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34-111-21801

Well Details

Well ID: 34-111-21801
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Country: United States
State: Ohio
County: Monroe
Municipality: Center Township
Operator Name: P P & G OIL
Well Pad ID:
Farm/Lease Name: CALVERT GEORGE
License Status: Producing
License Date: 1969-10-23
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.760000
Longitude: -81.160000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Change of Owner 1999-09-02 Operator changed from 3735, CHRISTMAN NOVA A to 4695, P P & G OIL
Record Last Modified 2013-10-03

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1999 Bbl 30000 NSR

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 P P & G OIL 567.00 25.00 365
2009 P P & G OIL 314.00 52.00 365
2010 P P & G OIL 168.00 33.00 365
2011 P P & G OIL 246.00 93.00 0
2012 P P & G OIL 346.00 93.00 366
2013 P P & G OIL 317.00 0.00 365
2014 P P & G OIL 255.00 80.00 365
2015 P P & G OIL 91.00 40.00 365
2016 P P & G OIL 120.00 0.00 365
2017 P P & G OIL 81.00 0.00 365
2018 P P & G OIL 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 P P & G OIL Brine 20 365
2009 P P & G OIL Brine 10 365
2010 P P & G OIL Brine 12 365
2011 P P & G OIL Brine 17
2012 P P & G OIL Brine 19 366
2013 P P & G OIL Brine 22 365
2014 P P & G OIL Brine 190 365
2015 P P & G OIL Brine 80 365
2016 P P & G OIL Brine 0 365
2017 P P & G OIL Brine 0 365
2018 P P & G OIL Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-394207633 2004-4-21 0:00: PW No Violations
0394207633 2004-04-21 Production Wells No Violations No violations noted well was pumping on the day of my inspection.

Note:Clean up at well site preformed recently.

0506055044 2014-01-09 Production Wells Violations Noted Upon inspection it was observed that the production water is being discharged from a open valve on a plastic tank inside the tank battery and being allowed to flow through installed drain lines out of the dike and down over the hill behind the earthen containment dike with obvious signs of contamination present in a area of 3 x 30. Instructions are as follows- stop dispersant of production water onto the earth surface. Contact was made by phone to Jason Ludwig and a compliance notice was mailed out. ODNR contact Monroe Co inspector Bill Stolarik, Supervisor Rocky King Zanesville office-740-588-0631.
1077323387 2004-02-19 Production Wells No Violations Upon inspecting well site found clean up needed around wellhead company rep stated service rig had recently worked on well. Informed pumper that identification would need to be refreshed, small mess within dike area needs attention.unable to get GPS reading (cloud cover)Domestic Hookup!
1342111323 2012-07-12 Production Wells No Violations Inspection of the well head found the following equipment present, 2 tubing & rods with the production valves open and the well being produced by the means of a pumping unit. A 100 barrel tank and 1200 gallon plastic tank are present in an established dike with proper well identification.
1510837888 2017-11-15 Production Wells No Violations Order follow up 2016-1801. Upon inspection the well was observed to be equipped with casing tubing and rods and set up to be produced by the means of a pumping unit driven by an electric motor set on an automatic timer. The well was observed in operation and at the production facility fluid could be heard entering the production tank. Also noted is situated in close proximity to the well head is a commercial gas sales master meter separate form the domestic supply hook up at the well head. The production facility consists of a single 100 barrel production tank with a plastic 250 gallon tank also present. There is a earthen dike present around the production facility however the containment dike fluid drain valves are not secured with a plug and there is signs of stressed vegetation and salt deposits both inside and outside the dike.
1709191293 2014-05-01 Production Wells No Violations Compliance notice # 506055044 found the scald area behind the production tank area has been repaired and the surface discharge has ceased with the standing water inside the dike area tested with a high level chloride strip and no chloride levels found above 250 parts per million. The prior violation shall be resolved on this day.
325441397 2020-4-8 0:00:0 PW No Violations 0.60
506055044 2014-1-9 0:00:0 PW No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0506055044 US-OH-125517 2014-05-09 Well operation causing pollution and contamination
0506055044 US-OH-125518 2014-05-09 Dike or pit not able to prevent escape of brine or other wastes

For data sources see[8]

References