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| Well ID: 34-111-24302 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Monroe | |
| Municipality: Washington Township | |
| Operator Name: GULFPORT ENERGY CORPORATION | |
| Well Pad ID: US-OH-000470 | |
| Farm/Lease Name: WHITACRE ENTERPRISES INC | |
| License Status: Plugged Back | |
| License Date: 2011-08-16 | |
| Spud Date: 2011-08-29 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 2011-10-24 | |
| Well Total Depth: 9310.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.660000 | |
| Longitude: -81.200000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2011-08-16 | Proposed Formations:TRENTON BLACK RIVER, Issued Date:8/16/2011, Expired Date:8/15/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
| Correction to Well | 2011-09-16 | CORRECTION TO CASING PROGRAM |
| Reached Total Depth | 2011-10-24 | |
| Plugged Back | 2011-10-25 | |
| Completion Report Received | 2012-01-10 | |
| Construction Permit Expires | 2013-08-15 | |
| Change of Owner | 2015-02-25 | Operator changed from 8793, HG ENERGY LLC to 9193, AMERICAN ENERGY UTICA LLC |
| Change of Owner | 2015-06-19 | Operator changed from 9193, AMERICAN ENERGY UTICA LLC to 8799, GULFPORT ENERGY CORPORATION |
| Record Last Modified | 2015-09-24 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2012-09-26 | 10138 | 10288 | 55 |
| 2012-09-26 | 10890 | 11042 | 55 |
| 2012-09-26 | 10386 | 10542 | 55 |
| 11646 | 11798 | 55 | |
| 11394 | 11546 | 55 | |
| 11142 | 11294 | 55 | |
| 10890 | 11042 | 55 | |
| 10688 | 10790 | 44 | |
| 10386 | 10542 | 55 | |
| 10138 | 10288 | 55 | |
| 9882 | 10034 | 55 | |
| 9630 | 9786 | 55 | |
| 9381 | 9530 | 55 | |
| 9381 | 9530 | 55 | |
| 2012-09-26 | 9882 | 10034 | 55 |
| 2012-09-26 | 9381 | 9530 | 55 |
| 2012-09-26 | 9630 | 9786 | 55 |
| 2012-09-26 | 11394 | 11546 | 55 |
| 2012-09-26 | 11646 | 11798 | 55 |
| 2012-09-26 | 11142 | 11294 | 55 |
| 2012-09-26 | 10688 | 10790 | 44 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 0 | 0 | 0 |
For data sources see[4]
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2012 | HG ENERGY LLC | Brine | 4334 | 247 |
| 2013 | HG ENERGY LLC | Brine | 4343 | 31 |
| 2014 | AMERICAN ENERGY UTICA LLC | Brine | 17378 | 353 |
| 2015 | GULFPORT ENERGY CORPORATION | Brine | 2099 | 177 |
| 2016 | GULFPORT ENERGY CORPORATION | Brine | 2550 | 234 |
| 2017 | GULFPORT ENERGY CORPORATION | Brine | 2816 | 265 |
| 2018 | GULFPORT ENERGY CORPORATION | Brine | 2811 | 361 |
| 2019 | GULFPORT ENERGY CORPORATION | Brine | 840 | 86 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1717223427 | 2015-1-28 0:00: | DD | No Violations | |
| -2073344326 | 2015-1-28 0:00: | DD | No Violations | |
| -2144818464 | 2011-8-31 0:00: | SC | No Violations | 1.00 |
| -676857153 | 2020-6-8 0:00:0 | PW | No Violations | 1.00 |
| 0809512090 | 2015-06-18 | Production Wells | No Violations | Status check inspection found the well is in production with the production valves in the open position and 3 sets of 2-210 barrel production tanks on location in a plastic lined steel containment area supporting the said well along with the 5 other producing wells on location, there is also a total of 6 gas processing units on location supporting each well on the pad. Due to the recent rainfall standing water was found present on location and tested for chlorides with Low Level Quantab strip field strip tests finding no Chlorides on the entire location over 121 parts per million on this day. Also no sheen was observed as present. |
| 0887524019 | 2015-01-28 | Production Wells | No Violations | Administrative inspection to document the well drilling history. The said well was originally spudded as 3411124302-0000 and during the initial drilling process the well bore total drilling depth was reached but due to hole conditions the well bore collapsed before the drill string was pulled completely from the well bore and part of the drill string was left in the hole. The well bore bottom section was abandoned and plugged back to the vertical section and re permitted as 34111243020100 in which another well bore was lost once again and plugged back a 2nd time. A additional permit was issued as 34111243020200 in which the well bore was once again lost and plugged back into the vertical section for a 3rd time. A 4th permit was issued as 34111243020300 and the well was eventually completed as this API # and exists as producing today. I spoke with Steve Opritza in the Divisions Permitting section and he confirmed the well history as recorded to be accurate. |
| 1315490804 | 2011-09-06 | Drill / Deepen / Reopen | No Violations | On day of inspection I was accompanied by inspector Brett Farnsworth. Decker Rig 7 was on site and had completed the surface job on 09/05/2011. The rig was connecting their annular Blowout Preventer (BOP). The BOP was tested as well as the choke line. All pressure tests were successful. This rig is utilizing a closed loop system. |
