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34-111-24314

Well Details

Well ID: 34-111-24314
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Country: United States
State: Ohio
County: Monroe
Municipality: Wayne Township
Operator Name: PROFIT ENERGY COMPANY
Well Pad ID:
Farm/Lease Name: CYSSR LAND HOLDINGS
License Status: Producing
License Date: 2011-12-19
Spud Date: 2012-12-21
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC
Final Drill Date: 2011-12-27
Well Total Depth: 1830.00 ft
Configuration: Vertical
Latitude: 39.700000
Longitude: -81.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-12-19 Proposed Formations:KEENER-BEREA, Issued Date:12/19/2011, Expired Date:12/18/2013 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2011-12-27
Correction to Well 2011-12-30 ADDED FOOTAGE
Completion Report Received 2012-04-05
Correction to Well 2012-05-04 CORRECTION TO PROPOSED GEOLOGICAL FORMATION
Construction Permit Expires 2013-12-18
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2012-04-13 740 750 0
2012-04-13 514 520 0
740 750 0
514 520 0
1240 1250 0
1806 1814 0
514 520 0
2012-04-13 1806 1814 0
2012-04-13 1240 1250 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Other Treatment Type 0 0 0 4 GAS GUNS

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 PROFIT ENERGY COMPANY 0.00 0.00 365
2012 PROFIT ENERGY COMPANY 410.00 0.00 341
2013 PROFIT ENERGY COMPANY 1006.00 0.00 365
2014 PROFIT ENERGY COMPANY 407.00 14.00 365
2015 PROFIT ENERGY COMPANY 289.00 17.00 365
2016 PROFIT ENERGY COMPANY 256.00 48.00 365
2017 PROFIT ENERGY COMPANY 211.00 17.00 365
2018 PROFIT ENERGY COMPANY 213.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 PROFIT ENERGY COMPANY Brine 130 365
2012 PROFIT ENERGY COMPANY Brine 130 341
2013 PROFIT ENERGY COMPANY Brine 248 365
2014 PROFIT ENERGY COMPANY Brine 72 365
2015 PROFIT ENERGY COMPANY Brine 72 365
2016 PROFIT ENERGY COMPANY Brine 57 365
2017 PROFIT ENERGY COMPANY Brine 71 365
2018 PROFIT ENERGY COMPANY Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2127592715 2012-8-29 0:00: WR No Violations
0437151723 2016-04-06 Preliminary Restoration No Violations Preliminary Restoration status check inspection found the well site meets ORC 1509.072 with erosion control and vegetation established. Addressing the well head- the well is equipped 4.5 production casing 1.5 production tubing and pumping rods with the production valves open and the well set up to be produced by the means of a pumping unit. At the production facility a single 100 barrel production tank is present along with a mechanical separator and gas sales meter all located inside an established dike area with well identification posted.
1263375805 2012-11-05 Production Wells No Violations Status check found the well has been put back into production and the site reclaimed after previous work over procedures being completed this year.
1345496726 2012-08-20 Drill / Deepen / Reopen No Violations Inspector stopped by well site 2 times today to check on status on work over procedure .Monroe drilling rig on hole. Production casing along with production casing packer was pulled out of hole in order to clean out borehole, parts of the packer system failed to come out and leaving debris in the hole. Inspector did suggest to company that they increase the capacity of their work over pit.
1345558975 2012-08-21 Drill / Deepen / Reopen No Violations Inspector on site to review intended work over process. Spoke with Kerry Brown from Monroe drilling and discussed their intended procedure. Well up date work is as follows , 8-20-12, 706 of 4.5 casing along with formation packer was pulled out of hole, with the packer rubber and 2 of the packer slips being lost in hole, a magnet was run in hole on 8-21 in attempt to retrieve slips with no success . Rig crew now running in hole with drill bit and drill string in attempt to drill up debris from packer, remove down hole bridge and run to original TD of 1830. Inspector advised them that a variance was needed on original permit if well bore was going to be deepened and if they were working off the original un expired permit it must be on location . Inspector also noted that secondary pit was advised to be put in place due to close proximity to a fresh water spring holding tank, which is within 125 of well head.
2127592715 2012-08-29 Work Over Reconditioning No Violations Status check on well site and update on work over . Well had 700 of 4.5casing set on a packer. The string was pulled out of the hole and Monroe drilling attempted to get back down the bore hole to the original TD. When the packer was pulled out both the rubber and 2 of the slips were left in the hole plus the bore hole has collapsed down hole. They were able to make hole down to 900.
437151723 2016-4-6 0:00:0 PL No Violations 1.10
773829108 2020-6-25 0:00: PW No Violations 0.80

For data sources see[9]

References