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34-115-21439

Well Details

Well ID: 34-115-21439
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Country: United States
State: Ohio
County: Morgan
Municipality: York Township
Operator Name: TEMPLE OIL & GAS CO
Well Pad ID:
Farm/Lease Name: SMITH ISAAC-STEELE & GARLINGER
License Status: Producing
License Date: 1990-12-03
Spud Date: 1991-01-23
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1991-03-12
Well Total Depth: 4197.00 ft
Configuration: Vertical
Latitude: 39.730000
Longitude: -81.980000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1990-12-03 384 TEMPLE OIL & GAS CO GeoDate 12/3/90
Oil and Gas 1990-12-03 Issued Date 12/3/90 Expired Date 12/3/91 Acres 0040000 Tool Type CT Proposed Formation CLINTON Proposed Depth 04197 Proposed Drill Depth 04197
Original Spud 1991-01-23

-1/25/2010

Completed 1991-03-12

-1/25/2010

Reached Total Depth 1991-03-12

-1/25/2010

CO 1991-04-29 384 TEMPLE OIL & GAS CO GeoDate 6/30/75
Completion Report Received 1991-05-01

-1/25/2010

Construction Permit Expires 1991-12-03

-1/25/2010

Record Last Modified 2017-02-15

-1/25/2010

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4128 4188 0
4128 4188 0
2006-09-11 4162 4169 5
4162 4169 5
4128 4188 0
2006-09-11 4174 4188 15

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1594 Bbl 20000 FRAC W/1594 BW AND 200 SX SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TEMPLE OIL & GAS CO 0.00 401.00 365
1985 TEMPLE OIL & GAS CO 0.00 349.00 365
1986 TEMPLE OIL & GAS CO 0.00 217.00 365
1987 TEMPLE OIL & GAS CO 0.00 297.00 365
1990 TEMPLE OIL & GAS CO 0.00 50.00 365
1993 TEMPLE OIL & GAS CO 8269.00 0.00 365
1995 TEMPLE OIL & GAS CO 4523.00 0.00 365
1996 TEMPLE OIL & GAS CO 6311.00 0.00 360
1997 TEMPLE OIL & GAS CO 5964.00 0.00 250
1998 TEMPLE OIL & GAS CO 2152.00 0.00 241
1999 TEMPLE OIL & GAS CO 2341.00 0.00 243
2000 TEMPLE OIL & GAS CO 4993.00 0.00 261
2001 TEMPLE OIL & GAS CO 3422.00 0.00 337
2002 TEMPLE OIL & GAS CO 3368.00 0.00 257
2003 TEMPLE OIL & GAS CO 1629.00 0.00 365
2004 TEMPLE OIL & GAS CO 2082.00 0.00 253
2005 TEMPLE OIL & GAS CO 1076.00 0.00 135
2006 TEMPLE OIL & GAS CO 55.00 0.00 244
2007 TEMPLE OIL & GAS CO 245.00 0.00 313
2008 TEMPLE OIL & GAS CO 114.00 0.00 365
2009 TEMPLE OIL & GAS CO 0.00 0.00 261
2010 TEMPLE OIL & GAS CO 0.00 0.00 0
2011 TEMPLE OIL & GAS CO 1502.00 23.00 365
2012 TEMPLE OIL & GAS CO 0.00 0.00 366
2013 TEMPLE OIL & GAS CO 0.00 0.00 365
2014 TEMPLE OIL & GAS CO 0.00 0.00 365
2015 TEMPLE OIL & GAS CO 0.00 0.00 365
2016 TEMPLE OIL & GAS CO 0.00 0.00 365
2017 TEMPLE OIL & GAS CO 0.00 0.00 365
2018 TEMPLE OIL & GAS CO 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TEMPLE OIL & GAS CO Brine 0 365
1985 TEMPLE OIL & GAS CO Brine 15 365
1986 TEMPLE OIL & GAS CO Brine 35 365
1987 TEMPLE OIL & GAS CO Brine 40 365
1990 TEMPLE OIL & GAS CO Brine 5 365
1993 TEMPLE OIL & GAS CO Brine 0 365
1995 TEMPLE OIL & GAS CO Brine 0 365
1996 TEMPLE OIL & GAS CO Brine 0 360
1997 TEMPLE OIL & GAS CO Brine 0 250
1998 TEMPLE OIL & GAS CO Brine 0 241
1999 TEMPLE OIL & GAS CO Brine 0 243
2000 TEMPLE OIL & GAS CO Brine 0 261
2001 TEMPLE OIL & GAS CO Brine 0 337
2002 TEMPLE OIL & GAS CO Brine 0 257
2003 TEMPLE OIL & GAS CO Brine 0 365
2004 TEMPLE OIL & GAS CO Brine 0 253
2005 TEMPLE OIL & GAS CO Brine 0 135
2006 TEMPLE OIL & GAS CO Brine 0 244
2007 TEMPLE OIL & GAS CO Brine 0 313
2008 TEMPLE OIL & GAS CO Brine 0 365
2009 TEMPLE OIL & GAS CO Brine 0 261
2010 TEMPLE OIL & GAS CO Brine 0 0
2011 TEMPLE OIL & GAS CO Brine 0 365
2012 TEMPLE OIL & GAS CO Brine 0 366
2013 TEMPLE OIL & GAS CO Brine 0 365
2014 TEMPLE OIL & GAS CO Brine 0 365
2015 TEMPLE OIL & GAS CO Brine 0 365
2016 TEMPLE OIL & GAS CO Brine 0 365
2017 TEMPLE OIL & GAS CO Brine 0 365
2018 TEMPLE OIL & GAS CO Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1954745030 2016-6-20 0:00: PW No Violations 2.00
-220441170 2015-10-5 0:00: PW No Violations 2.50
-252082761 2016-6-20 0:00: PW No Violations 2.00
-899349533 2020-2-11 0:00: PW No Violations 0.50
-927442533 2020-4-10 0:00: PW No Violations 0.50
0220441170 2015-10-05 Production Wells Violations Noted No identification was found at the well site. A large brine scald was found at the well location. The brine traveled downhill to another area where another scald kill area was found. Valves were open on the production lines and production lines hooked up and converted to plastic lines. Last submitted production records on file were from 2011.

The brine scald will be cleaned up and good soil brought in. The site will then be seeded and mulched to allow vegetation to reestablish at the site, this is to include both kill areas affected by brine. Proper identification will be posted at the well. Production records for this well shall be submitted to the Columbus office from 2012 to current.

0252082761 2016-06-20 Production Wells No Violations Upon my inspection today I found that vegetation has been attempted to be establish and the area has been cleaned up. The production reports have been reported and are up to date. This well is capable of production at the time of inspection.
0509712482 2007-04-07 Final Restoration No Violations Restoration work at site satisfactory.
1580303609 2015-12-31 Production Wells No Violations Follow up on compliance notice 220441170 found that an attempt at cleaning up the scald had been made. The area had been seeded and straw/hay applied as mulch. More time will be needed to see if the vegetation will grow and reestablish to cover the entire affected area. No identification was found at the well head. No production records had been submitted either.
1954745030 2016-06-20 Production Wells No Violations On my inspection today I found this well to still be shut in at the production lines. The production has been reported and updated for the well and is still being reported as 0 for the previous years.
509712482 2007-4-7 0:00:0 FR No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0220441170 US-OH-122195 2015-10-07 Well operation causing pollution and contamination
0220441170 US-OH-122196 2015-10-07 Failure to legibly identify well
0220441170 US-OH-122197 2015-10-07 Statement of annual production not filed

For data sources see[9]

References