X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-115-23325

Well Details

Well ID: 34-115-23325
Loading map...
Country: United States
State: Ohio
County: Morgan
Municipality: Bloom Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: KLIES
License Status: Producing
License Date: 2019-03-25
Spud Date: 1983-11-07
Spud Drilling Contractor: SWANK-ULLMAN
Final Drill Date: 1983-11-09
Well Total Depth: 1640.00 ft
Configuration: Vertical
Latitude: 39.740000
Longitude: -81.830000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1983-11-04 Issued Date 11/4/83 Expired Date 5/2/84 Acres 0020000 Tool Type RTAF Proposed Formation BEREA Proposed Depth 01640 Proposed Drill Depth 01640
Original Spud 1983-11-07
Completed 1983-11-09
Reached Total Depth 1983-11-09
CO 1983-12-05 1177 ENERGY DISTRIBUTORS INC GeoDate 11/4/83
Completion Report Received 1983-12-06
CO 1991-12-11 3071 KINGSTON OIL CORP GeoDate 11/4/83
Change of Owner 2001-01-12 Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC
Change of Owner 2004-03-03 Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC
APP 2013-03-12 Proposed Formations:BEREA, Issued Date:3/12/2013, Expired Date:3/12/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2015-05-29 Proposed Formations:BEREA, Issued Date:5/29/2015, Expired Date:5/28/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2017-10-17 Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC
APP 2019-03-25 Proposed Formations:BEREA, Issued Date:3/25/2019, Expired Date:3/24/2021 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2019-04-01
Construction Permit Expires 2021-03-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1493 1513 0
1493 1513 0
2006-09-11 1512 1554 11
1512 1554 11
1493 1513 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 0 0 FRAC: FOAMED WATER, SAND, N2
H2O 0 300 Bbl 30000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 B B ENERGY CORP 11749.00 0.00 0
1987 ENERGY DISTRIBUTORS INC 495.00 0.00 0
1988 KINGSTON OIL CORP 737.00 0.00 0
1989 KINGSTON OIL CORP 546.00 0.00 365
1990 KINGSTON OIL CORP 633.00 13.00 365
1991 B B ENERGY CORP 32396.00 0.00 365
1992 KINGSTON OIL CORP 395.00 0.00 350
1993 KINGSTON OIL CORP 386.00 8.00 350
1994 KINGSTON OIL CORP 418.00 0.00 350
1995 KINGSTON OIL CORP 334.00 8.00 350
1996 KINGSTON OIL CORP 269.00 0.00 350
1997 KINGSTON OIL CORP 294.00 0.00 350
1998 KINGSTON OIL CORP 262.00 0.00 350
1999 KINGSTON OIL CORP 168.00 0.00 0
2000 KINGSTON OIL CORP 216.00 0.00 0
2001 CHEVRON APPALACHIA LLC 103.00 0.00 330
2002 CHEVRON APPALACHIA LLC 135.00 0.00 365
2003 ATLAS NOBLE LLC 169.00 0.00 365
2004 ATLAS NOBLE LLC 157.00 8.00 365
2005 ATLAS NOBLE LLC 168.00 0.00 365
2006 ATLAS NOBLE LLC 110.00 0.00 365
2007 ATLAS NOBLE LLC 32.00 0.00 365
2008 ATLAS NOBLE LLC 27.00 0.00 366
2009 ATLAS NOBLE LLC 15.00 0.00 365
2010 ATLAS NOBLE LLC 0.00 0.00 365
2011 ATLAS NOBLE LLC 0.00 0.00 0
2012 ATLAS NOBLE LLC 0.00 0.00 366
2013 ATLAS NOBLE LLC 0.00 0.00 365
2014 ATLAS NOBLE LLC 0.00 0.00 365
2015 ATLAS NOBLE LLC 0.00 0.00 365
2016 ATLAS NOBLE LLC 0.00 0.00 0
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 B B ENERGY CORP Brine 0 0
1987 ENERGY DISTRIBUTORS INC Brine 41 0
1988 KINGSTON OIL CORP Brine 142 0
1989 KINGSTON OIL CORP Brine 270 365
1990 KINGSTON OIL CORP Brine 224 365
1991 B B ENERGY CORP Brine 0 365
1992 KINGSTON OIL CORP Brine 223 350
1993 KINGSTON OIL CORP Brine 204 350
1994 KINGSTON OIL CORP Brine 208 350
1995 KINGSTON OIL CORP Brine 202 350
1996 KINGSTON OIL CORP Brine 165 350
1997 KINGSTON OIL CORP Brine 167 350
1998 KINGSTON OIL CORP Brine 162 350
1999 KINGSTON OIL CORP Brine 38
2000 KINGSTON OIL CORP Brine 0
2001 CHEVRON APPALACHIA LLC Brine 0 330
2002 CHEVRON APPALACHIA LLC Brine 0 365
2003 ATLAS NOBLE LLC Brine 0 365
2004 ATLAS NOBLE LLC Brine 0 365
2005 ATLAS NOBLE LLC Brine 0 365
2006 ATLAS NOBLE LLC Brine 0 365
2007 ATLAS NOBLE LLC Brine 0 365
2008 ATLAS NOBLE LLC Brine 0 366
2009 ATLAS NOBLE LLC Brine 0 365
2010 ATLAS NOBLE LLC Brine 0 365
2011 ATLAS NOBLE LLC Brine 0
2012 ATLAS NOBLE LLC Brine 0 366
2013 ATLAS NOBLE LLC Brine 0 365
2014 ATLAS NOBLE LLC Brine 0 365
2015 ATLAS NOBLE LLC Brine 0 365
2016 ATLAS NOBLE LLC Brine 0 0
2017 ATLAS NOBLE LLC Brine 0 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1040023812 2019-1-25 0:00: PW No Violations 0.50
