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| Well ID: 34-111-24653 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Monroe | |
| Municipality: Wayne Township | |
| Operator Name: GULFPORT APPALACHIA LLC | |
| Well Pad ID: US-OH-001066 | |
| Farm/Lease Name: ROGER 210596 | |
| License Status: Producing | |
| License Date: 2016-03-10 | |
| Spud Date: 2016-03-17 | |
| Spud Drilling Contractor: NOMAC DRILLING CORP | |
| Final Drill Date: 2016-07-20 | |
| Well Total Depth: 18065.00 ft | |
| Configuration: Horizontal | |
| Latitude: 39.700000 | |
| Longitude: -81.180000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2016-03-10 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:3/10/2016, Expired Date:3/10/2018 12:00:00 PM, Drilling unit acres:606.534, Proposed Well Type:OG, Proposed Well Class:EOUT |
| Reached Total Depth | 2016-07-20 | PR STATUS BASED ON 2Q PRODUCTION REPORTED...SO |
| Correction to Well | 2016-07-22 | CORRECTION TO TAKE-POINT INFORAMTION (FOOTAGE AND COORDINATES). |
| Correction to Well | 2017-03-24 | UPDATE TARGET/TAKEPOINT PER AS-DRILLED PLAT-RC |
| Record Last Modified | 2017-11-21 | PR STATUS BASED ON 2Q PRODUCTION REPORTED...SO |
| Correction to Well | 2017-12-29 | UPDATE TAKE PER FINAL AS-DRILLED PLAT |
| Construction Permit Expires | 2018-03-10 | PR STATUS BASED ON 2Q PRODUCTION REPORTED...SO |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2017-11-20 | 9664 | 9808 | 50 |
| 2017-11-20 | 17759 | 17905 | 50 |
| 17759 | 17905 | 50 | |
| 9664 | 9808 | 50 | |
| 9664 | 9808 | 50 |
For data sources see[3]
| Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
|---|---|---|---|---|---|
| 1 | 01/07/2017 | 02/25/2017 | 9135 | 8,785,060.0 | 0 |
| Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
|---|---|---|---|---|---|---|---|---|
| 1 | NEFE-180 | Chemplex | Corrosion Inhibitor/Iron Control | Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00006880 | 57.418 |
| Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00006880 | 57.418 | ||||
| Methanol | 67-56-1 | 35 | 0.000481594 | 401.924 | ||||
| Olefin | Proprietary | 5 | 0.00006880 | 57.418 | ||||
| 2-Propyn-1-ol | 107-19-7 | 5 | 0.00006880 | 57.418 | ||||
| Acetic acid | 64-19-7 | 65 | 0.000894389 | 746.431 | ||||
| Fatty acids, tall oil | 61790-12-3 | 5 | 0.00006880 | 57.418 | ||||
| 2-Ethylhexanol | 104-76-7 | 10 | 0.000137598 | 114.836 | ||||
| Hydrochloric Acid (28%) | Oxy | Acidizing | Water | 7732-18-5 | 64 | 0.133149 | 111122 | |
| Hydrochloric Acid (Hydrogen Chloride) | 7732-18-5 | 36 | 0.0748961 | 62506.1 | ||||
| Bio B2512 | Lubrizol | Biocide | Water | 7732-18-5 | 90 | 0.0311504 | 25997.2 | |
| 2,2-Dibromo-3-nitrilopropionamide | 10222-01-2 | 10 | 0.00346116 | 2888.58 | ||||
| Sand (100 Mesh Proppant) | Taylor Frac | Proppant | Silica Substrate | 14808-60-7 | 100 | 1.17368 | 979520 | |
| Water | Gulfport Energy | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 87.8431 | 73,311,300.0 | |
| Sand (40/70 White Proppant) | Taylor Frac | Proppant | Silica Substrate | 14808-60-7 | 100 | 10.6392 | 8,879,200.0 | |
| FRA-409 | Lubrizol | Friction Reducer | Water | 7732-18-5 | 70 | 0.0589053 | 49160.6 | |
| Distillates, Petroleum, Hydrotreated Light | 64742-47-8 | 30 | 0.0252451 | 21068.8 | ||||
| SI-20W | Stingray Pressure Pumping, LLC | Scale Inhibitor | Phosphinocarboxylic Acid | 110224-99-2 | 45 | 0.00709432 | 5920.72 | |
| Water | 7732-18-5 | 55 | 0.00867084 | 7236.43 | ||||
| Other Chemical(s) | Listed Above | See Trade Name(s) List | Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00006880 | 57.418 | |
| 2-Ethylhexanol | 104-76-7 | 10 | 0.000137598 | 114.836 | ||||
| Water | 7732-18-5 | 64 | 0.133149 | 111122 | ||||
| Methanol | 67-56-1 | 35 | 0.000481594 | 401.924 | ||||
| 2-Propyn-1-ol | 107-19-7 | 5 | 0.00006880 | 57.418 | ||||
| Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00006880 | 57.418 | ||||
| Fatty acids, tall oil | 61790-12-3 | 5 | 0.00006880 | 57.418 | ||||
| Water | 7732-18-5 | 90 | 0.0311504 | 25997.2 | ||||
