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34-111-21840

Well Details

Well ID: 34-111-21840
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Country: United States
State: Ohio
County: Monroe
Municipality: Center Township
Operator Name: D & D OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: CHRISTMAN CLAYTON
License Status: Producing
License Date: 1974-03-26
Spud Date: 1974-04-01
Spud Drilling Contractor:
Final Drill Date: 1974-11-19
Well Total Depth: 2400.00 ft
Configuration: Vertical
Latitude: 39.780000
Longitude: -81.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1974-03-26 703 CHRISTMAN CHARLES E GeoDate 3/26/74
Original Spud 1974-04-01 PERMIT EXPIRED
Completed 1974-11-19 PERMIT EXPIRED
Reached Total Depth 1974-11-19 PERMIT EXPIRED
Change of Owner 2013-03-08 Operator changed from 703, CHRISTMAN CHARLES E to 8874, D & D OIL & GAS LLC
Record Last Modified 2013-10-03 PERMIT EXPIRED

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 0 SAND, & ACID
ACID 0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 CHRISTMAN ROSALIE 0.00 168.00 360
1986 CHRISTMAN ROSALIE 0.00 159.00 360
1987 CHRISTMAN ROSALIE 0.00 205.00 360
1988 CHRISTMAN ROSALIE 0.00 100.00 360
1995 CHRISTMAN ROSALIE 0.00 136.00 0
1996 CHRISTMAN ROSALIE 0.00 73.00 0
1997 CHRISTMAN ROSALIE 0.00 88.00 0
1998 CHRISTMAN ROSALIE 0.00 98.00 365
1999 CHRISTMAN ROSALIE 0.00 60.00 365
2000 CHRISTMAN ROSALIE 0.00 116.00 365
2001 CHRISTMAN ROSALIE 567.00 100.00 365
2002 CHRISTMAN ROSALIE 1037.00 149.00 365
2003 CHRISTMAN ROSALIE 361.00 24.00 365
2004 CHRISTMAN ROSALIE 624.00 40.00 365
2005 CHRISTMAN ROSALIE 1663.00 375.00 365
2006 CHRISTMAN ROSALIE 208.00 116.00 365
2007 CHRISTMAN ROSALIE 0.00 94.00 365
2008 CHRISTMAN ROSALIE 359.00 60.00 365
2009 CHRISTMAN ROSALIE 354.00 96.00 365
2010 CHRISTMAN ROSALIE 180.00 98.00 365
2012 CHRISTMAN ROSALIE 602.00 69.00 0
2013 D & D OIL & GAS LLC 510.00 95.00 365
2014 D & D OIL & GAS LLC 501.00 63.00 365
2015 D & D OIL & GAS LLC 732.00 92.00 365
2016 D & D OIL & GAS LLC 745.00 62.00 365
2017 D & D OIL & GAS LLC 875.00 34.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 CHRISTMAN ROSALIE Brine 0 360
1986 CHRISTMAN ROSALIE Brine 0 360
1987 CHRISTMAN ROSALIE Brine 0 360
1988 CHRISTMAN ROSALIE Brine 0 360
1995 CHRISTMAN ROSALIE Brine 0 0
1996 CHRISTMAN ROSALIE Brine 0 0
1997 CHRISTMAN ROSALIE Brine 0
1998 CHRISTMAN ROSALIE Brine 0 365
1999 CHRISTMAN ROSALIE Brine 0 365
2000 CHRISTMAN ROSALIE Brine 0 365
2001 CHRISTMAN ROSALIE Brine 0 365
2002 CHRISTMAN ROSALIE Brine 0 365
2003 CHRISTMAN ROSALIE Brine 0 365
2004 CHRISTMAN ROSALIE Brine 0 365
2005 CHRISTMAN ROSALIE Brine 0 365
2006 CHRISTMAN ROSALIE Brine 0 365
2007 CHRISTMAN ROSALIE Brine 0 365
2008 CHRISTMAN ROSALIE Brine 0 365
2009 CHRISTMAN ROSALIE Brine 0 365
2010 CHRISTMAN ROSALIE Brine 0 365
2012 CHRISTMAN ROSALIE Brine 0 0
2013 D & D OIL & GAS LLC Brine 0 365
2014 D & D OIL & GAS LLC Brine 0 365
2015 D & D OIL & GAS LLC Brine 0 365
2016 D & D OIL & GAS LLC Brine 0 365
2017 D & D OIL & GAS LLC Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1192056607 2008-1-17 0:00: PW No Violations
1192056607 2008-01-17 Production Wells No Violations met with well owner about cleaning up at well site.tank needed diked and well needed diked also.upon this inspection date working on dikeand has diked up wellhead.well is supplied with pumpjack and a 100bbl tank.
1423765911 2015-02-12 Production Wells Violations Noted Producing well status check inspection found the following present at the well head 6.250 production casing along with 3 production tubing and rods with the production valves open and the well set up to be produced by the means of a pumping unit. A single 100 barrel production tank is present with a fluid knock out separator on top. It was observed on this day that there is a pit below the 100 barrel tank that the fluid knock out separator is being allowed to drain into with a visible oil sheen present, chloride levels were tested using low and high Quantab strip tests with the low the levels exceeding the low level strip tests and reading 1323 parts per million on the high level strip tests. There is also signs of long-term pollution and contamination at the well head where the stuffing box has leaked over a period of time. On the day of my inspection I met on site with Dean Christman with the following instructions given as follows - Immediately empty and remove the rusted out leaking 100 barrel production tank and remove the contaminated soil, recover the standing fluid located in the dike. Erect a containment dike capable of holding 110% of the largest vessel in the dike. The fluid knock separator is allowable but can not be constructed in such a way as to allow product to drain in any way other than into a gathering tank. The producer has 30 days maximum to complete the above tasks. ODNR Inspector Bill Stolarik 740-507-6592.
1425996952 2015-03-10 Production Wells No Violations Follow up inspection to the violation # 1423765911 issued on 02-13-2015. Upon inspection of the production tank it was observed that the tank was no longer leaking fluid. Contact was made with the well owner Dean Christman @ 10:14 am on this day and he indicated that the well was shut in and not pumping to avoid any further fluid loss and a new tank has been purchased for the well. We agreed on this day to allow time for the weather to cooperate before constructing a new tank pad.
1426673581 2015-03-17 Production Wells No Violations On this day it was observed upon inspection that the production tank that was leaking has been removed and the area remediated. A new tank pad has been built with a new 100 barrel tank placed in use. Compliance Action # 1423765911 issued on 02/13/2015 has been considered resolved on this day.
1515595334 2018-01-10 Production Wells No Violations Status check inspection found the well equipped with production casing- tubing and pumping rods. There is both tubing and casing production flow lines attached to the well head with valves present in line and in the open position. The production facility consists of a single 100 barrel steel production tank along with a 1,600 gallon plastic brine tank. The producer has erected an earthen dike around the production facility. Also noted is the producer has reported commercial production but no brine disposal.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1423765911 US-OH-112358 2015-03-31 Well operation causing pollution and contamination
1423765911 US-OH-112359 2015-03-31 No SPCC dike/or failure to keep dike free of water or oil
1423765911 US-OH-112360 2015-03-31 Unlawful use of pit for temporary storage of brine or other wastes
1423765911 US-OH-112361 2015-03-31 Failure to keep dike or pit free of brine or other wastes

For data sources see[8]

References