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Well ID: 34-111-24314 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Wayne Township | |
Operator Name: PROFIT ENERGY COMPANY | |
Well Pad ID: | |
Farm/Lease Name: CYSSR LAND HOLDINGS | |
License Status: Producing | |
License Date: 2011-12-19 | |
Spud Date: 2012-12-21 | |
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC | |
Final Drill Date: 2011-12-27 | |
Well Total Depth: 1830.00 ft | |
Configuration: Vertical | |
Latitude: 39.700000 | |
Longitude: -81.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-12-19 | Proposed Formations:KEENER-BEREA, Issued Date:12/19/2011, Expired Date:12/18/2013 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2011-12-27 | |
Correction to Well | 2011-12-30 | ADDED FOOTAGE |
Completion Report Received | 2012-04-05 | |
Correction to Well | 2012-05-04 | CORRECTION TO PROPOSED GEOLOGICAL FORMATION |
Construction Permit Expires | 2013-12-18 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2012-04-13 | 740 | 750 | 0 |
2012-04-13 | 514 | 520 | 0 |
740 | 750 | 0 | |
514 | 520 | 0 | |
1240 | 1250 | 0 | |
1806 | 1814 | 0 | |
514 | 520 | 0 | |
2012-04-13 | 1806 | 1814 | 0 |
2012-04-13 | 1240 | 1250 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Other Treatment Type | 0 | 0 | 0 | 4 GAS GUNS |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | PROFIT ENERGY COMPANY | 0.00 | 0.00 | 365 |
2012 | PROFIT ENERGY COMPANY | 410.00 | 0.00 | 341 |
2013 | PROFIT ENERGY COMPANY | 1006.00 | 0.00 | 365 |
2014 | PROFIT ENERGY COMPANY | 407.00 | 14.00 | 365 |
2015 | PROFIT ENERGY COMPANY | 289.00 | 17.00 | 365 |
2016 | PROFIT ENERGY COMPANY | 256.00 | 48.00 | 365 |
2017 | PROFIT ENERGY COMPANY | 211.00 | 17.00 | 365 |
2018 | PROFIT ENERGY COMPANY | 213.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | PROFIT ENERGY COMPANY | Brine | 130 | 365 |
2012 | PROFIT ENERGY COMPANY | Brine | 130 | 341 |
2013 | PROFIT ENERGY COMPANY | Brine | 248 | 365 |
2014 | PROFIT ENERGY COMPANY | Brine | 72 | 365 |
2015 | PROFIT ENERGY COMPANY | Brine | 72 | 365 |
2016 | PROFIT ENERGY COMPANY | Brine | 57 | 365 |
2017 | PROFIT ENERGY COMPANY | Brine | 71 | 365 |
2018 | PROFIT ENERGY COMPANY | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2127592715 | 2012-8-29 0:00: | WR | No Violations | |
0437151723 | 2016-04-06 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection found the well site meets ORC 1509.072 with erosion control and vegetation established. Addressing the well head- the well is equipped 4.5 production casing 1.5 production tubing and pumping rods with the production valves open and the well set up to be produced by the means of a pumping unit. At the production facility a single 100 barrel production tank is present along with a mechanical separator and gas sales meter all located inside an established dike area with well identification posted. |
1263375805 | 2012-11-05 | Production Wells | No Violations | Status check found the well has been put back into production and the site reclaimed after previous work over procedures being completed this year. |
1345496726 | 2012-08-20 | Drill / Deepen / Reopen | No Violations | Inspector stopped by well site 2 times today to check on status on work over procedure .Monroe drilling rig on hole. Production casing along with production casing packer was pulled out of hole in order to clean out borehole, parts of the packer system failed to come out and leaving debris in the hole. Inspector did suggest to company that they increase the capacity of their work over pit. |
1345558975 | 2012-08-21 | Drill / Deepen / Reopen | No Violations | Inspector on site to review intended work over process. Spoke with Kerry Brown from Monroe drilling and discussed their intended procedure. Well up date work is as follows , 8-20-12, 706 of 4.5 casing along with formation packer was pulled out of hole, with the packer rubber and 2 of the packer slips being lost in hole, a magnet was run in hole on 8-21 in attempt to retrieve slips with no success . Rig crew now running in hole with drill bit and drill string in attempt to drill up debris from packer, remove down hole bridge and run to original TD of 1830. Inspector advised them that a variance was needed on original permit if well bore was going to be deepened and if they were working off the original un expired permit it must be on location . Inspector also noted that secondary pit was advised to be put in place due to close proximity to a fresh water spring holding tank, which is within 125 of well head. |
2127592715 | 2012-08-29 | Work Over Reconditioning | No Violations | Status check on well site and update on work over . Well had 700 of 4.5casing set on a packer. The string was pulled out of the hole and Monroe drilling attempted to get back down the bore hole to the original TD. When the packer was pulled out both the rubber and 2 of the slips were left in the hole plus the bore hole has collapsed down hole. They were able to make hole down to 900. |
437151723 | 2016-4-6 0:00:0 | PL | No Violations | 1.10 |
773829108 | 2020-6-25 0:00: | PW | No Violations | 0.80 |
For data sources see[9]