-1157318770 2016-1-12 0:00: PW No Violations 1.00
-1583254268 2017-3-13 0:00: PW No Violations 1.00
-1770913328 2018-9-28 0:00: PW No Violations 0.50
-1796341561 2014-3-11 0:00: PW No Violations 0.50
-2069327875 2019-6-20 0:00: PW No Violations 7.00
-2103018221 2013-4-30 0:00: PW No Violations 0.50
-437639182 2016-4-5 0:00:0 PW No Violations 2.00
-714880789 2013-11-25 0:00 PW No Violations 0.80
-992164785 2018-12-14 0:00 PW No Violations 0.50
0000PL9647 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0437639182 2016-04-05 Production Wells No Violations Upon my follow-up today I found this well to still have its valves closed and not producing. I called Pat Irvin from Atlas and he informed me they do plan on plugging the wells but, the company they use for cement has been having issues with money. They put the rigs in the Atlass yard and will be plugging as soon as they get the money to afford it. There has been no resolution to the issue.
0477713150 2018-08-16 Production Wells No Violations I was on location today to do a follow-up inspection on this well for being idle and incapable of production. At this time there has been no change in the status of this well. the well is still sitting here idle and is not capable of production. I will contact Jody Jasper to see if I can get some information on what they are planning to do with the well.
0529594311 2017-11-13 Production Wells No Violations I have returned to this well today to do a follow-up inspection on it. At this time the well is still idle and incapable of production. All of the production valves are shut at the wellhead making the well incapable of any type of production. The well is still in violation.
0714880789 2013-11-25 Production Wells No Violations Compliance Action Follow-up 1658775082: There has been no resolution to any of the well issues. I called and left Mark of Atlas, a message regarding the issues.
0824886257 2015-01-06 Production Wells No Violations On my inspection today I found this well to be equipped with a 4 1/2 inch well head with 2 inch tubbing and a pump jack. The ball valves on the well head are all shut in. I spoke with Atlas on the phone and they informed me this was one of their many wells they were rotating with keeping closed or open to try and see if they can get production from the hole. They stated if there is no production they plan to plug and abandon the well as soon as possible. I told them I would call again in 30 days for any more updates. No tanks associated with this well could be found.
0885738456 2018-02-06 Production Wells No Violations I received a phone call today from Jody Jasper following up on the message I left him. He told me he did not know what was going on with this well. He asked me who the previous owner was and took down the information about the well. Jody stated that he would be contacting the pumper in the area to find out more about the well.
0992164785 2018-12-14 Production Wells No Violations I was back on location to follow up on the compliance notice issued on this well. The well at the time of my inspection is still sitting idle and incapable of production. I spoke with Allen Tarleton the production supervisor for the company today during my inspection and told me that he would try to find out what is going on with this well. He let me know he does not know anything about them at this time because of transferring from another area but he would let me know what he finds out.
1003418221 2014-07-28 Production Wells No Violations Compliance Action Follow-up 1658775082: There has been no resolution to any of the well issues. Gas is bubbling out between the 4.5 casing head and tubing. The well is still not in production. I calledand left a message with Pat Irving of Atlas.
1040023812 2019-01-25 Production Wells No Violations I was back on location today to follow-up on the well for non production and being idle. The status of the well has not changed. I left a message with Allen the production supervisor in this area but have not received anything back
1157318770 2016-01-12 Production Wells No Violations On my inspection today I did a follow up inspection on the compliance notice already on this well. There has been no resolution to any of the issues on this well.
