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| Well ID: 34-111-24305 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Monroe | |
| Municipality: Ohio Township | |
| Operator Name: STATOIL USA ONSHORE PROPERTIES | |
| Well Pad ID: US-OH-000783 | |
| Farm/Lease Name: DANGEL | |
| License Status: Plugged Back | |
| License Date: 2011-09-02 | |
| Spud Date: 2011-11-09 | |
| Spud Drilling Contractor: L WILSON DRLG | |
| Final Drill Date: 2012-01-18 | |
| Well Total Depth: 10980.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.670000 | |
| Longitude: -80.930000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2011-09-02 | Proposed Formations:BEREA THRU KNOX, Issued Date:9/2/2011, Expired Date:9/1/2013 12:00:00 PM, Drilling unit acres:156, Proposed Well Type:OG, Proposed Well Class:EDPW |
| Reached Total Depth | 2012-01-18 | |
| Completion Report Received | 2012-05-03 | |
| Change of Owner | 2012-12-26 | Operator changed from 8693, PROTEGE ENERGY II LLC to 9065, STATOIL USA ONSHORE PROP INC |
| Plugged Back | 2013-05-18 | |
| Construction Permit Expires | 2013-09-01 | |
| Record Last Modified | 2018-04-06 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2012-06-12 | 10716 | 10720 | 0 |
| 10716 | 10720 | 0 | |
| 10716 | 10720 | 0 |
For data sources see[3]
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2014 | STATOIL USA ONSHORE PROPERTIES | Brine | 3060 | 10 |
| 2015 | STATOIL USA ONSHORE PROPERTIES | Brine | 16422 | 204 |
| 2016 | STATOIL USA ONSHORE PROPERTIES | Brine | 6471 | 235 |
| 2017 | STATOIL USA ONSHORE PROPERTIES | Brine | 6708 | 365 |
| 2018 | EQUINOR USA ONSHORE PROPERTIES | Brine | 4270 | 345 |
| 2019 | EQUINOR USA ONSHORE PROPERTIES | Brine | 849 | 70 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1034745204 | 2013-5-15 0:00: | AM | No Violations | 1.00 |
| -1496686620 | 2012-8-20 0:00: | PL | No Violations | |
| -1551378329 | 2020-8-13 0:00: | PW | No Violations | 1.50 |
| -1635981385 | 2013-7-31 0:00: | DD | No Violations | 7.00 |
| -1929694370 | 2013-5-15 0:00: | PB | No Violations | 2.00 |
| -294244979 | 2019-1-28 0:00: | PW | No Violations | 0.10 |
| -489598037 | 2013-10-21 0:00 | DD | No Violations | 0.70 |
| -730585756 | 2013-5-16 0:00: | WR | No Violations | |
| -846062423 | 2013-5-30 0:00: | PB | No Violations | |
| 0294244979 | 2019-01-28 | Production Wells | No Violations | On this day, I found the pad gated with signage at the entrance. There are (7) producing wells, gas processing units, (6) 400-barrel steel production tanks within steel containment, (4) 30,000 gallon horizontal condensate pressure vessels in containment, and an Emergency Shutdown (ESD) button is present at the pad entrance. Concrete barriers surround the perimeter of the wellheads. Each well has identification and annular pressure monitoring devices equipped. The 9.625 inch diameter intermediate casing does not have a gauge, and the 13.375 inch diameter surface casing has a pressure of 0 psi. |
| 0489598037 | 2013-10-21 | Drill / Deepen / Reopen | No Violations | Notification was received from the company man on site over the past weekend that they had reached their total drilling depth at 11260 and are running and cementing the 5.5 production casing, upon inspection on this day the well bore drilling is complete and the rig is skidding to 3411124381-0000. |
| 0730585756 | 2013-05-16 | Work Over Reconditioning | No Violations | On this day I witnessed Mercer Well Svc rigged up on the hole attempting to drill out 3 composite plugs. Once the plugs are drilled out the Utica section shall be plugged back in order for the well to be completed in the Marcellus formation. The company man on site Rick Pace called later this day and indicated they will be ready to plug tomorrow at 12:00 pm. |
| 0846062423 | 2013-05-30 | Plug / Plug Back | No Violations | The company man Rick Pyles called at 4:45 pm and stated their first attempt to cut the casing at 3750 was unsuccessful and the pipe would not pull or circulate, I advised Him to keep moving up the hole and cutting the pipe until they reached a free point to recover the pipe and set their rip plug. |
| 0863928139 | 2012-12-20 | Production Wells | No Violations | On the day of my inspection the well was capable of production. No violations noted. |
| 0889083308 | 2013-10-21 | Drill / Deepen / Reopen | No Violations | Accompanied Inspector Bill Stolarik on inspection. Total depth at the time of inspection was 11260 ft. The hole was 8.5 in in diameter. Spoke with company men on site. |
| 1034745204 | 2013-05-15 | Administrative Inspection | No Violations | Rick Pyles of Stat Oil called on well about a Plug back job. The Utica perfs are at 10,716-10,720. The Marcellus perfs are at 6188-6191,6216-6219,6310-6313. The top of Cement is at 6170. The Top of the Kick plug will be at 3200-2400. |
