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Well ID: 34-111-21982 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Malaga Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: HOTHEM LUTHER C | |
License Status: Producing | |
License Date: 1980-10-01 | |
Spud Date: 1980-11-09 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-11-13 | |
Well Total Depth: 2052.00 ft | |
Configuration: Vertical | |
Latitude: 39.860000 | |
Longitude: -81.210000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-10-01 | 30 BANDS CO INC GeoDate 10/1/80 |
Original Spud | 1980-11-09 | R.I. 10-2-80 |
Completed | 1980-11-13 | R.I. 10-2-80 |
Reached Total Depth | 1980-11-13 | R.I. 10-2-80 |
CO | 1993-11-04 | 4695 P P & G OIL GeoDate 10/1/80 |
Change of Owner | 2010-02-08 | Operator changed from 4695, P P & G OIL to 1634, NORTHWOOD ENERGY CORP |
Record Last Modified | 2013-10-03 | R.I. 10-2-80 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1694 | 1916 | 25 |
1694 | 1916 | 25 | |
1694 | 1916 | 25 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1800 Bbl | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | BANDS COMPANY INC | 745.00 | 0.00 | 365 |
1991 | BANDS COMPANY INC | 2401.00 | 18.00 | 365 |
1992 | BANDS COMPANY INC | 2985.00 | 0.00 | 365 |
1993 | BANDS COMPANY INC | 1322.00 | 0.00 | 365 |
2008 | P P & G OIL | 970.00 | 0.00 | 365 |
2009 | P P & G OIL | 1540.00 | 0.00 | 365 |
2010 | NORTHWOOD ENERGY CORP | 432.00 | 0.00 | 365 |
2011 | NORTHWOOD ENERGY CORP | 524.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 278.00 | 0.00 | 366 |
2013 | NORTHWOOD ENERGY CORP | 368.00 | 0.00 | 365 |
2014 | NORTHWOOD ENERGY CORP | 461.00 | 0.00 | 365 |
2015 | NORTHWOOD ENERGY CORP | 666.00 | 0.00 | 365 |
2016 | NORTHWOOD ENERGY CORP | 680.00 | 0.00 | 365 |
2017 | NORTHWOOD ENERGY CORP | 514.00 | 0.00 | 365 |
2018 | NORTHWOOD ENERGY CORP | 107.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | BANDS COMPANY INC | Brine | 0 | 365 |
1991 | BANDS COMPANY INC | Brine | 0 | 365 |
1992 | BANDS COMPANY INC | Brine | 0 | 365 |
1993 | BANDS COMPANY INC | Brine | 0 | 365 |
2008 | P P & G OIL | Brine | 0 | 365 |
2009 | P P & G OIL | Brine | 0 | 365 |
2010 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2011 | NORTHWOOD ENERGY CORP | Brine | 0 | |
2012 | NORTHWOOD ENERGY CORP | Brine | 0 | 366 |
2013 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2014 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2015 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2016 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2017 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2018 | NORTHWOOD ENERGY CORP | Brine | 68 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-915253836 | 2009-3-3 0:00:0 | PW | No Violations | |
0915253836 | 2009-03-03 | Production Wells | No Violations | WELL HAD PUMPJACK.RODS WERE PULLED.WELL IS MAKING GAS.NO PRODUCTION IS BEING TURNED IN.WILL CALL OWNER. |
1361364351 | 2013-02-20 | Production Wells | No Violations | Inspection of the well head found the following equipment present-4.5 production casing-1.5 tubing. Inspector will note that the tubing is not hooked up and that the well is set up to produce gas off the 4.5 only. A single 100 barrel tank is present with a gas sales meter that has a current sales chart . |
1396881429 | 2014-04-07 | Production Wells | No Violations | Status check inspection of the tank battery. On this day while traveling East on Monroe County road 39 a strong smell of gas was present in the air and upon inspection of the tank battery I observed the 2 gas sales line had been broken off at the meter run. I will note that the area id being used as a recreational atv park and this is the 3rd time that the production equipment has been damaged. Bill Arnholt with Northwood Energy was notified at 9:10 am this morning of the gas leak. |
For data sources see[9]