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Well ID: 34-111-24330 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Washington Township | |
Operator Name: GULFPORT APPALACHIA LLC | |
Well Pad ID: US-OH-000470 | |
Farm/Lease Name: WHITACRE ENTERPRISES INC | |
License Status: Producing | |
License Date: 2012-04-05 | |
Spud Date: 2012-04-02 | |
Spud Drilling Contractor: DALLAS MORRIS | |
Final Drill Date: 2013-04-26 | |
Well Total Depth: 15314.00 ft | |
Configuration: Horizontal | |
Latitude: 39.660000 | |
Longitude: -81.200000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2012-04-05 | Proposed Formations:UTICA SHALE, Issued Date:4/5/2012, Expired Date:4/5/2014 12:00:00 PM, Drilling unit acres:558, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2013-04-26 | |
Construction Permit Expires | 2014-04-05 | |
Change of Owner | 2015-02-25 | Operator changed from 8793, HG ENERGY LLC to 9193, AMERICAN ENERGY UTICA LLC |
Completion Report Received | 2015-05-01 | |
Change of Owner | 2015-06-19 | Operator changed from 9193, AMERICAN ENERGY UTICA LLC to 8799, GULFPORT ENERGY CORPORATION |
Record Last Modified | 2018-02-27 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2013-05-17 | H2O | 15 | 8610 Bbl | 4500 | Producers Service Corporation | stge 6, 60 shots |
2013-05-20 | H2O | 15 | 8523 Bbl | 450000 | Producers Service Corporation | stage 7, 60 shots |
2013-05-23 | H2O | 15 | 8787 Bbl | 450000 | Producers Service Corporation | stage 9, 60 shots |
2013-06-01 | H2O | 15 | 8187 Bbl | 450000 | Producers Service Corporation | stage 15, 60 shots |
2013-05-13 | H2O | 15 | 9155 Bbl | 450000 | Producers Service Corporation | stage 2, 60 shots |
2013-06-04 | H2O | 15 | 8634 Bbl | 450000 | Producers Service Corporation | stage 17, 60 shots |
2013-05-15 | H2O | 15 | 8320 Bbl | 440000 | Producers Service Corporation | stage 4, 60 shots |
2013-05-14 | H2O | 15 | 8932 Bbl | 450000 | Producers Service Corporation | stage 3, 60 shots |
2013-05-09 | H2O | 15 | 7696 Bbl | 352800 | Producers Service Corporation | stage 1 |
2013-06-05 | H2O | 15 | 8094 Bbl | 450000 | Producers Service Corporation | stage 18, 60 shots |
2013-05-31 | H2O | 15 | 8334 Bbl | 450000 | Producers Service Corporation | stage 14, 60 shots |
2013-06-03 | H2O | 15 | 8590 Bbl | 450000 | Producers Service Corporation | stage 16, 60 shots |
2013-05-21 | H2O | 15 | 8131 Bbl | 450000 | Producers Service Corporation | stage 8, 60 shots |
2013-05-24 | H2O | 15 | 8362 Bbl | 450000 | Producers Service Corporation | stage 10, 60 shots |
2013-05-29 | H2O | 15 | 7965 Bbl | 450000 | Producers Service Corporation | stage 12, 60 shots |
2013-05-28 | H2O | 15 | 9116 Bbl | 450000 | Producers Service Corporation | stage 11, 60 shots |
2013-05-30 | H2O | 15 | 8610 Bbl | 450000 | Producers Service Corporation | stage 13, 60 shots |
2013-05-16 | H2O | 15 | 8263 Bbl | 450000 | Producers Service Corporation | stage 5, 60 shots |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2013 | HG ENERGY LLC | 145278 | 0 | 31 |
2014 | AMERICAN ENERGY UTICA LLC | 795656 | 0 | 343 |
2015 | GULFPORT ENERGY CORPORATION | 343984 | 0 | 262 |
2016 | GULFPORT ENERGY CORPORATION | 198739 | 0 | 241 |
2017 | GULFPORT ENERGY CORPORATION | 228249 | 0 | 269 |
2018 | GULFPORT ENERGY CORPORATION | 217729 | 0 | 360 |
2019 | GULFPORT ENERGY CORPORATION | 52302 | 0 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2013 | HG ENERGY LLC | Brine | 7754 | 31 |
2014 | AMERICAN ENERGY UTICA LLC | Brine | 23701 | 343 |
2015 | GULFPORT ENERGY CORPORATION | Brine | 2981 | 231 |
2016 | GULFPORT ENERGY CORPORATION | Brine | 2655 | 241 |
2017 | GULFPORT ENERGY CORPORATION | Brine | 6251 | 269 |
2018 | GULFPORT ENERGY CORPORATION | Brine | 5799 | 360 |
2019 | GULFPORT ENERGY CORPORATION | Brine | 1380 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1124816266 | 2020-6-8 0:00:0 | PW | No Violations | 1.00 |
-1991311909 | 2013-4-22 0:00: | DD | No Violations | |
-222155089 | 2013-1-28 0:00: | DD | No Violations | |
-585689935 | 2013-4-18 0:00: | DD | No Violations | 0.70 |
-990263768 | 2013-2-5 0:00:0 | DD | No Violations | |
0222155089 | 2013-01-28 | Drill / Deepen / Reopen | No Violations | Inspector on site for a status update found the company rigging up Dallas Morris rig #24 to begin completing the drilling process. Company records show the well was spudded on 04/02/12 and 80 of 20 conductor was set with no annular space. |
0301896590 | 2013-10-07 | Production Wells | No Violations | Preliminary Restoration found the wells on site all have been drilled and stimulated and the production equipment in place awaiting the gas processing transporting facility to begin purchasing the product. 6- 210 barrel storage tanks are on site in 2 tank individual containment areas, Proper well head identification is in place along with identification at the well site entry point. The site meets ORC 1509.072 regarding restoration. |
0456778647 | 2015-06-18 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection found the well is in production with the production valves in the open position and 3 sets of 2-210 barrel production tanks on location in a plastic lined steel containment area supporting the said well along with the 5 other producing wells on location, there is also a total of 6 gas processing units on location supporting each well on the pad. Due to the recent rainfall standing water was found present on location and tested for chlorides with Low Level Quantab strip field strip tests finding no Chlorides on the entire location over 121 parts per million on this day. Also no sheen was observed as present. Under ORC 1509.072 the Preliminary Restoration was passed on this day with vegetation established in the area affected by the initial well pad construction and erosion control in place. |
