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34-105-60871

Well Details

Well ID: 34-105-60871
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Country: United States
State: Ohio
County: Meigs
Municipality: Sutton Township
Operator Name: ORPHAN WELL PROGRAM
Well Pad ID:
Farm/Lease Name: CREW ROBERT
License Status: Final Restoration
License Date: 2012-03-13
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1925-04-09
Well Total Depth: 538.00 ft
Configuration: Vertical
Latitude: 38.990000
Longitude: -81.930000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1925-04-09 I&O 2011 11 026
Reached Total Depth 1925-04-09 I&O 2011 11 026
APP 2012-03-13 Proposed Formations:, Issued Date:3/13/2012, Expired Date:3/13/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged by Orphan Well Program 2012-06-06 Plugged by Orphan Well Program
Plugged/Abandoned 2012-06-06 I&O 2011 11 026
Construction Permit Expires 2014-03-13 I&O 2011 11 026
Record Last Modified 2019-06-14 I&O 2011 11 026

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1048460020 2012-8-13 0:00: FR No Violations 0.50
-1275937123 2012-9-28 0:00: AM No Violations 0.30
-1497299407 2013-2-28 0:00: PB No Violations 0.50
-157658114 2012-5-23 0:00: OR No Violations
-160016548 2012-10-4 0:00: FR No Violations 0.30
-1725285525 2012-5-31 0:00: PB No Violations
-1917848952 2012-8-29 0:00: FR No Violations 0.30
-1978206297 2012-5-24 0:00: PB No Violations
-453684163 2011-10-25 0:00 OR No Violations 1.00
-547795710 2012-6-6 0:00:0 PB No Violations
-817261988 2012-5-25 0:00: PB No Violations
0157658114 2012-05-23 Orphan No Violations Meadows service rig on the well. Sediment fence has been installed between well and Ohio river. Installed containment area made of staked down straw bales and plastic sheeting (down slope from the well). Rig crew pulling rods at 8:30 am. Pulled 1528 feet of rods at 10:00am. Well is deeper than records indicate. Well pressured up and blew out 100 feet of rods and the pump. No one was injured. Blow out created an oil mist that coated Route 124 with oil mist. Emergency responders (Racine Fire Department and Meigs EMA) were called to close the road for safe clean up of the oil. Meadows crew cleaned the road with oil absorbent. Route 124 was open at 1:00 pm. ODOT county manager Brett Jones and State patrol trooper Webb were satisfied with the clean up. Landowner across Route 124 (Dave Wilsons property) was impacted by the over spray. Mist was seen on 3 trees and on a truck and car. Meadows paid Wilson $100.00 to have the vehicles cleaned. 5 3/16 casing head parted 2 feet below surface. 2 tubing has multiple holes in it. Installed 3 casing with a sand hitch ( 3 flared on end and material is wrapped around casing and secured. 3 is lowered into 5 3/16 casing and sand is poured into annulus) tension was pulled on 3 casing and pulled stretch on the 5. 3 by 2 swedge with 2 valve was installed.
0160016548 2012-10-04 Final Restoration No Violations Restoration requirements still not met. Small amounts of contaminated soils remain on site and vegetative cover has not yet been established.
0208771818 2012-07-31 Final Restoration No Violations The area in the front of Mr. Westons yard is still void of vegetation and areas of the yard still appear contaminated. I spoke with Meadows about finishing the restoration.
0453684163 2011-10-25 Orphan No Violations Accompanied J. Scott to have landowner sign Right of Entry form.
0520889682 2012-05-30 Plug / Plug Back No Violations I & O plugging, Jon Scott requested I arrive at site, having trouble plugging well. Well has kicked out and flowed a couple times. Well located near St Rt 124, Ohio River and houses. Set at plug from 1344ft to 848ft between 5 casing and 2 tubing. Mixed 28 sacks of cement for plug, pumped plug through 1 tubing.
0547795710 2012-06-06 Plug / Plug Back No Violations Tagged plug at 210ft. Ran in 1 1/2 tubing set plug from 210ft to 3ft from surface.
0603474237 2012-06-07 Plug / Plug Back No Violations Area has been graded , the steel pit has been removed, the area has been reseeded and mulched, no drilling equipment on site.
0809464292 2012-08-23 Final Restoration No Violations There had been no further steps taken in the restoration.
0817261988 2012-05-25 Plug / Plug Back No Violations Two water trucks on location. 1640 feet of 1 tubing ran inside 2 tubing. Pumped 1 barrel fresh water at 200 psi. Pressure dropped to 100 psi then pressured back up to 200 psi. Bleed pressure off and connected 1 tubing with valve to Water truck. Well kicked off and flowed into water truck. Pumped 1.25 barrels fresh water through 1 tubing and well kicked off at 350 to 400 psi. Loaded well casing with brine. Circulate brine to surface and into to steel tank. Well is under control. Pumped 5 sacks Cemex cement down 1 tubing. Displace with 1.25 barrels water. Circulated back to surface while pumping cement. Extract 1 tubing. No gas or oil circulated out of well. Shut in wellhead with swedge and valve.
1048460020 2012-08-13 Final Restoration No Violations Follow up restoration work has not been completed. Areas around well head, under rig, and under cement pump are still void of vegetation. Small areas of soil in these areas still appear to be contaminated. Lime has been applied to the soil.
1256366454 2012-07-25 Final Restoration No Violations The pits have been closed, and there is no equipment on site. However the soil around the wellhead appears to contain oil and grass has not grown in it as of yet. The landowner states no grass seed was ever put down.