| Water | 7732-18-5 | 70 | 0.0589053 | 49160.6 | ||||
| Olefin | Proprietary | 5 | 0.00006880 | 57.418 | ||||
| Water | 7732-18-5 | 55 | 0.00867084 | 7236.43 |
For data sources see[4]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 2017-02-24 | H2O | 15 | 241962 Gal | 2777323 | STINGRAY PRESSURE PUMPING LLC | STAGE 35/35
STAGES 2-34 SEE IMAGES |
| 2017-01-06 | H2O | 15 | 41748 Gal | 255813 | STINGRAY PRESSURE PUMPING LLC | STAGE 1/35
STAGES 2-34 SEE IMAGES |
For data sources see[5]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2017 | GULFPORT ENERGY CORPORATION | 2279794 | 0 | 268 |
| 2018 | GULFPORT ENERGY CORPORATION | 1114170 | 0 | 364 |
| 2019 | GULFPORT ENERGY CORPORATION | 184687 | 0 | 90 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2017 | GULFPORT ENERGY CORPORATION | Brine | 44247 | 268 |
| 2018 | GULFPORT ENERGY CORPORATION | Brine | 13715 | 364 |
| 2019 | GULFPORT ENERGY CORPORATION | Brine | 2379 | 90 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1249830674 | 2016-7-12 0:00: | PB | No Violations | |
| -1553715052 | 2016-9-7 0:00:0 | DD | No Violations | 2.00 |
| -1707165262 | 2016-8-16 0:00: | DD | No Violations | 2.50 |
| -1848929064 | 2016-11-7 0:00: | PL | No Violations | 0.50 |
| -2145465844 | 2017-3-6 0:00:0 | PL | No Violations | 0.50 |
| -521022096 | 2016-3-17 0:00: | CS | No Violations | |
| -770601048 | 2017-6-27 0:00: | PL | No Violations | 0.20 |
| -826274655 | 2018-3-15 0:00: | PW | No Violations | 0.20 |
| 0521022096 | 2016-03-17 | Casing String Witnessed | No Violations | The said well was spudded on 03/17/2016 with a 110 x 36 conductor borehole being drilled by Butches Rat Hole Service and -110 of 26 .375 wall-weld connection conductor pipe was set and cemented by Stingray Cement Service using 490 sacks of Class A cement with 2% calcium and .125 lb/sk lcm additives, with 15 barrels of 6% gel space ran ahead. Circulation was established prior to cementing and maintained throughout the job with cement being displaced with 62 barrels of fresh water and cement returns witnessed to surface. |
| 0574855393 | 2016-07-11 | Drill / Deepen / Reopen | No Violations | My inspection today finds the well is shut in and the casing pressure is being monitored and currently sets at 1690 psi . The rig recently pumped a 93 barrel Hydro-plug Halliburton lost circulation material pill and are waiting for the pill to seal the lost circulation zone. On July 7 the company experienced a 12 barrel kick. While trying to circulate the gas out a lost circulation zone was encountered and to date 2500 barrels of mud have been lost. No annular pressure has been noted. |
| 0640416410 | 2016-07-14 | Drill / Deepen / Reopen | No Violations | Status check inspection on the well drilling process found Nomac Rig # 83 on the well. The company is currently attempting to recover their 5 drill string from the well bore that became stuck after a cement squeeze job was attempted on 07/12/2016. The drill string and bottom hole assembly is positioned in the well bore at 7,082 and KLX Energy pipe recovery service is on location and has successfully severed the 5 drill string at 6,912. The company plans on running in the hole and setting a mechanical bridge plug above the top od the drill string in the hole. The company will propose and submit a plan to the Division to be approved by the Division Management before proceeding with the well bore drilling. |
| 0770601048 | 2017-06-27 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection found the area affected by the well site construction has vegetation established and erosion control in place and is in compliance with ORC 1509.072. Addressing the well site. There is 6 producing wells on the pad all in line and selling product with tubing well heads installed on each well and the production valves in the open position. The wells are selling into gas processing units (GPU) with (6) units present. Also on the well site is the production fluid storage facility consisting of (4) steel production tanks all located inside a polymer lined steel containment dike area. The company has installed electrically controlled emergency shut down devices at each well head and also at the production facility and the well pad entrance. Located along the well site entrance lease road is a mid stream operation owned by Rice Energy in which all the wells on the pad sell into. Signage is posted at the well pad entrance and at each well head. |
