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Well ID: 34-111-23737 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Ohio Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: DENNIS | |
License Status: Final Restoration | |
License Date: 2014-11-14 | |
Spud Date: 1999-02-17 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 1999-02-22 | |
Well Total Depth: 6681.00 ft | |
Configuration: Vertical | |
Latitude: 39.690000 | |
Longitude: -80.880000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 1999-01-29 | Proposed Formations:BEREA THRU ORISKANY, Issued Date:1/29/99, Expired Date:1/29/00 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW |
Original Spud | 1999-02-17 | RBDMS Rec |
Completed | 1999-02-22 | RBDMS Rec |
Reached Total Depth | 1999-02-22 | RBDMS Rec |
Completion Report Received | 1999-06-07 | RBDMS Rec |
Change of Owner | 2006-02-03 | Operator changed from 2789, SMELTZER BENJAMIN CO to 1634, NORTHWOOD ENERGY CORP |
APP | 2014-11-14 | Proposed Formations:HELDERBERG LIMESTONE, Issued Date:11/14/2014, Expired Date:11/13/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-01-04 | RBDMS Rec |
Construction Permit Expires | 2016-11-13 | RBDMS Rec |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1999-09-07 | 6538 | 6542 | 17 |
6538 | 6542 | 17 | |
6538 | 6542 | 17 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 40000 Gal | 0 | 250 GALLONS HCL ACID |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2005 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2006 | NORTHWOOD ENERGY CORP | 88.00 | 0.00 | 365 |
2007 | NORTHWOOD ENERGY CORP | 885.00 | 0.00 | 365 |
2008 | NORTHWOOD ENERGY CORP | 416.00 | 0.00 | 365 |
2009 | NORTHWOOD ENERGY CORP | 324.00 | 0.00 | 365 |
2010 | NORTHWOOD ENERGY CORP | 489.00 | 0.00 | 365 |
2011 | NORTHWOOD ENERGY CORP | 243.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 296.00 | 0.00 | 366 |
2013 | NORTHWOOD ENERGY CORP | 424.00 | 0.00 | 365 |
2014 | NORTHWOOD ENERGY CORP | 1025.00 | 0.00 | 365 |
2015 | NORTHWOOD ENERGY CORP | 36.00 | 0.00 | 60 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2005 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2006 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2007 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2008 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2009 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2010 | NORTHWOOD ENERGY CORP | Brine | 24 | 365 |
2011 | NORTHWOOD ENERGY CORP | Brine | 0 | |
2012 | NORTHWOOD ENERGY CORP | Brine | 70 | 366 |
2013 | NORTHWOOD ENERGY CORP | Brine | 114 | 365 |
2014 | NORTHWOOD ENERGY CORP | Brine | 70 | 365 |
2015 | NORTHWOOD ENERGY CORP | Brine | 0 | 60 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1075531252 | 2015-1-14 0:00: | PB | No Violations | 4.00 |
-1343311190 | 2009-4-8 0:00:0 | PW | No Violations | |
0012177026 | 2002-09-24 | Production Wells | No Violations | |
1075531252 | 2015-01-14 | Plug / Plug Back | No Violations | 01/14/2014 On site inspection to witness the 25 sack bottom hole plug set through 1.5 tubing at 6,550 by Cemenco Inc with a calculated top of cement to be 6,210. Davis Well Service is the service rig on location and shall pull the 1.5 tubing with a proposed plan to perforate the 4.5 production casing on 01/15/2015 and establish annular circulation then pump a bottom hole balanced plug to isolate the Marcellus. |
12177026 | 2002-9-24 0:00: | PW | No Violations | |
1343311190 | 2009-04-08 | Production Wells | No Violations | WELL IS SUPPLIED WITH A8 5/8 CAS,4 1/2 CAS,4X2 REDUCER TEE AND THEN SALES LINE.ANNULUS IS SHUT OFF.TANK IS 100BBL THAT IS LEAKING AT HEAT TUBE. CALLED MIKE CORP AND WILL REPLACE TANK.THE WELL WILL BE A MARCELLUS CANIDATE. |
1421423892 | 2015-01-15 | Plug / Plug Back | No Violations | Administrative inspection to document the plugging activities on this day not witnessed by the inspector due to being required to attend a monthly Division meeting. A -500- 2nd bottom plug set by perforating the 4.5 above TOC on annular side and breaking circulation and displacing a balance plug to cover the Marcellus formation with 6 perforations shot at 6,040. The top of cement was tagged with the wireline on the bottom plug set through tubing on the previous day at 6,040 |
1421430705 | 2015-01-16 | Plug / Plug Back | No Violations | 01/16/15 JET wireline ran in and tagged the top of cement @ 5,313 and cut the 4.5 with a chemical cuter @ 5,313 one joint was pulled out of the hole and plugging will resume on 01/19/2014. |
1423137156 | 2015-02-05 | Plug / Plug Back | No Violations | 02/05/2015 The 4.5 has been pulled and 1.5 ran into 2,480 with a 400 plug set to cover the Berea, the tubing was then pulled up to 1,636 and a 200 plug set to cover the bottom of the surface casing. A final 200 to surface plug was then set with the cement staying up to surface. Davis Well Service was the rig and Cemenco was the plugging contractor along with JET wireline Service throughout the job, Earl Barns was the company representative on site throughout the cementing process. H&L water truck service was the water hauler with the plugging pit being emptied at the end of each working day. The well casing will be cut off @ 30 and the production equipment removed along with the well site restored when the weather breaks in the spring. |
1437523847 | 2015-07-21 | Final Restoration | No Violations | Final Restoration status check inspection found the well casing has been cut off below grade and the area reclaimed with the production equipment removed and the roadway restored and noticeable vegetation established. The restoration meets ORC 1509.072. |
1872212311 | 2015-01-22 | Plug / Plug Back | No Violations | I am onsite to witness the rip plug and the first stage of the Devonian isolation plug. The company representative Earl Barns informed me that they believed the casing was plugged. Jet Wireline Services ran a chemical casing cutter in the casing to cut the casing off above the obstruction; however no obstruction was found. The decision was then made to attempt to pull a few joints of casing to determine if it was free prior to spotting the rip plug. Four joints of casing were pulled before the casing was free. A 57 sack class A cement plug was placed at 5036 with 14 sacks of gel spacer balanced above the plug. The casing was then pulled up to a depth of 3011. Cemenco then placed a 120 sack plug (400) to cover the bottom of the Upper Devonian formations. Circulation was established and maintained through out all plug emplacement. |
iDIAN00165 | 1999-09-07 | Preliminary Restoration | No Violations | |
iDIAN001654 | 1999-9-7 0:00:0 | PL | No Violations |
For data sources see[9]