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Well ID: 34-115-21211 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Bristol Township | |
Operator Name: BUCKEYE OIL PRODUCING CO | |
Well Pad ID: | |
Farm/Lease Name: MILLER J O | |
License Status: Final Restoration | |
License Date: 2018-03-30 | |
Spud Date: 1971-06-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1971-07-03 | |
Well Total Depth: 4749.00 ft | |
Configuration: Vertical | |
Latitude: 39.690000 | |
Longitude: -81.780000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1971-06-18 | 853 REDMAN OIL CO INC GeoDate 6/18/71 |
Original Spud | 1971-06-21 | UPDATE LOCATION PER DOGRM SURVEY 5/21/18 ALE. GMM CHANGED PLUG STATUS PER PLUG REPORT |
Completed | 1971-07-03 | UPDATE LOCATION PER DOGRM SURVEY 5/21/18 ALE. GMM CHANGED PLUG STATUS PER PLUG REPORT |
Reached Total Depth | 1971-07-03 | UPDATE LOCATION PER DOGRM SURVEY 5/21/18 ALE. GMM CHANGED PLUG STATUS PER PLUG REPORT |
CO | 1992-12-09 | 3243 OHIO PRODUCTION CORP GeoDate 6/18/71 |
Change of Owner | 1998-03-10 | Operator changed from 3243, OHIO PRODUCTION CORP to 6091, OHIO ENERGY ASSETS, INC. |
Change of Owner | 2007-07-20 | Operator changed from 6091, OHIO ENERGY ASSETS, INC. to 56, BUCKEYE OIL PRODUCING CO |
APP | 2014-05-22 | Proposed Formations:CLINTON, Issued Date:5/22/2014, Expired Date:5/21/2016 12:00:00 PM, Drilling unit acres:75.36, Proposed Well Type:OG, Proposed Well Class: |
APP | 2018-03-30 | Proposed Formations:CLINTON, Issued Date:3/30/2018, Expired Date:3/29/2020 12:00:00 PM, Drilling unit acres:75.36, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2019-04-01 | UPDATE LOCATION PER DOGRM SURVEY 5/21/18 ALE. GMM CHANGED PLUG STATUS PER PLUG REPORT |
Record Last Modified | 2019-05-30 | UPDATE LOCATION PER DOGRM SURVEY 5/21/18 ALE. GMM CHANGED PLUG STATUS PER PLUG REPORT |
Construction Permit Expires | 2020-03-29 | UPDATE LOCATION PER DOGRM SURVEY 5/21/18 ALE. GMM CHANGED PLUG STATUS PER PLUG REPORT |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4616 | 4654 | 2 |
4616 | 4654 | 2 | |
4616 | 4654 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2700 Bbl | 60000 | FORM. BREAK @ 1880 P.S.I. AVG. PRESS 2100 PSI. @ 57 BBL. PER MIN. HORSEPOWER USED 2955 SHUT IN PRESS AFT. 5 MINS. 800 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | REDMAN OIL CO INC | 326.00 | 0.00 | 31 |
1993 | OHIO PRODUCTION CORP | 3505.00 | 132.00 | 365 |
1994 | OHIO PRODUCTION CORP | 3291.00 | 153.00 | 341 |
1995 | OHIO PRODUCTION CORP | 3306.00 | 0.00 | 365 |
1996 | OHIO PRODUCTION CORP | 2616.00 | 221.00 | 358 |
1997 | OHIO PRODUCTION CORP | 2678.00 | 152.00 | 360 |
1998 | OHIO ENERGY ASSETS, INC. | 2713.00 | 154.00 | 365 |
1999 | OHIO ENERGY ASSETS, INC. | 2682.00 | 115.00 | 365 |
2000 | OHIO ENERGY ASSETS, INC. | 2406.00 | 101.00 | 365 |
2001 | OHIO ENERGY ASSETS, INC. | 2249.00 | 105.00 | 365 |
2002 | OHIO ENERGY ASSETS, INC. | 1491.00 | 154.00 | 364 |
2003 | OHIO ENERGY ASSETS, INC. | 1944.00 | 71.00 | 353 |
2004 | OHIO ENERGY ASSETS, INC. | 2096.00 | 129.00 | 355 |
2005 | OHIO ENERGY ASSETS, INC. | 672.00 | 30.00 | 93 |
2006 | OHIO ENERGY ASSETS, INC. | 0.00 | 0.00 | 0 |
2008 | BUCKEYE OIL PRODUCING CO | 1434.00 | 14.00 | 365 |
2009 | BUCKEYE OIL PRODUCING CO | 1364.00 | 53.00 | 365 |
2010 | BUCKEYE OIL PRODUCING CO | 1484.00 | 102.00 | 365 |
