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34-111-24213

Well Details

Well ID: 34-111-24213
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Country: United States
State: Ohio
County: Monroe
Municipality: Lee Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: FETTY LUTHER
License Status: Producing
License Date: 2008-08-11
Spud Date: 2008-08-19
Spud Drilling Contractor: G & L DRILLING
Final Drill Date: 2008-09-04
Well Total Depth: 6330.00 ft
Configuration: Vertical
Latitude: 39.650000
Longitude: -80.990000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-08-11 Proposed Formations:BEREA/DEVONIAN SHALE THRU ORISKANY, Issued Date:8/11/2008, Expired Date:8/11/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2008-09-04
Construction Permit Expires 2009-08-11
Completion Report Received 2009-09-24
Change of Owner 2013-05-29 Operator changed from 8172, APPALACHIAN ENERGY RES LLC to 8844, ECLIPSE RESOURCES I LP
Change of Owner 2016-07-25 Operator changed from 8844, ECLIPSE RESOURCES I LP to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2016-07-25

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2009-12-29 2386 2390 10
2009-12-29 2274 2326 16
2274 2326 16
2386 2390 10
2566 2648 26
2796 2838 32
2972 2982 10
2274 2326 16
2009-12-29 2566 2648 26
2009-12-29 2972 2982 10
2009-12-29 2796 2838 32

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 20 105000 Gal 0 STAGE 1 OF 3…GORDON & FIFTH SANDS
H2O 20 108960 Gal 0 STAGE 3 OF 3…FRAC PLUG SET @ 2460'…INCLUDES WEIR SAND
H2O 20 105000 Gal 0 STAGE 2 OF 2…FRAC PLUG SET @ 2720'

