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Well ID: 34-111-24287 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Wayne Township | |
Operator Name: WEISS DRILLING INC | |
Well Pad ID: | |
Farm/Lease Name: SMTH BERNARD C | |
License Status: Final Restoration | |
License Date: 2015-10-01 | |
Spud Date: 2011-05-23 | |
Spud Drilling Contractor: R WOLFE DRLG | |
Final Drill Date: 2011-05-24 | |
Well Total Depth: 1275.00 ft | |
Configuration: Vertical | |
Latitude: 39.740000 | |
Longitude: -81.240000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-02-07 | Proposed Formations:KEENER, Issued Date:2/7/2011, Expired Date:2/6/2013 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2011-05-24 | |
Completion Report Received | 2011-07-07 | |
APP | 2015-10-01 | Proposed Formations:KEENER SAND, Issued Date:10/1/2015, Expired Date:9/30/2017 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-02-25 | |
Construction Permit Expires | 2017-09-30 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-09-14 | 1235 | 1240 | 0 |
2011-09-14 | 1245 | 1250 | 0 |
1245 | 1250 | 0 | |
1235 | 1240 | 0 | |
1235 | 1240 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2011-06-20 | 0 | 0 | 0 | USED 2 5' GAS GUNS, PROPELLANT STIMULATIONS
PACKER SET@1154' |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2000 | KLJ INC | 80.00 | 70.00 | 205 |
2009 | WHITACRE ENTERPRISES | 52.00 | 29.00 | 365 |
2011 | WEISS DRILLING INC | 0.00 | 0.00 | 90 |
2012 | WEISS DRILLING INC | 0.00 | 82.00 | 366 |
2013 | WEISS DRILLING INC | 0.00 | 0.00 | 365 |
2014 | WEISS DRILLING INC | 0.00 | 75.00 | 365 |
2015 | WEISS DRILLING INC | 0.00 | 0.00 | 100 |
2016 | WEISS DRILLING INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2000 | KLJ INC | Brine | 0 | 205 |
2009 | WHITACRE ENTERPRISES | Brine | 0 | 365 |
2011 | WEISS DRILLING INC | Brine | 0 | 90 |
2012 | WEISS DRILLING INC | Brine | 0 | 366 |
2013 | WEISS DRILLING INC | Brine | 147 | 365 |
2014 | WEISS DRILLING INC | Brine | 114 | 365 |
2015 | WEISS DRILLING INC | Brine | 15 | 100 |
2016 | WEISS DRILLING INC | Brine | 21 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1456421331 | 2016-02-25 | Plug / Plug Back | No Violations | 02/25/2016 - A service rig owned by Chuck Dye is now on the hole and has pulled the production equipment and ran 1.5 tubing in the hole to 1,258, Formation Cementing is on location and set a bottom 40 sack 500 cement plug through the tubing. The tubing was pulled and the 4.5 shot off at 594 by JET Wireline. Formation Cementing then set a 210 plug to cover the bottom of the 7 surface casing set at 484. The 4.5 was then pulled up to 200 and a surface plug was then set, completing the plugging process. |
1473849389 | 2016-06-30 | Final Restoration | No Violations | The well site meets ORC 1509.072. |
For data sources see[9]