2011 | BUCKEYE OIL PRODUCING CO | 2012.00 | 58.00 | 365 |
2012 | BUCKEYE OIL PRODUCING CO | 1659.00 | 0.00 | 366 |
2013 | BUCKEYE OIL PRODUCING CO | 1376.00 | 56.00 | 365 |
2014 | BUCKEYE OIL PRODUCING CO | 496.00 | 35.00 | 365 |
2017 | BUCKEYE OIL PRODUCING CO | 0.00 | 0.00 | 365 |
2018 | BUCKEYE OIL PRODUCING CO | 0.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1004738513 | 2019-3-25 0:00: | PB | No Violations | |
-1068014342 | 2018-9-10 0:00: | PW | No Violations | 0.50 |
-293615931 | 2019-5-28 0:00: | FR | No Violations | 0.40 |
0050054998 | 2011-04-05 | Production Wells | No Violations | Inspection this day found well with jack, producing. Current chart in meter, good IDs, good dike. |
0293615931 | 2019-05-28 | Final Restoration | No Violations | The final restoration meets 1509.072(B) requirements. |
0653613856 | 2019-04-01 | Plug / Plug Back | No Violations | I am back on location today to witness the plugging of this well. The surface plug needs topped off. The cement has settled out at 100 feet so the company has brought in more bags of cement to top it off. We filled the casing back to the surface with the cement. The well is now plugged. |
1004738513 | 2019-03-25 | Plug / Plug Back | No Violations | I was on location today to witness the plugging activities of this well. Bishop Well Services has moved there service rig in on this well to plug it. Today they have TimCo Wireline Services on location to shoot the bottom joint of the tubing off so they can set the bottom plug through the 2 inch diameter tubing. Once the tubing was shot off Petroset Cementing hooked onto the 2 inch tubing and pumped the bottom plug from 4539-4139 feet. The tubing was then pulled up to 3420 feet so the wireline company can drop there gun out of the bottom and perforate the Big Lime. A Big Lime plug was set from 3430-3130 feet. The rig company then pulled the tubing out of the well so the could rip the 4.5 inch casing. The plug was tagged at 3230 and the 4.5 inch casing was ripped at 3170 feet. |
1035009605 | 2019-03-28 | Plug / Plug Back | No Violations | I was back on location today to check the cement on tis well. The surface plug settled out at around 150 feet. Buckeye Oil Producing brought out 40 sacks of cement to top off the surface plug. They did not have enough sacks to top it off so they are waiting until Monday to finish it. |
1068014342 | 2018-09-10 | Production Wells | Violations Noted | I was on location today to do a field inspection on this well. During my inspection I found the well is not capable of any production. All of the production valves on the wellhead are currently closed making the well incapable of production. The last time production was reported for this well was in 2014. The well owner/operator shall submit a written plugging schedule to (Justin Smith) at (5880 Memory Rd Zanesville Oh, 43701) within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1553705490 | 2019-3-27 0:00: | PB | No Violations | 4.00 |
1790698359 | 2013-01-22 | Production Wells | No Violations | Well is in compliance. No issues are found at location. |
50054998 | 2011-4-5 0:00:0 | PW | No Violations | 0.50 |
653613856 | 2019-4-1 0:00:0 | PB | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1068014342 | US-OH-101398 | 2019-03-28 | NONE | Well shall be plugged |
For data sources see[9]