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Well ID: 34-115-22377 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Center Township | |
Operator Name: POORBOY EXPLORATION LLC | |
Well Pad ID: | |
Farm/Lease Name: MINCKS E | |
License Status: Producing | |
License Date: 1981-03-19 | |
Spud Date: 1981-03-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-03-16 | |
Well Total Depth: 1939.00 ft | |
Configuration: Vertical | |
Latitude: 39.640000 | |
Longitude: -81.620000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 759 J H J OIL CO |
Original Spud | 1981-03-13 | |
Completed | 1981-03-16 | |
Reached Total Depth | 1981-03-16 | |
Change of Owner | 1998-12-04 | Operator changed from 759, J H J OIL CO to 4350, CENTURY WELL SERVICE |
Change of Owner | 2008-04-04 | Operator changed from 4350, CENTURY WELL SERVICE to 8312, BROAD STREET SERV LLC |
Change of Owner | 2010-12-29 | Operator changed from 8312, BROAD STREET SERV LLC to 8740, DART ENERGY LLC |
Change of Owner | 2013-08-01 | Operator changed from 8740, DART ENERGY LLC to 9156, POORBOY EXPLORATION INC |
Last Compliance Report | 2014-11-03 | |
Record Last Modified | 2014-11-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1828 | 1832 | 16 |
1828 | 1832 | 16 | |
1828 | 1832 | 16 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 57000 Gal | 0 | SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | BROAD STREET SERV LLC | 0.00 | 0.00 | 0 |
2009 | BROAD STREET SERV LLC | 0.00 | 0.00 | 0 |
2010 | DART ENERGY LLC | 0.00 | 0.00 | 0 |
2011 | DART ENERGY LLC | 6.00 | 0.00 | 3 |
2012 | DART ENERGY LLC | 110.00 | 0.00 | 300 |
2013 | DART ENERGY LLC | 0.00 | 0.00 | 0 |
2014 | POORBOY EXPLORATION LLC | 0.00 | 0.00 | 0 |
2016 | POORBOY EXPLORATION LLC | 0.00 | 0.00 | 0 |
2017 | POORBOY EXPLORATION LLC | 0.00 | 0.00 | 0 |
2018 | POORBOY EXPLORATION LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | BROAD STREET SERV LLC | Brine | 0 | 0 |
2009 | BROAD STREET SERV LLC | Brine | 0 | 0 |
2010 | DART ENERGY LLC | Brine | 0 | 0 |
2011 | DART ENERGY LLC | Brine | 0 | 3 |
2012 | DART ENERGY LLC | Brine | 0 | 300 |
2013 | DART ENERGY LLC | Brine | 0 | 0 |
2014 | POORBOY EXPLORATION LLC | Brine | 0 | 0 |
2016 | POORBOY EXPLORATION LLC | Brine | 0 | 0 |
2017 | POORBOY EXPLORATION LLC | Brine | 0 | 0 |
2018 | POORBOY EXPLORATION LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1079981785 | 2005-4-26 0:00: | PW | No Violations | |
-1149498382 | 2005-4-26 0:00: | PW | No Violations | |
-1824250607 | 2005-4-26 0:00: | PW | No Violations | |
-302955848 | 2005-4-26 0:00: | PW | No Violations | |
-597440069 | 2013-1-22 0:00: | PW | No Violations | 0.50 |
-729991456 | 2005-4-26 0:00: | PW | No Violations | |
-943027700 | 2013-6-11 0:00: | PW | No Violations | 2.00 |
0001289i91 | 2002-02-05 | Production Wells | No Violations | T.A.A.D WELL |
0302955848 | 2005-04-26 | Production Wells | Violations Noted | Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
0501655392 | 2014-04-24 | Production Wells | No Violations | Compliance Notice Follow-up 1015923271: Dave has posted identification on the tank. The well is currently shut in and he still has not restored vegetative growth on scaled area. |
0597440069 | 2013-01-22 | Production Wells | No Violations | The well is capable of producing, however it is currently shut. I spoke with Randy, owner of Dart Energy, and he said they have been working on the well and have been producing more gas but need to service the well in order to increase production. He said they will get out in the spring to hook up a new meter, disconnect the annular disposal, and fix the motor. |
0696393690 | 2005-04-26 | Production Wells | No Violations | FOLLOW UP TO NOV # -302955848 Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
0729991456 | 2005-04-26 | Production Wells | No Violations | FOLLOW UP TO NOV # -302955848 Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
0806917960 | 2007-12-03 | Annular Disposal | Violations Noted
All valves at wellhead are shut separator at site has parts missing and storage tank is in need of proper dike construction if well is too be produced. | |
0943027700 | 2013-06-11 | Production Wells | No Violations | Compliance Action Follow-up 1015923271: There has been no resolution to any of the issues. |
