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| Well ID: 34-115-22519 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Morgan | |
| Municipality: Penn Township | |
| Operator Name: STONEBRIDGE OPERATING CO LLC | |
| Well Pad ID: | |
| Farm/Lease Name: JUTTE RALPH | |
| License Status: Final Restoration | |
| License Date: 2009-05-01 | |
| Spud Date: 1982-06-25 | |
| Spud Drilling Contractor: BEVERLY DRLG | |
| Final Drill Date: 1982-07-03 | |
| Well Total Depth: 4955.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.570000 | |
| Longitude: -81.840000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1982-06-03 | Issued Date 6/3/82 Expired Date 12/1/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04955 Proposed Drill Depth 04955 |
| Original Spud | 1982-06-25 | |
| Completed | 1982-07-03 | |
| Reached Total Depth | 1982-07-03 | |
| Completion Report Received | 1982-08-09 | |
| CO | 1982-12-29 | 2098 OPI INC GeoDate 6/3/82 |
| CO | 1994-06-28 | 631 BT ENERGY CORP GeoDate 6/3/82 |
| Change of Owner | 2007-10-12 | Operator changed from 631, BT ENERGY CORP to 2070, STONEBRIDGE OPERATING CO |
| Last Compliance Report | 2009-04-13 | |
| APP | 2009-05-01 | Proposed Formations:PENNSYLVANIA/BEREA/DEVONIAN SHALE/BIG LIME, Issued Date:5/1/2009, Expired Date:5/1/2010 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:TAAD, Proposed Well Class:ENPW |
| Plugged/Abandoned | 2010-04-28 | |
| Construction Permit Expires | 2010-05-01 | |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 4785 | 4807 | 0 |
| 4785 | 4807 | 0 | |
| 2006-09-11 | 4871 | 4877 | 14 |
| 4871 | 4877 | 14 | |
| 4785 | 4807 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 1280 Bbl | 30000 | FRAC: 1280 BBL H2O, 30M SAND |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | BT ENERGY CORP | 7458.00 | 1371.00 | 365 |
| 1985 | BT ENERGY CORP | 7470.00 | 1449.00 | 148 |
| 1986 | BT ENERGY CORP | 7363.00 | 1449.00 | 365 |
| 1987 | BT ENERGY CORP | 9662.00 | 1061.00 | 365 |
| 1995 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
| 1996 | BT ENERGY CORP | 217.00 | 147.00 | 91 |
| 1997 | BT ENERGY CORP | 2477.00 | 699.00 | 91 |
| 1998 | STONEBRIDGE OPERATING CO LLC | 6565.00 | 740.00 | 344 |
| 1999 | BT ENERGY CORP | 4047.00 | 532.00 | 315 |
| 2000 | STONEBRIDGE OPERATING CO LLC | 2586.00 | 515.00 | 366 |
| 2001 | STONEBRIDGE OPERATING CO LLC | 2227.00 | 707.00 | 365 |
| 2002 | BT ENERGY CORP | 2358.00 | 178.00 | 364 |
| 2003 | BT ENERGY CORP | 128.00 | 48.00 | 175 |
| 2004 | BT ENERGY CORP | 29.00 | 0.00 | 61 |
| 2005 | BT ENERGY CORP | 7.00 | 0.00 | 61 |
| 2006 | BT ENERGY CORP | 0.00 | 0.00 | 91 |
| 2007 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 343 |
| 2008 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 365 |
| 2009 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 7 |
| 2010 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 217 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | BT ENERGY CORP | Brine | 0 | 365 |
| 1985 | BT ENERGY CORP | Brine | 75 | 148 |
| 1986 | BT ENERGY CORP | Brine | 100 | 365 |
| 1987 | BT ENERGY CORP | Brine | 40 | 365 |
| 1995 | BT ENERGY CORP | Brine | 0 | 0 |
| 1996 | BT ENERGY CORP | Brine | 0 | 91 |
| 1997 | BT ENERGY CORP | Brine | 0 | 91 |
| 1998 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 344 |
| 1999 | BT ENERGY CORP | Brine | 76 | 315 |
| 2000 | STONEBRIDGE OPERATING CO LLC | Brine | 90 | 366 |
| 2001 | STONEBRIDGE OPERATING CO LLC | Brine | 42 | 365 |
| 2002 | BT ENERGY CORP | Brine | 464 | 364 |
| 2003 | BT ENERGY CORP | Brine | 35 | 175 |
