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| Well ID: 34-111-20198 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Monroe | |
| Municipality: Seneca Township | |
| Operator Name: FURR OIL & GAS LLC | |
| Well Pad ID: | |
| Farm/Lease Name: MCCORT MARY C | |
| License Status: Producing | |
| License Date: | |
| Spud Date: 1940-12-24 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1941-05-07 | |
| Well Total Depth: 1600.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.860000 | |
| Longitude: -81.230000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1940-12-24 | |
| Completed | 1941-05-07 | |
| Reached Total Depth | 1941-05-07 | |
| Change of Owner | 2012-07-27 | Operator changed from 9998, HISTORIC OWNER to 8974, FURR OIL & GAS LLC. WELL TRANSFERRED PER OWNERSHIP AFFIDAVIT. SEE OWNER FILE FOR DOCUMENTATION. |
| Record Last Modified | 2013-10-03 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 0 | 0 | 0 |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2005 | FURR OIL & GAS LLC | 850.00 | 0.00 | 365 |
| 2006 | FURR OIL & GAS LLC | 961.00 | 0.00 | 365 |
| 2007 | FURR OIL & GAS LLC | 940.00 | 0.00 | 365 |
| 2008 | FURR OIL & GAS LLC | 815.00 | 0.00 | 365 |
| 2009 | FURR OIL & GAS LLC | 1056.00 | 0.00 | 365 |
| 2010 | FURR OIL & GAS LLC | 1222.00 | 0.00 | 365 |
| 2011 | FURR OIL & GAS LLC | 1056.00 | 0.00 | 365 |
| 2012 | FURR OIL & GAS LLC | 744.00 | 0.00 | 232 |
| 2013 | FURR OIL & GAS LLC | 0.00 | 0.00 | 0 |
| 2014 | FURR OIL & GAS LLC | 0.00 | 0.00 | 0 |
| 2015 | FURR OIL & GAS LLC | 0.00 | 0.00 | 0 |
| 2016 | FURR OIL & GAS LLC | 0.00 | 0.00 | 0 |
| 2017 | FURR OIL & GAS LLC | 40.00 | 0.00 | 150 |
| 2018 | FURR OIL & GAS LLC | 351.00 | 0.00 | 355 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2005 | FURR OIL & GAS LLC | Brine | 0 | 365 |
| 2006 | FURR OIL & GAS LLC | Brine | 0 | 365 |
| 2007 | FURR OIL & GAS LLC | Brine | 0 | 365 |
| 2008 | FURR OIL & GAS LLC | Brine | 0 | 365 |
| 2009 | FURR OIL & GAS LLC | Brine | 0 | 365 |
| 2010 | FURR OIL & GAS LLC | Brine | 0 | 365 |
| 2011 | FURR OIL & GAS LLC | Brine | 0 | 365 |
| 2012 | FURR OIL & GAS LLC | Brine | 0 | 232 |
| 2013 | FURR OIL & GAS LLC | Brine | 0 | 0 |
| 2014 | FURR OIL & GAS LLC | Brine | 0 | 0 |
| 2015 | FURR OIL & GAS LLC | Brine | 0 | 0 |
| 2016 | FURR OIL & GAS LLC | Brine | 0 | 0 |
| 2017 | FURR OIL & GAS LLC | Brine | 0 | 150 |
| 2018 | FURR OIL & GAS LLC | Brine | 0 | 355 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -131759005 | 2015-6-4 0:00:0 | PW | No Violations | |
| 0131759005 | 2015-06-04 | Production Wells | No Violations | Compliance Notice # 1398690935 follow up inspection. Upon inspection it was observed that the said well remains idle with the 6.625 casing present approximately 36 below grade level with no production equipment present. Phone notification has been made to the producer in regards to the idle well, they say they are waiting on Chuck Dye with his service rig. The initial violation expired on 11-12-2014. I shall on this day refer the well over to my Supervisor Brent bear for the issuance of a Chiefs order. |
| 0833539680 | 2015-04-13 | Production Wells | No Violations | Compliance Notice # 1398690935 follow up inspection. Upon inspection it was observed that the said well remains idle with the 6.625 casing present approximately 36 below grade level with no production equipment present. Phone notification was left with the producer on this day to proceed with the repairs or plug the well. |
| 1368709182 | 2013-05-15 | Work Over Reconditioning | No Violations | Status check inspection found Harmons Well Service rig on the hole with the 2 tubing pulled out of the hole and 3.375 tubing on location to be run back into the well bore. |
| 1398690935 | 2014-04-28 | Production Wells | Violations Noted | Status check inspection found no casing present and the production tubing pulled out of the hole with the well appearing to be filled in with dirt. My previous inspection witnessed Harmons well service rig on the hole trying to retrieve the down hole packer lost off the tubing. Instructions are as follows-plug the said well within 180 days. ODNR contact Monroe County Inspector Bill Stolarik 740-507-6592. |
| 1405213236 | 2014-07-12 | Production Wells | No Violations | On this day my inspection found that a service rig owned by Chuck Dye has been moved on the hole with the following observed, 6.625 casing was found present approximately 4 below the surface grade level and Chuck Dye was on location trying to get a string of tools down the hole on the service rig wireline but was having difficulties at 8 below grade with a tight spot in the casing, a fluid level could be seen at approximately 70 below grade level possibly indication a hole in the 6.625 casing near that point. Chuck Dye will continue to try and work the tools down hole and recover the lost completion packer in the hole. |
| 1416243472 | 2014-11-17 | Administrative Inspection | No Violations | On 11/14/2014 the well owner called and informed me that He was awaiting Chuck Dye to return to the well with His service rig and once again attempt to recover the lost 6.625 packer in the hole. He indicated if the attempts to recover the packer and get a new packer set on good tubing were unsuccessful He would apply for a plugging permit and plug the well accordingly. I informed Him I had stopped by while Chuck Dye was working on the well and spoke with Chuck Dye also and would allow them to proceed with the attempted repair process. (Note) The elderly landowner uses the gas from the well to heat his home. |
| 1438909882 | 2015-08-06 | Production Wells | No Violations | Compliance Notice # 1398690935 follow up inspection found the well owner has contracted a local well service rig company owned by Chuck Dye and they are on location and have sucessfully ran and set 1568 of 4.5 casing into the well with a formation packer placed in the well bore on the casing. |
| 1439230323 | 2015-08-10 | Production Wells | No Violations | Compliance Notice # 1398690935 follow up inspection found the well now has 4.5 casing in the well bore set to a depth of 1,574 with a formation packer on the string at 1,486 with 1,566 of 2x 10 round tubing set in the well. The well is producing from the Berea formation (1,556 to 1,570). The well total depth by measurement of wieline logger is 1,574. The violation was resolved on this day. |
| 1915548147 | 2015-06-25 | Production Wells | No Violations | Compliance Notice # 1398690935 follow up inspection found the well owner has contracted a local well service rig company owned by Chuck Dye and they are on location making an attempt to recover the lost formation packer set in the well bore. In conversation with Chuck Dye on this day they shall attempt to recover the packer, if the packer is recovered they shall set a new packer on 4.5 casing in the well bore. The well is producing from the Berea Formation at approximately 1,500. Verbal communication was received by Chuck Dye on 06/26/2015 that they had indeed recovered the lost formation packer from the well bore and ran a log to indicate the well total depth and 6.625 casing total depth. |
| 833539680 | 2015-4-13 0:00: | PW | No Violations | 1.00 |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 1398690935 | US-OH-111805 | 2015-08-11 | Well shall be plugged |
For data sources see[8]