0585689935 | 2013-04-18 | Drill / Deepen / Reopen | No Violations | Status check inspection of the current drilling progress found the current drilling depth to be 8441 using a 8.5 drill bit and drilling with oil based drilling fluid. The current bore hole position is just starting into the horizontal curve. |
0990263768 | 2013-02-05 | Drill / Deepen / Reopen | No Violations | Notification was received that the current drilling depth of 1200 has been reached and upon pulling out of the hole with the drill string it was discovered that the hammer drill bit cutting head had twisted off and has been lost in the borehole. The company man noted that the bit recovery process would begin later this morning and that He would keep me posted on the recovery process. |
1168340280 | 2014-05-31 | Casing String Witnessed | No Violations | On 05/31/2013 Decker drilling rig 10 is now on the hole and has drilled a 17.5 surface borehole to a depth of 1,085 with 1,071 of 13.375 surface pipe ran and cemented by Baker Hughes using 850 sacks of class A .25 pound per sack flake, .5% calcium and 35 barrels of cement returns to surface with the casing being pressure tested to 845 psi. |
1360192490 | 2013-02-06 | Drill / Deepen / Reopen | No Violations | Notification was received @ 9:07 Am from Josh Hinton from HG energy that the surface bore hole was loaded with A 500 barrel mix of brine water and other hole conditioning material. Josh indicated that did not realize their mistake until after they had completed the process of trying to retrieve the lost cutting head off of the hammer bit and stabilize the bore hole. I immediately made notification to my supervisor Rocky King and MRI 3 over the regions drilling and plugging Pat Shreve and the decision was made to allow the company to continue running the surface casing into the bore hole and then circulate the unwanted fluid out of the hole. A full description and amount of the fluids introduced into the well bore was received. Inspector will note that I was on site through out the entire running of the casing; circulation of the mud flush and cementing procedures. The drilling permit was issued 04/05/2012. |
1360597888 | 2013-02-11 | Drill / Deepen / Reopen | No Violations | Upon inspection the current drilling depth was found to be 1267 using a 12.250 bit. A 17.5 bit was lost at 1247 and was tagged at 1224 with the bottom of the surface set on top of the lost tool at 1140. The borehole below the surface then was cemented with 200 sacks of type 1 cement. The company allowed the cement to set and then went back to drilling and deviated the borehole around the lost bit. |
1360956856 | 2013-02-15 | Drill / Deepen / Reopen | No Violations | Inspection and update on the drilling status found the current drilling depth to be 5596 using a 12.250 bit with a proposed Total Depth for this current intermediate string of 8350. The rig is drilling on air. |
1361285953 | 2013-02-19 | Drill / Deepen / Reopen | No Violations | Status check inspection on the drilling progress found the current drilling depth to be 8279 using a 12.250 drill bit, with the projected total drilling depth of 8345 on this current segment of the well bore. Company man stated they should start running the 2 stage 9.625 casing string by tomorrow morning. |
1361497346 | 2013-02-21 | Drill / Deepen / Reopen | No Violations | Inspector on site from 7AM until 3:30 PM to witness the cementing of 8273 of 9.625 casing in a 2 stage process with 30 % cement excess ran on both stages and the 2 stage tool set at 5448. A copy of the casing tally and cement job tickets was received. |
1361547200 | 2013-02-22 | Drill / Deepen / Reopen | No Violations | Status update inspection to document that the 9.625 has been set at a depth of 8273 and the rig has skidded over to the #3H well API # 3411124322. |
1367283430 | 2013-04-29 | Casing String Witnessed | No Violations | I received notification of the completion of the drilling process and the running and cementing of the production casing on the weekend of 04/27 & 04/28 2013. On 04/ 29/ 13 I picked up the casing and cement records and completed the casing report in the database. The company also informed me on this day that the well stimulation process would begin immediately on the 5 completed wells on this drilling pad. |
1367536262 | 2013-05-02 | Drill / Deepen / Reopen | No Violations | On this day whil doing a site inspection I observed the well bubbiling between the 13.375 and the 9.625 casing strings. My completion records showed that we bond logged the 9.625 casing cement job due to no cement returns with the bond log showing the cement top at 200 from surface and the bottom of the 13.375 at 1247. We will continue to monitor and access the situation. |
1367863593 | 2013-05-06 | Drill / Deepen / Reopen | No Violations | Status check inspection in regards to the well communicating between the 13.375 and 9.625 casing found the well control has been implemented and is in place. |
1991311909 | 2013-04-22 | Drill / Deepen / Reopen | No Violations | Status check inspection on the current drilling progress found the current drilling depth to be 13,643 in the horizontal bore hole using a 8.5 drill bit. |
301896590 | 2013-10-7 0:00: | PW | No Violations | 2.30 |
456778647 | 2015-6-18 0:00: | PL | No Violations | 1.50 |
For data sources see[8]