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| Well ID: 34-111-20757 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Monroe | |
| Municipality: Summit Township | |
| Operator Name: P P & G OIL | |
| Well Pad ID: | |
| Farm/Lease Name: CHIRSTMAN NOVA | |
| License Status: Producing | |
| License Date: 1970-09-10 | |
| Spud Date: 1947-11-21 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1947-12-22 | |
| Well Total Depth: 2074.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.740000 | |
| Longitude: -81.180000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1947-11-21 | RE-OPEN 9-16-70, |
| Completed | 1947-12-22 | RE-OPEN 9-16-70, |
| Reached Total Depth | 1947-12-22 | RE-OPEN 9-16-70, |
| CO | 1970-09-10 | 703 CHRISTMAN CHARLES E GeoDate 9/10/70 |
| Change of Owner | 2004-06-01 | Operator changed from 3735, CHRISTMAN NOVA A to 4695, P P & G OIL |
| Change of Owner | 2004-06-01 | Operator changed from 703, CHRISTMAN CHARLES E to 3735, CHRISTMAN NOVA A |
| Record Last Modified | 2018-05-30 | RE-OPEN 9-16-70, |
For data sources see[2]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2008 | P P & G OIL | 0.00 | 0.00 | 365 |
| 2009 | P P & G OIL | 0.00 | 0.00 | 365 |
| 2011 | P P & G OIL | 0.00 | 21.00 | 0 |
| 2012 | P P & G OIL | 0.00 | 9.00 | 366 |
| 2013 | P P & G OIL | 0.00 | 20.00 | 365 |
| 2014 | P P & G OIL | 0.00 | 24.00 | 365 |
| 2015 | P P & G OIL | 0.00 | 20.00 | 365 |
| 2016 | P P & G OIL | 0.00 | 0.00 | 365 |
| 2017 | P P & G OIL | 0.00 | 22.00 | 365 |
| 2018 | P P & G OIL | 0.00 | 21.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2008 | P P & G OIL | Brine | 0 | 365 |
| 2009 | P P & G OIL | Brine | 0 | 365 |
| 2011 | P P & G OIL | Brine | 4 | |
| 2012 | P P & G OIL | Brine | 0 | 366 |
| 2013 | P P & G OIL | Brine | 0 | 365 |
| 2014 | P P & G OIL | Brine | 0 | 365 |
| 2015 | P P & G OIL | Brine | 5 | 365 |
| 2016 | P P & G OIL | Brine | 0 | 365 |
| 2017 | P P & G OIL | Brine | 5 | 365 |
| 2018 | P P & G OIL | Brine | 4 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -757716255 | 2014-3-25 0:00: | PW | No Violations | 1.50 |
| 0154945180 | 2017-01-17 | Production Wells | No Violations | Compliance Notice #757716255 follow up inspection found that the well owner has addressed the previously noted pollution and contamination violation. |
| 0757716255 | 2014-03-25 | Production Wells | Violations Noted | Status check inspection found the following equipment present 6.625 casing-2 tubing and pumping rods with only a tubing production valve and line present and the well being produced by the means of a pumping unit, at the production area a single 100 barrel production tank is present with a 55 gallon fluid separator knock out tank set on top of the production tank all located in an established dike with proper well identification posted, on this day I followed the 1 drain line coming from the knock out tank mentioned as located on top of the production tank down over the hill and discovered the line was open ended and a impact scald area of 20 x 100 was observed and photographed. Jason Ludwig was contacted and informed that the well product could not be discharged into the ditchline or on the ground. |
| 154945180 | 2017-1-17 0:00: | PW | No Violations | 0.60 |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0757716255 | US-OH-128622 | 2017-01-18 | Well operation causing pollution and contamination |
For data sources see[7]