| 1184151295 | 2012-11-30 | Production Wells | No Violations | Inspection of the site found the well completed and waiting on the sales transportation lines to be installed. |
| 1305665608 | 2013-05-30 | Plug / Plug Back | No Violations | Status check inspection on the company attempting to cut their 5.5 production casing at the top of the cement on the backside. The company was removing the BOP stack and would be several hours and would not be ready to cement until the next morning, The company man Rick Pyles will post me this evening of their progress. |
| 1337277576 | 2012-05-16 | Completion Testing | No Violations | On day of inspection well was fraced week prior and Weatherford was flowing back well for the company. |
| 1367517886 | 2013-05-02 | Plug / Plug Back | No Violations | Status check inspection on the plug back process. The company is testing the completed Utica formation and has Schulumberger completion and cementing service standing by on location. The company man will notify me when they are ready to set the bottom plug. |
| 1368576145 | 2013-05-14 | Work Over Reconditioning | No Violations | Status check inspection found Mercer Well Svc work over rig rigging up snubbing unit well head control and service related equipment preparing to set the Utica plug and pull the 5.5 production casing. |
| 1369143025 | 2013-05-18 | Plug / Plug Back | No Violations | On site inspection to witness the setting of the 2 bottom hole plugs over the Utica and Marcellus shale sections, Upon arrival the well bore production casing had 3500 psi on it and a 180 barrel 10.8# fluid pill was used to kill the well, Schlumberger well services are the cement contractors scheduled on location for 9:30 AM but did not arrive until 3:30 Pm, A 900 bottom hole plug was set and a 449 Marcellus plug was set from 6612 to 6163, with the intention of setting a cast iron bridge plug on top of the cement and ripping the pipe at the annular cement top and setting a 600 rip plug properly covering the Marcellus on the Annular of the 5.5 that did not have proper coverage on the initial well bore completion process. |
| 1369167747 | 2013-05-21 | Plug / Plug Back | No Violations | On this day we ran tubing and a tooth bit in to check the top plug set on 05/18/2013, The plug was to be set from 6612 to 6163. The plug was not in place or encountered. The company circulated the hole clean and shall place a cast iron bridge plug below the bottom perforation and will re cement this section accordingly. |
| 1369316877 | 2013-05-22 | Plug / Plug Back | No Violations | On site inspection to witness the plugging of the Marcellus formation, A cement plug was set inside of the 5.5 production covering a perforated section that was tested to check the Frack gradient, The plug was set from 6773 to 6163 and a cast iron bridge plug was set at 6160 at the approximate height of the cement on the backside of the 5.5 annular space. The casing will be shot off tomorrow just above the cast iron plug and a 400 cement rip plug shall be set to complete the Marcellus zonal isolation. |
| 1369702612 | 2013-05-23 | Plug / Plug Back | No Violations | On site inspection to witness the company attempting to cut the 5.5 production casing at the top of the cement above the Marcellus production zone. The service company was unable to pull stretch on the casing to get the casing out of the well head slips due to the casing being set in the slips 120,000 pounds over string weight by the drilling rig. The company continued to work on the project the next day with no success. |
| 1369833593 | 2013-05-28 | Plug / Plug Back | No Violations | Status check inspection on the plugging back of the Utica Formation. I will note that the Halliburton cement bond log that the company had on file showed a cement top on the backside of the 5.5 production casing at 6170 and this is the depth we have been working off of trying to cut the casing and isolate the top of the Marcellus. On this day Grey wire line company re-bond logged the well and found the cement top to be at approximately 3850. The company will run in the hole with tubing and finish setting the top of the Marcellus plug inside the 5.5 producing casing on 05/29/13 and then finish plugging the well accordingly. |
| 1369865532 | 2013-05-29 | Plug / Plug Back | No Violations | On site status check inspection to witness the setting of the plug inside of the 5.5 production casing on top of the Marcellus formation. Upon arrival I found that the rig crew had set the tubing string down in the last cement set in the casing plugging it up as not to allow circulation. The rig crew removed the plugged tubing joint and will run back in and set a 450 plug. |