| 0826274655 | 2018-03-15 | Production Wells | No Violations | On this day, I found the well equipped with annular pressure monitoring devices. The pressure gauges are labeled with surface pressure reading 0 pounds per square inch, and the intermediate gauge reading 1,100 pounds per square inch. There are (6) total wellheads, all in production, with concrete barriers surrounding them, and an electronic shutdown button at each wellhead. The facility is gated with proper signage, and an electronic shutdown button on the left-side, prior to the pad. The back right-side of the pad is equipped with (4) 400 barrel steel tanks and (1) 50 barrel steel tank all within containment, and an electronic shutdown button is present. There are (6) gas processing units along the right-side of the pad with electronic shutdown buttons on each, and a midstream facility on the right, at the entrance. |
| 0857105774 | 2016-06-08 | Drill / Deepen / Reopen | No Violations | |
| 1015024663 | 2017-03-06 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection accompanied by ODNR Inspector Austin Gutridge. The area affected by the well pad construction meets ORC 1509.072 with vegetation established and erosion control in place. The lease road is stoned and in good repair. Signage is posted at the well pad entrance. Hybrid Services completion rig # 102 is on location drilling out the completion plugs on the Roger # 4-A well. The rig is situated on polymer containment with the well pad perimeter earthen berm serving as the primary containment with the pad drain valves closed. There is 6 total wells on the pad that have been drilled and stimulated that will now be completed and the initial flow back operations commenced. |
| 1033365128 | 2016-07-07 | Drill / Deepen / Reopen | No Violations | |
| 1226503824 | 2017-03-06 | Completion Testing | No Violations | On the day of my inspection accompanied by ODNR Inspector Pat Shreve, I met with Gulfport Consultant David Wade and Completions Superintendent Bello Kellum. Hybrid Drilling Rig had just drilled out the last frac plug, abandoned their drill out bit and motor. Hybrid Drilling Rig will circulate the wellbore clean, trip out to 6400 feet; install the remainder of the 2.375 inch diameter production tubing and trip back in landing the tubing at 9375 feet and 75 degrees in the curve. |
| 1249830674 | 2016-07-12 | Plug / Plug Back | No Violations | Status check inspection on the current well drilling process found Nomac Drilling rig # 83 on the well bore and currently attempting to drill the 8.5 production borehole at a measured depth of 9,849, the company experienced an over pressurization of the well bore from a high influx of 3rd party gas from the well bore and is currently circulation through the Blow Out Preventer choke manifold and fairing the 3900 units of gas. The drill string is setting at 7,059 and the rig is circulating 14.3 lb/gl synthetic oil based drilling mud at a rate of 6 barrels a minute, at this rate the well bore is holding a constant fluid volume and not taking or making fluid. The company did set their 9.625intermediate casing at a measured depth of 7,959 and the Queenstown formation top is at 7,585 True vertical depth with the Reedsville at 8,075 TVD and Utica following at 8,924 TVD. The company has indicated the well bore has a loss circulation area believed to be in the Queenstown formation and they have proposed to spot a 115 barrel cement plug into the well bore through the drill string in anticipation of isolation the loss circulation area. No annular pressure is present on the 9.625 intermediate casing string. |
