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Well ID: 34-111-22235 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Malaga Township | |
Operator Name: G-R CONTRACTING INC | |
Well Pad ID: | |
Farm/Lease Name: FORREST FRANK | |
License Status: Final Restoration | |
License Date: 2016-11-01 | |
Spud Date: 1981-02-01 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-03-19 | |
Well Total Depth: 2750.00 ft | |
Configuration: Vertical | |
Latitude: 39.820000 | |
Longitude: -81.170000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-12-31 | 2107 GORDON ENERGY CORP GeoDate 12/31/80 |
Oil and Gas | 1980-12-31 | Issued Date 12/31/80 Expired Date 12/31/81 Acres 0040000 Tool Type CT Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1981-02-01 | UPDATED LOCATION PER SURVEYOR COORDINATE-03/15/2017-ALE. |
Completed | 1981-03-19 | UPDATED LOCATION PER SURVEYOR COORDINATE-03/15/2017-ALE. |
Reached Total Depth | 1981-03-19 | UPDATED LOCATION PER SURVEYOR COORDINATE-03/15/2017-ALE. |
Completion Report Received | 1981-04-23 | UPDATED LOCATION PER SURVEYOR COORDINATE-03/15/2017-ALE. |
CO | 1992-11-23 | 952 G-R CONTRACTING INC GeoDate 12/31/80 |
APP | 2016-11-01 | Proposed Formations:OHIO SHALE, Issued Date:11/1/2016, Expired Date:11/1/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-10-13 | UPDATED LOCATION PER SURVEYOR COORDINATE-03/15/2017-ALE. |
Record Last Modified | 2018-06-29 | UPDATED LOCATION PER SURVEYOR COORDINATE-03/15/2017-ALE. |
Construction Permit Expires | 2018-11-01 | UPDATED LOCATION PER SURVEYOR COORDINATE-03/15/2017-ALE. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2307 | 2323 | 0 |
2006-09-11 | 2414 | 2429 | 0 |
2307 | 2323 | 0 | |
2307 | 2323 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 930 Bbl | 90000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | GORDON ENERGY CORP | 5791.00 | 0.00 | 0 |
1985 | SUPERIOR PETROL SERV INC | 567.00 | 0.00 | 300 |
1986 | WESTERN HEMISPHERE GROUP | 557.00 | 0.00 | 300 |
1987 | WESTERN HEMISPHERE GROUP | 564.00 | 0.00 | 300 |
1988 | GORDON ENERGY CORP | 5567.00 | 45.00 | 365 |
1989 | WESTERN HEMISPHERE GROUP | 560.00 | 0.00 | 300 |
1991 | GORDON ENERGY CORP | 4162.00 | 28.00 | 310 |
1996 | G-R CONTRACTING INC | 1519.00 | 0.00 | 365 |
1997 | G-R CONTRACTING INC | 1265.00 | 0.00 | 365 |
1998 | G-R CONTRACTING INC | 1121.00 | 0.00 | 365 |
2000 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2001 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2002 | G-R CONTRACTING INC | 466.00 | 0.00 | 365 |
2003 | G-R CONTRACTING INC | 791.00 | 44.00 | 365 |
2004 | G-R CONTRACTING INC | 1277.00 | 0.00 | 365 |
2005 | G-R CONTRACTING INC | 1189.00 | 0.00 | 365 |
2006 | G-R CONTRACTING INC | 824.00 | 0.00 | 365 |
2007 | G-R CONTRACTING INC | 557.00 | 0.00 | 365 |
2008 | G-R CONTRACTING INC | 469.00 | 0.00 | 365 |
2009 | G-R CONTRACTING INC | 430.00 | 0.00 | 365 |
2010 | G-R CONTRACTING INC | 374.00 | 0.00 | 365 |
2011 | G-R CONTRACTING INC | 243.00 | 0.00 | 365 |
2012 | G-R CONTRACTING INC | 203.00 | 0.00 | 366 |
2013 | G-R CONTRACTING INC | 270.00 | 0.00 | 365 |
2014 | G-R CONTRACTING INC | 226.00 | 0.00 | 365 |
2015 | G-R CONTRACTING INC | 269.00 | 0.00 | 365 |
2016 | G-R CONTRACTING INC | 170.00 | 0.00 | 365 |
2017 | G-R CONTRACTING INC | 84.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | GORDON ENERGY CORP | Brine | 0 | 0 |
1985 | SUPERIOR PETROL SERV INC | Brine | 0 | 300 |
1986 | WESTERN HEMISPHERE GROUP | Brine | 0 | 300 |
1987 | WESTERN HEMISPHERE GROUP | Brine | 0 | 300 |
1988 | GORDON ENERGY CORP | Brine | 0 | 365 |
1989 | WESTERN HEMISPHERE GROUP | Brine | 0 | 300 |
1991 | GORDON ENERGY CORP | Brine | 40 | 310 |
1996 | G-R CONTRACTING INC | Brine | 0 | 365 |
1997 | G-R CONTRACTING INC | Brine | 0 | 365 |
1998 | G-R CONTRACTING INC | Brine | 0 | 365 |
2000 | G-R CONTRACTING INC | Brine | 0 | 365 |
2001 | G-R CONTRACTING INC | Brine | 0 | 365 |
2002 | G-R CONTRACTING INC | Brine | 0 | 365 |
2003 | G-R CONTRACTING INC | Brine | 0 | 365 |
2004 | G-R CONTRACTING INC | Brine | 0 | 365 |
2005 | G-R CONTRACTING INC | Brine | 0 | 365 |
2006 | G-R CONTRACTING INC | Brine | 0 | 365 |