| 1348324190 | 2013-12-11 | Production Wells | No Violations | The well drilling and stimulation process has been completed and the company is hooking up the completion testing equipment with the well being in production within 24 hours. |
| 1360677764 | 2013-02-12 | Production Wells | No Violations | Upon inspection of the tank battery site it was observed that the steel lined dike was standing full of what appeared to be rain water. Inspector made note of this to the company man on site and asked that the water be removed. Notification was also made to Josh Hinton, HGs operations manager. |
| 1381158295 | 2013-10-07 | Preliminary Restoration | No Violations | Preliminary Restoration found the wells on site all have been drilled and stimulated and the production equipment in place awaiting the gas processing transporting facility to begin purchasing the product. 6- 210 barrel storage tanks are on site in 2 tank individual containment areas, Proper well head identification is in place along with identification at the well site entry point. The site meets ORC 1509.072 regarding restoration. |
| 1422452285 | 2015-01-28 | Drill / Deepen / Reopen | No Violations | Administrative inspection to document the well drilling history. The said well was originally spudded as 3411124302-0000 and during the initial drilling process the well bore total drilling depth was reached but due to hole conditions the well bore collapsed before the drill string was pulled completely from the well bore and part of the drill string was left in the hole. The well bore bottom section was abandoned and plugged back to the vertical section and re permitted as 34111243020100 in which another well bore was lost once again and plugged back a 2nd time. A additional permit was issued as 34111243020200 in which the well bore was once again lost and plugged back into the vertical section for a 3rd time. A 4th permit was issued as 34111243020300 and the well was eventually completed as this API # and exists as producing today. I spoke with Steve Opritza in the Divisions Permitting section and he confirmed the well history as recorded to be accurate. |
| 1600192887 | 2013-02-13 | Production Wells | No Violations | Inspection of the well head found the well in production and selling gas off of the production tubing. 2-400 barrel production tanks are present in a man made dike area. Inspector will note that my request on 02-11-2013 to have the rain water removed from the dike impoundment has been meet and the dike is now empty. |
| 1717223427 | 2015-01-28 | Drill / Deepen / Reopen | No Violations | Administrative inspection to document the well drilling history. During the initial drilling process the well bore total drilling depth was reached but due to hole conditions the well bore collapsed before the drill string was pulled completely from the well bore and part of the drill string was left in the hole. The well bore bottom section was abandoned and plugged back to the vertical section and re permitted as 34111243020100 in which another well bore was lost once again and plugged back a 2nd time. A additional permit was issued as 341112430200 in which the well bore was once again lost and plugged back into the vertical section for a 3rd time. A 4th permit was issued as 34111243020300 and the well was eventually completed as this API # and exists as producing today. I spoke with Steve Opritza in the Divisions Permitting section and he confirmed the well history as recorded to be accurate. |
| 2073344326 | 2015-01-28 | Drill / Deepen / Reopen | No Violations | Administrative inspection to document the well drilling history. The said well was originally spudded as 3411124302-0000 and during the initial drilling process the well bore total drilling depth was reached but due to hole conditions the well bore collapsed before the drill string was pulled completely from the well bore and part of the drill string was left in the hole. The well bore bottom section was abandoned and plugged back to the vertical section and re permitted as 34111243020100 in which another well bore was lost once again and plugged back a 2nd time. A additional permit was issued as 34111243020200 in which the well bore was once again lost and plugged back into the vertical section for a 3rd time. A 4th permit was issued as 34111243020300 and the well was eventually completed as this API # and exists as producing today. I spoke with Steve Opritza in the Divisions Permitting section and he confirmed the well history as recorded to be accurate. |
| 2144818464 | 2011-08-31 | Surface Facility Construction | No Violations | On day of inspection I was accompanied by inspector Brett Farnsworth. Site construction is almost complete and Decker Rig 7 has started moving their equipment on site. |
| 809512090 | 2015-6-18 0:00: | PW | No Violations | 1.50 |
| 887524019 | 2015-1-28 0:00: | PW | No Violations |
For data sources see[7]