 Field Inspected, Well Not Found No Violations Well not found in brush.
2008523458 2007-04-30 Production Wells No Violations The well was found incapable of production.
2043379166 2015-11-23 Production Wells Violations Noted Well equipped with 8 5/8 surface casing, 4 1/2 production casing, a swage and reducer. The valves on each of the casings are closed, there are no lines, production equipment a the well, or identification. The well owner/operator shall submit a written plugging schedule to: ODNR Division of Oil & Gas, c/o Josh Garland, 5880 Memory Rd, Zanesville OH 43701 within 30 days, per OAC 1501: 9-11-05 (b) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
239838113 2019-6-18 0:00: FR No Violations 0.40
428837895 2019-5-8 0:00:0 PB No Violations 6.80
728598503 2018-5-31 0:00: PW No Violations 0.40
PL10736 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1662624799 US-OH-116438 2015-12-01 Failure to legibly identify well
1662624799 US-OH-116439 2015-12-01 Nonproduction; well shall be plugged or placed in temporary inactive status
1662624799 US-OH-116440 2015-12-01 Statement of annual production not filed
2043379166 US-OH-120799 2015-12-01 Well shall be plugged

For data sources see[9]

References