1275937123 2012-09-28 Administrative Inspection No Violations I spoke with Jason Meadows and we discussed the restoration requirements for the well. he told me they would be addressing the issues early next week.
1320111772 2011-10-05 Orphan No Violations I&O Complaint inspection. Inspector Josh Garland and I met with James Weston at the well site. Well is equipped with 14 , and 10 casing both are open. 5 casing with 2 tubing. Well is not connected to production equipment or production lines. Well is leaking gas in the 10 and 5 annulus. Oil residue is on the ground around the well casing. James Weston told us that when the Ohio river floods and fills up the well that oil is released from the well into the river and onto the property. Photos were taken along with a sketch of the site. The well is being referred to the Orphan well program.
1337870072 2012-05-23 Plug / Plug Back No Violations 1653 feet of rods were pulled from the well. Records show the well as producing from the Cow Run formation, this well is producing oil from the Berea Sandstone. As the last rods were being pulled, the well kicked and blew trapped gas and bring out of the tubing. The river was unaffected, the contamination was carried towards St Rt 124 by the wind. The well blew itself down. The 5 casing head was completely rotted away and we were unable to install a swedge on that string of casing. So a joint of 4 casing was installed inside the 5 casing with a sand hitch so a swedge could be installed to control the well.
1338492242 2012-05-31 Plug / Plug Back No Violations Five inch casing was shot at 777 feet. Unable to pull the five inch. Pumped an 18 sack, 14 lb/ft, class A cement plug from 848 feet to 700 feet. Plug displaced through 1.5 inch tubing with 1.5 Bbl fresh water.
1338569706 2012-06-01 Plug / Plug Back No Violations Cement top inside 5 inch tagged at 685 feet. Casing shot at 552 feet, then 441 feet, and 332 feet. After each shot an attempt was made to pull the casing. Each time 20,000 lbs of stretch was pulled and the casing never parted. A 45 sack Class A cement plug was pumped down 1 1/2 inch tubing into the 5 inch casing from 685 to 300 feet.
1339002215 2012-05-29 Plug / Plug Back No Violations Damage to neighbors trees across the street was accessed. 1.5 inch tubing was to be used to pump plug between 2 and 5 from 1344-849. Cement was tested and the mixture was too thin. The plug was displaced out of the hole. The 5 began to gas so salt water was used to kill the well.
1339161253 2012-06-04 Plug / Plug Back No Violations Tagged plug set by Josh Garland, plug at 283ft. Sot off 5 casing at 243ft, pulled casing. Ran in 1 1/2 tubing and set plug from 283ft to 210ft. Will not remove 10 casing, it appears to be drive pipe and set at 122ft.
1339682401 2012-05-30 Plug / Plug Back No Violations Meet Dan Goins MRI 3 on location and reviewed well records and time line of plugging up to today. I was called out to Gallia County at 9:30 AM, and Dan witnessed the cement plug through 1 tubing from 1344 to 848 28 sacks. I returned to plug site at 12:30 PM and no gas was observed at the wellhead. Meadows removed the 8 by 4 swedge and ran a 2 overshot onto the 2 tubing. Rig up wire line to shoot the tubing at 824 with a Primer Cord shot. Extract 824 of 2 tubing. Ran collar locator on 5 casing. Collar locator having interference with 2 tubing at 824. Good collar on 5 casing located at 793 and 771.
1414407720 2011-12-12 Administrative Inspection No Violations James Weston called and requested a letter from ODNR / DOGRM stating that the well is in the Orphan program and that the state will plug the well. His bank requested it. He also wants a copy of the right of entry form. Request was forwarded to I&O section.
1416454701 2012-05-29 Plug / Plug Back No Violations Tag top of cement plug inside 2 tubing at 848 feet. Fluid level at 175 feet. No gas show. Install 8 by 4 swedge. Run 1 tubing inside 5 casing beside 2 tubing to 1344. Water truck on location. Mix 28 sacks cement for a 496 plug. Circulate water and oil prior to pumping cement. Pumped cement. Cement mix was light. Mud scale weight 11 pounds. Well started to kickoff. Circulate light cement out of well with 30 barrels water until clear. Hauled 35 barrels brine and loaded the well to gain control.
1497299407 2013-02-28 Plug / Plug Back No Violations
1626588963 2013-03-18 Final Restoration No Violations The areas along the drive way and below the propane tank have been reseeded and mulched. The top soil has been replaced.
1725285525 2012-05-31 Plug / Plug Back No Violations 2 tubing shot off at 824 ft, removed tubing. Located collars on 5 casing and shot at 777 ft, not able to pull casing. Will set cement plug from 848 ft to 700ft. Jon Scott and Josh Garland on site.
1917848952 2012-08-29 Final Restoration No Violations The soil still shows signs of contamination and no grass seed has been laid down.
1978206297 2012-05-24 Plug / Plug Back No Violations Well is under control. Water truck on location. Used 1 hose to clean out 5 annulus down to 30 feet. Filled annulus and tubing with fresh water and flowed oil into steel pit. Used 60 barrels fresh water to flow oil into pit. Cleaned out annulus and installed wellhead on 10 casing. Ran 1 tubing inside 2 tubing to total depth (1640). Moved cement pumping equipment on location.
208771818 2012-7-31 0:00: FR No Violations 0.80
520889682 2012-5-30 0:00: PB No Violations
603474237 2012-6-7 0:00:0 PB No Violations 0.80
809464292 2012-8-23 0:00: FR No Violations 0.50

For data sources see[3]

References