| 2004 | BT ENERGY CORP | Brine | 1555 | 61 |
| 2005 | BT ENERGY CORP | Brine | 1555 | 61 |
| 2006 | BT ENERGY CORP | Brine | 0 | 91 |
| 2007 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 343 |
| 2008 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 365 |
| 2009 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 7 |
| 2010 | STONEBRIDGE OPERATING CO LLC | Brine | 41 | 217 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1036617255 | 2009-3-2 0:00:0 | AD | No Violations | |
| -1777081899 | 2009-3-2 0:00:0 | AD | No Violations | |
| -561746067 | 2011-6-14 0:00: | FR | No Violations | 0.70 |
| -851215289 | 2009-3-2 0:00:0 | AD | No Violations | |
| 0000PL9986 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0193227297 | 2009-03-02 | Annular Disposal | No Violations | FOLLOW UP TO NOV # -1036617255 FOLLOW UP TO NOV # 1329179716 Upon inspecting site at request of landowner Ralph Juttee found well incapable of producing,pump jack has been removed and tubing&rods removed from site, landowner stated that owner told him that casing has a hole in ,making it incapable of producing in its present state of repair,the last production reported on well was back in 2005. |
| 0241868633 | 2009-03-02 | Annular Disposal | No Violations | FOLLOW UP TO NOV # -851215289 FOLLOW UP TO NOV # 1329179716 Upon inspecting site at request of landowner Ralph Juttee found well incapable of producing,pump jack has been removed and tubing&rods removed from site, landowner stated that owner told him that casing has a hole in ,making it incapable of producing in |
| 0561746067 | 2011-06-14 | Final Restoration | No Violations | Inspection this day found location and lease road reclaimed, grass growing nicely, no debris, |
| 0851215289 | 2009-03-02 | Annular Disposal | No Violations | FOLLOW UP TO NOV # 1329179716 Upon inspecting site at request of landowner Ralph Juttee found well incapable of producing,pump jack has been removed and tubing&rods removed from site, landowner stated that owner told him that casing has a hole in ,making it incapable of producing in |
| 1036617255 | 2009-03-02 | Annular Disposal | No Violations | FOLLOW UP TO NOV # 1329179716 Upon inspecting site at request of landowner Ralph Juttee found well incapable of producing,pump jack has been removed and tubing&rods removed from site, landowner stated that owner told him that casing has a hole in ,making it incapable of producing in its present state of repair,the last production reported on well was back in 2005. |
| 1329179716 | 2009-03-02 | Annular Disposal | Violations Noted | Upon inspecting site at request of landowner Ralph Juttee found well incapable of producing,pump jack has been removed and tubing&rods removed from site, landowner stated that owner told him that casing has a hole in ,making it incapable of producing in its present state of repair,the last production reported on well was back in 2005. |
| 1777081899 | 2009-03-02 | Annular Disposal | No Violations | FOLLOW UP TO NOV # 1329179716. I inspected this site at request of landowner, Ralph Juttee. I found this well incapable of producing. The pumping unit, tubing and rods have been removed. The landowner stated that the owner told him that casing has a hole it, making it incapable of production. 1/20/12 - Records show well plugged 4/10 - RESOLVED |
| 193227297 | 2009-3-2 0:00:0 | AD | No Violations | |
| 241868633 | 2009-3-2 0:00:0 | AD | No Violations | |
| PL9986 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 1329179716 | US-OH-109419 | 2009-03-03 | Well shall be plugged |
For data sources see[9]