| 1468605728 | 2016-07-15 | Drill / Deepen / Reopen | No Violations | On site inspection to verify the well bore pressure status. Upon inspection it was observed that Nomac Drilling rig 83 was on the hole and KLX Energys pipe recover back off truck had once again attempted to separate the drill string at a measured depth of 6,810, the drill string showed separation at the drill joint by means of the wire line collar locator. The drilling rig then proceeded to recover (2) drill stands measuring 95 in length from the well bore, putting the bottom of the drill string recovered at 6,620. The rig then proceeded to circulate the well bore using 14.4 lb/gl synthetic based drilling mud at a rate of 7 strokes per minute carrying a volume of .0692 bbl. per stroke, at 5000 strokes into displacement (bottoms up) the 3rd party gas was showing at 3,200 units with the annular valves standing open and not circulating through the choke manifold. At the time of my report the circulation cycle was at 6,094 strokes and the 3rd party gas was at 4,069 units. The company man on site reported they had circulated bottoms up multiple times the previous day from 6,283 to surface. The company had shut the well bore in to repair the gas buster flair system. |
| 1469109268 | 2016-07-21 | Drill / Deepen / Reopen | No Violations | Status check inspection on the well drilling process found Nomac Rig # 83 on location and currently cutting a 8.5 window out of the 9.625 casing at a measured depth of 6,647. The proposed depth for this section is 8,395 or 200 into the Reedsville formation. The rig is mist drilling on air and the company man on site indicated they are planning on switching to fluid before penetrating the Queenston formation. Also noted is the company has indicated they with make a 8.625 reamer run on the well bore to achieve the 1 dimensional clearance between the 7.625 liner to be ran and the well bore. |
| 1469577230 | 2016-07-26 | Drill / Deepen / Reopen | No Violations | Status check inspection on the well drilling process found Nomac Drilling rig # 83 on location with the 2nd intermediate well bore section total measured drilling depth recently reached at 8,396 utilizing a 8.625 drill bit. The company will run a 7.625 liner from 6,347 to 8,376. All records pertaining to the borehole and liner have been received and reviewed. |
| 1469632702 | 2016-07-27 | Casing String Witnessed | No Violations | On this day I was on site to witness a casing liner being set and cemented out of a window cut in the 9.625 casing at 6,647. Nomac Drilling rig 83 was on location and has ran a 7.625 -29.7 lb/ft liner that measured a total of 2,049 in length with the liner top being at 6,347 and the bottom liner casing shoe at 8,376. The liner hanger was a Halliburton VersaFlex type pressure activated liner hanger. Stingray Cement service cemented the casing liner through the 5 drill string attached to the liner by the means of the liner hanger. The casing was cemented with 203 sacks of class H cement with a 15.2 lb/gl cement mix density verified by weight of scale. The cement job and liner setting procedure started with total circulation being established and 50 barrels of 6% bentonite gel spacer being ran ahead of the cement followed by the 45 barrel cement mix, a latch down wiper plug was then deployed and displaced with 192 barrels of processed liquid, upon the landing of the cement plug pressure was increased to 4900 psi to allow the circulating disc to break inside the liner hanger, a 2.250 diameter ball was then dropped to allow the liner hanger tool to cause the liner hanger to be set into the 9.625 casing string with a total of 347,000 lb pulled on the string to assist in the setting of the tool, once the tool was set the well was circulated to remove any cement debris left above the hanger, the total consist will then be pressure tested before proceeding. |