1198042653 2014-10-06 Administrative Inspection No Violations Compliance Action Follow-up 1658775082: I talked with Pat Irving of Atlas and he stated that he will call me next week to update me on the status of his plugging rig and if he can get it to Morgan County this year.
1247274874 2016-08-24 Production Wells No Violations I returned to this well to do a follow-up on the compliance notice issued on this well. The well at this time still has the production valves shut at the well head making the well incapable of any production. The well is still currently still in violation. I took photos of the well today during my inspection.
1583254268 2017-03-13 Production Wells No Violations The inspection this day revealed that this well is equipped with a pumping unit, a 4 1/2 inch diameter wellhead, and 1 1/2 inch diameter production tubing. The valves on the wellhead are closed at the time of inspection. I was unable to located any tanks associated with this well in the area. There has been no resolution to this issue on this well and the well is not in production at the time of inspection.
1658775082 2012-12-27 Production Wells Violations Noted Well is sitting idle and equipped with 8, 4.5 casing, tubing, and rusted rod. The pumpjack has no motor and electric box is disconnected. The valves on casing are closed.
1733116368 2015-11-04 Production Wells No Violations Compliance Action Follow-up 1658775082: This well is still sitting idle. The valve on the production string is still closed and the valve on the 4 1/2 is still closed. There is no electric motor. There are parts of the unit strewn around the location. There is also a piece of plastic pipe not being used at the site. This well sits about 125 off of ST RT 376.
1770913328 2018-09-28 Production Wells No Violations I was back on location today to do a follow-up inspection on this well. At this time the valves on the wellhead are still shut in making the well incapable of production. The vegetation has overgrown around the pumping unit. There are no signs of the well being in production. I left a message with Matt Kapinus one of the Production supervisors for M&R Investments. He let me know that these wells are under Allen Tarletons area so I sent Allen a message to follow-up on the wells. I have not received a response back from him at this time.
1796341561 2014-03-11 Production Wells No Violations Compliance Action Follow-up 1658775082: There has been no resolution to any of the well issues. The well is still equipped with a pumpjack which has no motor. The valves are shut on the wellhead. I called and left Mark, of Atlas, a message regarding these issues.
1832254113 2020-3-24 0:00: PW No Violations 0.50
1838105370 2019-6-17 0:00: PB No Violations 0.50
1843128280 2018-05-02 Production Wells No Violations I have returned to this well today to do a follow-up inspection on it. At this time the well is still idle and incapable of production. All of the production valves are shut at the wellhead making the well incapable of production. The well is still in violation at this time. The compliance notice on the well was issued on 12/27/2012. I contacted Jody Jasper today to talk with him about the well. Jody said he would have to go back through his notes to see what they had decided and would let me know.
1879900445 2018-02-02 Production Wells No Violations I have returned to this well today to do a follow-up inspection on it. At this time the well is still idle and incapable of production. All of the production valves are shut at the wellhead making the well incapable of production. The well is still in violation at this time. The compliance notice on the well was issued on 12/27/2012. I called Jody Jasper today and left him a message letting him know I was doing a follow-up inspection on the well.
1884788951 2019-11-25 0:00 PW No Violations 0.40
1917773552 2018-08-31 Production Wells No Violations I was back on location today to do a follow-up on this well and check the status of it. At this time the well is still idle and incapable of production with all of the production valves shut at the well. I have sent a message to Jody Jasper to see if he can get me an update on the well to see if they will be put back in production or plugged.
2103018221 2013-04-30 Production Wells Violations Noted Compliance Action Follow-up 1658775082: There has been no resolution to any of the well issues. Gas is now bubbling between the 4.5 casing collar and tubing.
2112947064 2018-03-13 Production Wells No Violations I have returned to this well today to do a follow-up inspection on it. At this time the well is still idle and incapable of production. All of the production valves are shut at the wellhead making the well incapable of production. The well is still in violation at this time. The compliance notice on the well was issued on 12/27/2012. I will be calling Jody Jasper again today to get a follow-up on this well.
477713150 2018-8-16 0:00: PW No Violations 0.50
529594311 2017-11-13 0:00 PW No Violations 0.50
824886257 2015-1-6 0:00:0 PW No Violations 1.00
885738456 2018-2-6 0:00:0 PW No Violations 0.20
PL9647 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1658775082 US-OH-116385 2012-12-27 Forfeiture of bond
1658775082 US-OH-116386 2012-12-27 Nonproduction; well shall be plugged or placed in temporary inactive status
2103018221 US-OH-121504 2013-06-12 Equipment pressure rated below operating pressure

For data sources see[9]

References