2007 | G-R CONTRACTING INC | Brine | 0 | 365 |
2008 | G-R CONTRACTING INC | Brine | 0 | 365 |
2009 | G-R CONTRACTING INC | Brine | 0 | 365 |
2010 | G-R CONTRACTING INC | Brine | 0 | 365 |
2011 | G-R CONTRACTING INC | Brine | 0 | 365 |
2012 | G-R CONTRACTING INC | Brine | 0 | 366 |
2013 | G-R CONTRACTING INC | Brine | 0 | 365 |
2014 | G-R CONTRACTING INC | Brine | 0 | 365 |
2015 | G-R CONTRACTING INC | Brine | 0 | 365 |
2016 | G-R CONTRACTING INC | Brine | 0 | 365 |
2017 | G-R CONTRACTING INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1595793814 | 2016-4-1 0:00:0 | AM | No Violations | |
-1934009240 | 2004-8-9 0:00:0 | PW | No Violations | |
-829273763 | 2017-1-5 0:00:0 | AM | No Violations | 0.20 |
0146346804 | 2015-03-23 | Production Wells | Violations Noted | Inspection per request of the landowner as part of complaint # 4969. Upon inspection of the well head the following equipment was found-4.5 production casing-2.375 tubing with the production valves in the open position and the well set up to be produced by the means of a plunger lift system. At the production fluid storage area 2-100 barrel production tanks were found along with mechanical separator and gas sales meter with a current active sales chart. Addressing the complaint by the landowner that the said well has a hole in the 4.5 casing contact was made with Jordan Jones with G&R contracting who indicated the well did have downhole issues that need addressed. |
0829273763 | 2017-01-05 | Administrative Inspection | No Violations | Administrative inspection follow up to violation #146346804 and complaint # 4649. A plugging permit has been issued and the well is slated to be plugged this year. |
1403045700 | 2017-10-13 | Plug / Plug Back | No Violations | On this day, I accompanied ODNR Inspector William Stolarik. Please refer to his comments for a detailed report. G & R Contracting and Formation Cementing are onsite. A 200 foot rip plug was set at a depth of 1,260 feet. The 4 1/2 inch diameter casing was then pulled up to 980 feet where a 200 foot plug was set. Then, the casing was pulled up to 200 feet to set the surface plug. |
1456243700 | 2016-02-23 | Production Wells | No Violations | Compliance Follow up inspection in response to complaint # 4649. On this day I met with the landowner Frank Forest and explained the well construction and how the fresh water aquifer was protected by the setting of the surface casing. I also spoke with the Divisions Permitting Geologist Steve Opritza who indicated the nearest water well was 1,600 away. Addressing the unresolved violation # 146346804. On this day it was observed that the well is set up to be produced by the means of a plunger lift system with the tubing valve in the open position and the gas sales meter showing active production, the meter is however a conjoined meter between multiple wells in the area owned by the same producer identified as G-R Contracting. On this day I also notified a Jordan Jones with G-R Contracting and advised him of the unresolved violation. Jordan indicated that they would address the issue by either plugging the well or setting an isolation packer. |
146346804 | 2015-3-23 0:00: | PW | No Violations | 1.00 |
1474979170 | 2016-09-27 | Production Wells | No Violations | Follow up inspection to violation #146346804 and complaint # 4649 found the well equipped with 4.5 production casing and 2.375 tubing with the well set up to be produced by the means of a plunger lift system and the master control box being found to be out of service, the production valves are open and the 2 sales line valve is closed down stream from the well head. Historically the well has a hole in the 4.5 production casing located below the surface pipe at 1,700. On this day I contacted Jordan Jones with G_R Contracting and informed him of the unresolved violation and to apply for a plugging permit with the Division. |