| 1470359904 | 2016-08-04 | Drill / Deepen / Reopen | No Violations | On site status check inspection found Nomac Drilling rig # 83 on location currently drilling the 6.750 production borehole at a measured depth of 11,393. The company is maintaining well control utilizing 14.2 lb./gal synthetic oil based drilling mud with 4,424 units of 3rd party gas present. |
| 1471544630 | 2016-08-18 | Drill / Deepen / Reopen | No Violations
- | |
| 1471977124 | 2016-08-23 | Drill / Deepen / Reopen | No Violations | Status check inspection on the current well drilling status found Nomac Drilling rig # 83 on location with the 6.750 production borehole total depth reached and the 5.5 production casing ran in the hole to td. During the initial stages of the cement process it was discovered that the casing was parted and the company directly pumped all the cement out of the well and began to attempt to recover all the casing. The casing in the horizontal section was not recovered and a cement plug was set from 9,275 to 8,700 on the evening of 08/23/2016. The company was pulling out of the hole with the drill string at the time of my inspection and preparing to conduct a BOP test. |
| 1553715052 | 2016-09-07 | Drill / Deepen / Reopen | No Violations | |
| 1707165262 | 2016-08-16 | Drill / Deepen / Reopen | No Violations | My inspection today finds the well operator, Gulfport Energy Corporation, has been unable to pump the KLX wireline logging tools to a depth greater than 9315. No casing failures could be found between surface and 9315. The calculated point of casing failure is between 9500 and 10,000 based on cement returns to surface. Moving forward, the company representative, Scott Treadway, stated that Gulfport intends to build mud weight from 15.4 pounds per gallon (ppg) to 15.6 ppg, then pull the free casing out of the well. Once the free casing has been retrieved, the rig will run drill pipe and a spear to make an attempt to pull the remaining casing out of the well. The well is currently static with no fluid loss or gains and no gas flow to surface. |
| 1764546166 | 2016-06-03 | Casing String Witnessed | No Violations | On site inspection to witness the surface casing cement job. Nomac Driling rig # 83 is on location and has drilled a 17.5 surface hole to a measured depth of 1,369 and ran 1,368 of 13.375 54.5lb/ft J-55 casing with a guide shoe and float collar ran along with proper centralizer placement being demonstrated. Stingray Cement Service was on location to cement the casing using 1,200 sacks of class H cement with 30% open hole cement excess ran and circulation established prior to cementing. The cement & wiper plug was displaced with 204 barrels of fluid and the casing was pressure tested to 500 psi over cement displacement pressure upon the landing of the cement plug. Circulation was established prior to and maintained throughout the job with cement returns witnessed to surface. |
| 1848929064 | 2016-11-07 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection found the well site meets ORC 1509.072. The well has been drilled and is awaiting completion. |
| 2145465844 | 2017-03-06 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection accompanied by ODNR Inspector Austin Gutridge. The area affected by the well pad construction meets ORC 1509.072 with vegetation established and erosion control in place. The lease road is stoned and in good repair. Signage is posted at the well pad entrance. Hybrid Services completion rig # 102 is on location drilling out the completion plugs on the Roger # 4-A well. The rig is situated on polymer containment with the well pad perimeter earthen berm serving as the primary containment with the pad drain valves closed. There is 6 total wells on the pad that have been drilled and stimulated that will now be completed and the initial flow back operations commenced. |
| 324812647 | 2020-4-15 0:00: | PW | No Violations | 0.30 |
| 574855393 | 2016-7-11 0:00: | DD | No Violations | 3.00 |
| 640416410 | 2016-7-14 0:00: | DD | No Violations | |
| 857105774 | 2016-6-8 0:00:0 | DD | No Violations | 1.60 |
For data sources see[10]