1015923271 | 2013-05-20 | Production Wells | Violations Noted | The inspection of the tank battery revealed a brine leak in and out of the dike. The area of contamination is around 20X20. The dike is also in poor condition and needs to be reconstructed to prevent future contamination outside of the dike. It appears that the brine came from the line that was recently disconnected from the tank. Coordinates for the well and tank were reported on earlier inspection. I called Randy Rainer and explained to him the issues and that he need to clean up the scald area and restore vegetative growth. He said he would send someone out there to look at location. |
1079981785 | 2005-04-26 | Production Wells | No Violations | FOLLOW UP TO NOV # 2002562637 FOLLOW UP TO NOV # -302955848 Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
1122506198 | 2005-07-25 | Annular Disposal | No Violations | Upon inspecting well site for compliance of NOV found no change in status of well(still idle) have made several calls to company office with no reply, so their fore recommend Chiefs Order to plug said well. |
1149498382 | 2005-04-26 | Production Wells | Violations Noted | FOLLOW UP TO NOV # -302955848 Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
1158205573 | 2014-09-25 | Production Wells | No Violations | Compliance Notice Follow-up 1015923271: The old scald area from the previous operator is still present adjacent to the tank. I talked to Dave and he stated he will have it cleaned up in a few weeks. |
1289i91 | 2002-2-5 0:00:0 | PW | No Violations | |
1387467561 | 2013-12-19 | Production Wells | No Violations | Compliance Action Follow-up 1015923271: The broken separator has been removed from location, however the brine scald still exists just outside of the dike. The operator is still trying to get well back into commercial production. I will come back in Spring to see if they has cleaned up and restored the location. |
1644805276 | 2005-04-26 | Production Wells | No Violations | FOLLOW UP TO NOV # 696393690 FOLLOW UP TO NOV # -302955848 Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
1802579024 | 2014-10-20 | Production Wells | No Violations | The well is now in compliance. |
1824250607 | 2005-04-26 | Production Wells | No Violations | FOLLOW UP TO NOV # -1149498382 FOLLOW UP TO NOV # -302955848 Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
2002562637 | 2005-04-26 | Production Wells | No Violations | FOLLOW UP TO NOV # -302955848 Upon well site found well to be idle(incorrect I.D.posted) no production has been reported on well since current owner has owned well,well is quipped with pumpjack with no motor,and 1-100 bbl tank and separator. |
2012321628 | 2009-03-11 | Annular Disposal | No Violations | A.D. not hooked up, well is still idle and incapable of producing in its present state of repair,have called company several times with no response in getting outstanding violations at site resolved,Recommend Chiefs Order to plug said well. |
2094951620 | 2013-09-03 | Production Wells | No Violations | Compliance Action Follow-up 1015923271: There has been no resolution to any of the issues. There is now a leak from a broken separator which is laying down on the ground. A rag has been stuffed into one of the pipes and is dripping brine. |
501655392 | 2014-4-24 0:00: | PW | No Violations | 0.30 |
588163049 | 2020-5-19 0:00: | TD | No Violations | 0.50 |
696393690 | 2005-4-26 0:00: | PW | No Violations | |
806917960 | 2007-12-3 0:00: | AD | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0302955848 | US-OH-123149 | 2005-04-30 | Failure to legibly identify well | |
0302955848 | US-OH-123150 | 2005-04-30 | Well shall be plugged | |
0806917960 | US-OH-129170 | 2015-01-08 | Failure to legibly identify well | |
0806917960 | US-OH-129171 | 2015-01-08 | Well shall be plugged | |
1015923271 | US-OH-100079 | 2014-10-28 | Well operation causing pollution and contamination | |
1015923271 | US-OH-100080 | 2014-10-28 | No SPCC dike/or failure to keep dike free of water or oil | |
1015923271 | US-OH-100081 | 2014-10-28 | Dike or pit not able to prevent escape of brine or other wastes | |
1149498382 | US-OH-103893 | 2005-04-30 | Failure to legibly identify well | |
1149498382 | US-OH-103894 | 2005-04-30 | Well shall be plugged |
For data sources see[9]