1507827056 | 2017-10-12 | Plug / Plug Back | No Violations | On site inspection accompanied by ODNR Inspector Tom Thomas. Upon arrival I discovered that the company owned service rig had set the 3.275 upset 8 round tubing to a total depth 2,307 and the well completion records indicate the bottom perforating is at 2,429 so I required the company to run in 4 more tubing joints to a total depth of 2,470. The extra 4 tubing joints were not on location and had to be brought in. Once the tubing was in the hole Formation Cementing began to circulate with fresh water and the well began to unload so I then required the company to stop circulation with fresh water and bring in brine water to so the well would be properly killed and remain static. The company owned water truck brought in brine and the well was circulated until static with approximately 25 barrels of oil being evacuated out of the well before the well was static and cement was pumped down the well bore. Formation than pumped a 6.30 barrels absolute volume bottom plug consisting of 30 sacks of 1.18 yield 15.6 pound per gallon cement with gel spacer ran ahead and behind the cement. The rig then pulled the tubing and the wireline will tag the top of cement on the next working day before shooting the casing off. There is also a unresolved violation #146346804 and complaint # 4649 against the well that will be considered resolved upon the completion of the plugging process. The previous complaint and violation are considered resolved on this day. |
1507828513 | 2017-10-12 | Plug / Plug Back | No Violations | On this day, I accompanied ODNR Inspector William Stolarik. Please refer to his comments for a detailed report. G & R Contracting are onsite with a service rig and Formation Cementing is onsite pumping the bottom plug. The tubing was set at a depth of 2,470 feet. Well circulated approximately 25 barrels of oil into a pit and all oil was removed from location on this day. Brine water was used to stabilize the well. 30 sacks of cement, with a yield of 1.18 and 15.6 pounds per gallon were pumped for the bottom plug. |
1507914248 | 2017-10-13 | Plug / Plug Back | No Violations | On site at 8.00 am to witness the last stages of the plug job with Formation Cementing to set a 200 rip plug through he 4.5 diameter casing set at 1,260. The plug was an absolute volume of 13.4 barrels mix and consisted of 60 sacks of class A cement. And 1% gel cement additives, the cement was displaced with 16.8 barrels of fresh water and equalized properly upon reaching total displacement. Of 16.8 barrels. The 4.5 diameter casing was then pulled up to 980 and a 200 plug set to cover the bottom of the surface that was also 13 barrels absolute volume and consisted of 60 sacks of cement, the plug was displaced with 13 barrels of fresh water. The rig then pulled the 4.5 diameter casing up to 200 for the setting of the surface plug with cement returns to surface and the remainder of the casing pulled and the well bore topped of with cement to 30 below grade level. |
1529330599 | 2018-06-18 | Final Restoration | No Violations | On site inspection found the well site meets ORC 1509.072 with vegetation established and erosion control in place. The plugging pit has been closed. The production facility is shared with other wells on the lease still active. |
1595793814 | 2016-04-01 | Administrative Inspection | No Violations | Administrative inspection to document that on 03/31/2016 I received a phone call from Jordon Jones with G&R Contracting who indicated they would be plugging the said well. |
1934009240 | 2004-08-09 | Production Wells | No Violations | No violations noted on the day of my inspection.
Unable to get GPS reading due to cloud cover. |
2055774811 | 2016-06-15 | Administrative Inspection | No Violations | Follow up administrative inspection to violation #146346804 and complaint # 4649. On this day I stopped by G-R Contractings Lewisville office and spoke with Dick Sulzberger in regards to the unresolved violation. Mr. Sulzberger indicated they planned on plugging the well. I informed Him they needed to apply for a plugging permit and address the violation. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0146346804 | US-OH-113425 | 2017-10-17 | Defective casing, leaking well |
For data sources see[9]