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2009 APPALACHIAN ENERGY RES LLC 3890.00 102.00 365
2010 APPALACHIAN ENERGY RES LLC 2017.00 0.00 365
2011 APPALACHIAN ENERGY RES LLC 1068.00 13.00 365
2012 APPALACHIAN ENERGY RES LLC 1014.00 35.00 366
2013 ECLIPSE RESOURCES I LP 158.00 0.00 180
2014 ECLIPSE RESOURCES I LP 753.00 0.00 357
2016 M & R INVESTMENTS OHIO LLC 0.00 0.00 365
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2009 APPALACHIAN ENERGY RES LLC Brine 1363 365
2010 APPALACHIAN ENERGY RES LLC Brine 0 365
2011 APPALACHIAN ENERGY RES LLC Brine 106 365
2012 APPALACHIAN ENERGY RES LLC Brine 171 366
2013 ECLIPSE RESOURCES I LP Brine 0 180
2014 ECLIPSE RESOURCES I LP Brine 0 357
2016 M & R INVESTMENTS OHIO LLC Brine 9 365
2017 M & R INVESTMENTS OHIO LLC Brine 0 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1510641504 2008-8-22 0:00: DD No Violations
-173433044 2008-9-2 0:00:0 DD No Violations
-2100133187 2008-9-3 0:00:0 PB No Violations
-305566349 2009-1-16 0:00: PW No Violations
-5578426 2020-2-26 0:00: PW No Violations 0.60
-558446278 2008-9-4 0:00:0 PB No Violations
0173433044 2008-09-02 Drill / Deepen / Reopen No Violations THE FIRST STRING FLOAT IS AT 3288.THE WIRELINE WILL NOT GET ANY FARTHER THAN THIS.WE HAD TO LOAD THE HOLE WITH BRINE WATER.TIMCO WENT IN TO SHOOT THE PIPE OFF WITH AN 1 3/8 SHOT.FIRED OFF BUT PIPE DID NOT SEPARATE.CONTINUED THIS FOR ALL DAY.ABOUT THE 6TH TIME WE HAD NO SHOT LEFT.WE TRIED PRIMER CORD NO LUCK.CALLED AROUND ABOUT A COLLAR BUSTER.JET WIRELINE WILL COME 9-3-08 .
0305566349 2009-01-16 Production Wells No Violations BRIAN CHAVEZ FROM HEINRICH ENTERPRIZES CALLED ON TANK THAT BURPED A LITTLE OIL INTO THE DIKE.WAS CONTAINED AND CLEANED UP WITH DIAPERS.
0558446278 2008-09-04 Plug / Plug Back No Violations ON THIS DAY WE RAN A 15SUB BELOW THE SHOT.RAN INTO HOLE FINALLY GOT THROUGH DOWNHOLE TOOL AND GOT TO FIRST FLOAT.SHOT OFF NO GO.PULLED OUT RAN IN AGAIN.WITH THIRTY SHOT PULLED UP ON THE JARS ALITTLE SHOT OFF AT 3187.PIPE JUMPED THREE FEET DRIVING TOP DRIVE UP.PULLED DRILLPIPE AND LOGGED HOLE WITH JET WIRELINE.RAN 4.5 CASING TO 3150 AND PUT LATCHDOWN INSERT AT ONE JT.UP WHICH IS 42 FT.MADE A GORDON WELL OUT OF IT.
0757618463 2012-07-23 Production Wells No Violations Inspection of the well site found the following equipment, 7 surface casing, 4.5 production casing, 1.5 tubing & rods with the production valves open and the well being produced by the means of a pumping unit. At the production fluid storage area the following equipment is present, 2-100 barrel tanks along with a separator and gas meter with proper well identification and an established dike impoundment.
1221822903 2008-08-29 Drill / Deepen / Reopen No Violations ON DAY OF INSPECTION OF WORK WELL WAS TD AT 6332 AND PIPE WAS STUCK IN HOLE.THE RIG PULLED PIPE AFTER DRILLING AND AFTER 11 JTS WERE PULLED PIN BROKE ON DRILL PIPE AND PIPE WITH A STRING WEIGHT OF OVER 60,000 LBS WENT STRAIGHT DOWN.THE RIG AND TWO PORTAPOWERS WERE USED TO PULL PIPE UP AND COULD ONLY GET ABOUT 1 FT OF STRETCH.WE THEN GOT OFF OF DRILLPIPE AND CALLED TIMCO WIRELINE.THEY WOULD SHOW UP ONSEPT 2ND.
1389634358 2014-01-13 Preliminary Restoration No Violations The well site meets 1509.072, 2-100 barrel tanks are present in an established dike area with proper identification posted.
1491778978 2017-04-07 Production Wells No Violations On 04/06/2017 the landowner contacted me and indicated the well head stuffing box had leaked oil onto the well head and on the ground around the well head. The landowner indicated the product was minimal and contained around the well head and he also shut the well in and off. I contacted Eddie Moss and Darrin Crum who are company men for M&R Investments and they had field personnel respond and address the issue. I followed up the following morning 04/07/2017 to find no product on the earths surface around the well head.
1510641504 2008-08-22 Drill / Deepen / Reopen No Violations ON THE DAY OF BOP TEST.WE STARTED TO HOOK THINGS UP AND WE HAD LEAKS. DISASSEMBLED EVERYTHING AND TAPED UP BOPS.PRESSURED UP TO 300 PSI. HELD FOR APPROXIMATE 30 MIN.HELD GOOD.
2100133187 2008-09-03 Plug / Plug Back No Violations JET SHOWED UP AND RAN IN WIRELINE WITH 1 11/16 SHOT.MADE FIRST RUN IN.20SHOTS ON A WIRE.FLIUD LEVEL AT 2200 FT.COULD NOT GET BIGGER SHOT DOWN HOLE.PAST DOWNHOLE TOOL.(HYDRAULIC JARS,OVERSHOT.)WHICH WERE AT 2625.
757618463 2012-7-23 0:00: PW No Violations

For data sources see[9]

References

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