| 1370016173 | 2013-05-31 | Plug / Plug Back | No Violations | Plugging inspection found the company trying to cut and pull the 5.5 production casing. The casing was cut with a jet cut wire line cutting tool at 3600 and a collar buster at 3422 with good telegraph to surface on both cuts but the casing will still not pull due to it being set in the slips by the drilling rig at 135,000# over string weight. A set of hydraulic casing jacks were brought in to try and lift the casing out of the slips. A mechanical plug was set at 3750. |
| 1370141807 | 2013-06-01 | Administrative Inspection | No Violations | I received phone notification from the company man on site Rick Pyles that they were able to free the 5.5 production casing from the well head slips with the assist from the casing jacks by lifting 400,000 pounds on the casing and pressuring 1100 psi on the annular on the casing. The company will try tomorrow to cut the casing again at 3422 with a collar buster explosive shot. |
| 1370306729 | 2013-06-03 | Plug / Plug Back | No Violations | On site inspection to witness the kick & rip plug being set on this day. The casing was ripped at 3422 and pulled out of the hole. 2.375 tubing was ran back in to a depth of 3433 and a cement plug set from 3433 to 2376. The well was circulated at 2376 and the plug shall be tagged tomorrow morning. |
| 1370392938 | 2013-06-04 | Plug / Plug Back | No Violations | On this day the rig crew ran in with tubing and tagged the top of the kick plug at 2400 and pressure tested the 9.625 casing at 2800 psi. |
| 1370445706 | 2013-06-05 | Plug / Plug Back | No Violations | The plug back is complete and the rig is rigging down and moving off the hole. The big rig is due in sometime in July. I reviewed the plug back records with Rick Pyles and confirmed that all records corresponded. |
| 1496686620 | 2012-08-20 | Preliminary Restoration | No Violations | On the day of my inspection the well site was restored in accordance with the preliminary restoration requirements. Preliminary restoration is now passed. |
| 1635981385 | 2013-07-31 | Drill / Deepen / Reopen | No Violations | |
| 1642064757 | 2015-01-14 | Preliminary Restoration | No Violations | Shale well preliminary restoration status check inspection found the said well has had the drilling and completion process completed and multiple wells are producing on the well pad with the following production related equipment in place on the location. There are 7 total wells on location each with individual gas processing units and a total of 4 -3,000 gallon 150 psi cylindrical vessels used for condensate along with 4-400 barrel production water tanks. Preliminary Restoration passed. |
| 1835808091 | 2013-05-17 | Plug / Plug Back | No Violations | 12:00 PM call out to begin plugging back the Completed Utica formation to complete the Marcellus section. Upon arrival the company man informed me that the job was postponed until tomorrow morning -Saturday 05/18/2013 @ 9:00Am, I contacted my supervisor and received permission to work a maximum of 8 hours overtime only. |
| 1929694370 | 2013-05-15 | Plug / Plug Back | No Violations | Status check inspection found Mercer Well Svc running tubing into the hole to drill out composite bridge plugs set during a Frac Gradient test. The current tubing depth is 6,000 with the 1st plug set @ 6,250. Once the plugs are removed the company will pull the tubing and remove the drill bit and run in open ended and set the bottom plug over the Utica formation and then plug the well back accordingly. |
| 1948458190 | 2013-05-08 | Work Over Reconditioning | No Violations | On site inspection found the company running in the hole with 1.250 coil tubing to a depth of 6,000 to try and make an attempt to kill the completed Utica formation in order to change out the production well head and replace it with a completion well head. |
| 2035963821 | 2013-10-15 | Drill / Deepen / Reopen | No Violations | Status check inspection of the current drilling progress found the current drilling depth to be 5781 with a TVD of 5685 using a 8.5 directional drilling tool with a current curve being built at 16 degrees with a Azimuth of 175 degrees. Pressure test of the 9.625 previous casing string was done on 10/14/13 to a pressure of 2800 psi with no recorded loss, A formation leak off and integrity test was also done and recorded. |
| 863928139 | 2012-12-20 0:00 | PW | No Violations | 0.50 |
| 889083308 | 2013-10-21 0:00 | DD | No Violations | 1.50 |
For data sources see[6]