If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-115-23319 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.67,"lon":-82,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Deerfield Township | |
Operator Name: J T PLUS WELL SERVICE LLC | |
Well Pad ID: | |
Farm/Lease Name: BELL RICHARD | |
License Status: Producing | |
License Date: 1983-10-20 | |
Spud Date: 1983-10-20 | |
Spud Drilling Contractor: [[ALTEX INC [ALTHEIRS]]] | |
Final Drill Date: 1983-11-17 | |
Well Total Depth: 1418.00 ft | |
Configuration: Vertical | |
Latitude: 39.670000 | |
Longitude: -82.000000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1983-09-20 | |
Oil and Gas | 1983-10-20 | Issued Date 10/20/83 Expired Date 4/17/84 Acres 0010000 Tool Type CT Proposed Formation BEREA Proposed Depth 01418 Proposed Drill Depth 01418 |
Completed | 1983-11-17 | |
Reached Total Depth | 1983-11-17 | |
CO | 1983-11-26 | 482 ALTIER J V GAS & OIL GeoDate 10/20/83 |
Construction Permit Expires | 1984-04-17 | |
Completion Report Received | 1984-07-26 | |
Change of Owner | 2007-11-27 | Operator changed from 482, ALTIER J V GAS & OIL to 1512, ALTIER H L SERVICE CO INC |
Change of Owner | 2015-01-09 | Operator changed from 1512, ALTIER H L SERVICE CO INC to 8699, J T PLUS WELL SERVICE LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 1340 | 1356 | 0 |
1340 | 1356 | 0 | |
2006-09-11 | 1348 | 1350 | 1 |
1348 | 1350 | 1 | |
1340 | 1356 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | FRAC: FOAM,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | J V ALTIER GAS & OIL INC | 315.00 | 70.00 | 365 |
1992 | J V ALTIER GAS & OIL INC | 465.00 | 76.00 | 365 |
2001 | H L ALTIER SERVICE CO INC | 0.00 | 37.00 | 30 |
2002 | H L ALTIER SERVICE CO INC | 15.00 | 35.00 | 365 |
2003 | H L ALTIER SERVICE CO INC | 20.00 | 52.00 | 365 |
2004 | H L ALTIER SERVICE CO INC | 20.00 | 21.00 | 365 |
2005 | H L ALTIER SERVICE CO INC | 20.00 | 0.00 | 365 |
2006 | H L ALTIER SERVICE CO INC | 12.00 | 0.00 | 365 |
2007 | H L ALTIER SERVICE CO INC | 35.00 | 18.00 | 365 |
2009 | H L ALTIER SERVICE CO INC | 0.00 | 0.00 | 365 |
2010 | H L ALTIER SERVICE CO INC | 0.00 | 0.00 | 365 |
2011 | H L ALTIER SERVICE CO INC | 0.00 | 0.00 | 365 |
2012 | H L ALTIER SERVICE CO INC | 0.00 | 0.00 | 366 |
2013 | H L ALTIER SERVICE CO INC | 0.00 | 7.00 | 365 |
2015 | J T PLUS WELL SERVICE LLC | 0.00 | 154.00 | 365 |
2016 | J T PLUS WELL SERVICE LLC | 0.00 | 0.00 | 0 |
2017 | J T PLUS WELL SERVICE LLC | 0.00 | 0.00 | 0 |
2018 | J T PLUS WELL SERVICE LLC | 19.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | J V ALTIER GAS & OIL INC | Brine | 120 | 365 |
1992 | J V ALTIER GAS & OIL INC | Brine | 0 | 365 |
2001 | H L ALTIER SERVICE CO INC | Brine | 0 | 30 |
2002 | H L ALTIER SERVICE CO INC | Brine | 10 | 365 |
2003 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2004 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2005 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2006 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2007 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2009 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2010 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2011 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2012 | H L ALTIER SERVICE CO INC | Brine | 0 | 366 |
2013 | H L ALTIER SERVICE CO INC | Brine | 0 | 365 |
2015 | J T PLUS WELL SERVICE LLC | Brine | 0 | 365 |
2016 | J T PLUS WELL SERVICE LLC | Brine | 0 | 0 |
2017 | J T PLUS WELL SERVICE LLC | Brine | 0 | 0 |
2018 | J T PLUS WELL SERVICE LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1633525992 | 2007-3-22 0:00: | PW | No Violations | |
-1927393489 | 2015-1-12 0:00: | PW | No Violations | 1.00 |
-254523404 | 2015-2-12 0:00: | PW | No Violations | 0.70 |
0000PL9652 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0254523404 | 2015-02-12 | Production Wells | No Violations | Compliance Follow-up -1927393489: There is still contamination in the dike and one tank has a slow leak of oil coming from the nipple. The well has recently been transferred to JT Plus Well Service. I called and left a message. |
0346063516 | 2015-02-20 | Administrative Inspection | No Violations | Compliance Follow-up -1927393489: Pat Altier called and stated that he was aware of the dike contamination and would clean everything up and get things in order in the next few weeks. |
1575449559 | 2015-05-20 | Production Wells | No Violations | I was at this well to do a follow-up inspection on it. Pat Altier contacted me last week and said they got the dike cleaned up and fixed the dike. During my inspection I found the contamination had been removed and new stone has been brought in for the dike. The violations have been resolved. There are no violations at this time. |
1633525992 | 2007-03-22 | Production Wells | No Violations | |
1886350616 | 2015-03-23 | Administrative Inspection | No Violations | I talked with Pat Altier and he stated he has some guys lined up to head over to tank battery to clean up the mess in the dike. |
1927393489 | 2015-01-12 | Production Wells | Violations Noted | The well is currently in production and being used for domestic use. There is oil and brine contamination in the dike. I called Tim Altier and left a message explaining the issues. |
346063516 | 2015-2-20 0:00: | AM | No Violations | 0.30 |
826508944 | 2020-10-22 0:00 | PW | No Violations | 1.00 |
PL9652 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1927393489 | US-OH-119402 | 2015-07-20 | Well operation causing pollution and contamination |
For data sources see[9]