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34-115-23847

Well Details

Well ID: 34-115-23847
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Country: United States
State: Ohio
County: Morgan
Municipality: Deerfield Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: DINGEY
License Status: Producing
License Date: 1985-05-08
Spud Date: 1985-08-28
Spud Drilling Contractor: DUSTY DRILLING
Final Drill Date: 1985-09-17
Well Total Depth: 1372.00 ft
Configuration: Vertical
Latitude: 39.660000
Longitude: -81.940000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1985-05-08 Issued Date 5/8/85 Expired Date 11/4/85 Acres 0010000 Tool Type CT Proposed Formation BEREA Proposed Depth 01372 Proposed Drill Depth 01372
Original Spud 1985-08-28
Completed 1985-09-17
Reached Total Depth 1985-09-17
CO 1985-10-04 1868 DUSTY DRILL & PRO CORP GeoDate 5/8/85
Completion Report Received 1985-10-21
Construction Permit Expires 1985-11-04
Change of Owner 2003-09-24 Operator changed from 1868, DUSTY DRILL & PRO CORP to 2867, DNL OIL CORP
Change of Owner 2007-07-11 Operator changed from 2867, DNL OIL CORP to 8227, DEEP RESOURCES LLC
Change of Owner 2011-10-13 Operator changed from 8227, DEEP RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1322 1340 0
1322 1340 0
2006-09-11 1336 1338 1
1336 1338 1
1322 1340 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1025 Bbl 20000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 DUSTY DRILLING & PRODUCING COR 179.00 341.00 182
1986 DUSTY DRILLING & PRODUCING COR 1292.00 648.00 365
1987 DUSTY DRILLING & PRODUCING COR 710.00 232.00 365
1988 DUSTY DRILLING & PRODUCING COR 672.00 209.00 323
1989 DUSTY DRILLING & PRODUCING COR 652.00 109.00 330
1990 DUSTY DRILLING & PRODUCING COR 601.00 117.00 351
1991 DUSTY DRILLING & PRODUCING COR 675.00 179.00 351
1992 DUSTY DRILLING & PRODUCING COR 747.00 119.00 365
1994 DUSTY DRILLING & PRODUCING COR 696.00 186.00 365
1995 DUSTY DRILLING & PRODUCING COR 37.00 176.00 365
2005 DNL OIL CORP 619.00 147.00 365
2006 DNL OIL CORP 595.00 145.00 365
2007 DNL OIL CORP 72.00 62.00 183
2010 DEEP RESOURCES LLC 154.00 157.00 365
2011 DEEP RESOURCES LLC 134.00 38.00 90
2012 M & R INVESTMENTS OHIO LLC 70.00 0.00 366
2013 M & R INVESTMENTS OHIO LLC 0.00 64.00 365
2014 M & R INVESTMENTS OHIO LLC 0.00 140.00 365
2015 M & R INVESTMENTS OHIO LLC 10.00 0.00 365
2016 M & R INVESTMENTS OHIO LLC 10.00 0.00 0
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 DUSTY DRILLING & PRODUCING COR Brine 360 182
1986 DUSTY DRILLING & PRODUCING COR Brine 686 365
1987 DUSTY DRILLING & PRODUCING COR Brine 370 365
1988 DUSTY DRILLING & PRODUCING COR Brine 330 323
1989 DUSTY DRILLING & PRODUCING COR Brine 172 330
1990 DUSTY DRILLING & PRODUCING COR Brine 184 351
1991 DUSTY DRILLING & PRODUCING COR Brine 283 351
1992 DUSTY DRILLING & PRODUCING COR Brine 187 365
1994 DUSTY DRILLING & PRODUCING COR Brine 0 365
1995 DUSTY DRILLING & PRODUCING COR Brine 0 365
2005 DNL OIL CORP Brine 90 365
2006 DNL OIL CORP Brine 77 365
2007 DNL OIL CORP Brine 62 183
2010 DEEP RESOURCES LLC Brine 0 365
2011 DEEP RESOURCES LLC Brine 0 90
2012 M & R INVESTMENTS OHIO LLC Brine 0 366
2013 M & R INVESTMENTS OHIO LLC Brine 0 365
2014 M & R INVESTMENTS OHIO LLC Brine 88 365
2015 M & R INVESTMENTS OHIO LLC Brine 0 365
2016 M & R INVESTMENTS OHIO LLC Brine 120 0
2017 M & R INVESTMENTS OHIO LLC Brine 7 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1154157541 2015-5-20 0:00: PW No Violations 1.00
-1273868557 2014-2-27 0:00: PW No Violations 2.80
-1440672697 2014-3-28 0:00: PW No Violations 1.30
0000PL9411 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0029116408 2014-03-21 Production Wells No Violations Compliance Follow-up -1273868557: The pumpjack horse head and bridle have been re-attached to the pumpjack and Andy Corp has repaired the stuffing box. Andy will have the contamination cleaned up by next Thursday and will restore vegetative growth in the next few months.
0506240713 2015-02-09 Production Wells Violations Noted Upon inspection, I found that the 1500 gallon tank was full and leaking in several areas. There were signs that the dike was holding brine. There is evidence of brine outside of the dike around the drain pipe. Quantabs revealed over 600 ppm of chlorides all around the outside and inside of the dike. I called and left messages with field supervisor, Jody Jasper, and Manager Rusty Hutson. I talked to well tender, Andy Corp and explained the issues. Operator needs to remove leaking tank and all contamination in and outside of the dike.
0692506244 2014-12-23 Production Wells No Violations Compliance Follow-up -1273868557: Andy Corp, of M & R, has replaced the flow line and secured it up above the stream in one area but has yet to do the same to the area that had the main concern. The original issues concerning the electric and flow lines tangled up and lying in the streams still has no resolution. Andy said he would finish the job this week.
0891078853 2015-03-10 Production Wells No Violations Compliance follow-up -1273868557: Operator has removed the flow line from the creekbed and chained it to a tree. They have also severed the electric line but there are no signs they have reconnected it anywhere else.
1154157541 2015-05-20 Production Wells No Violations I was at this well to do a follow-up inspection on it. The violations have been resolved at this time. The well is in production and there are no violations.
1273868557 2014-02-27 Production Wells Violations Noted I met the landowner Jim Flynn out at his property to inspect three wells. This well is equipped with a pumpjack with it head disconnected and laying on the ground. It was still attached to the rods. There is contamination from the stuffing box all around the wellhead. The valves were open and the landowner stated Andy Corp was out there in October repairing the leaking stuffing box. The flow line and electric line run through the creek down below and both are exposed in the water and in danger of breaking from debris. I talked with the field supervisor Jody Jasper and he said they would get on all of these problems this week. Operator must remove and properly dispose of all contamination and repair or replace any faulty equipment.
1415229812 2014-11-05 Production Wells No Violations Compliance Follow-up -1273868557: I was on location with Diversified/M & R Investments field manager, Rusty Hutson. He stated that they will order two rolls of plastic flow line to replace and re-route the old, bent lines in the stream. They will also re-route the electric line.
1423758806 2015-02-12 Production Wells No Violations Compliance follow-up -1273868557: I was on location to witness operator replace the plastic tank with a 50 bbl steel tank. Yesterday they had removed all of the material from inside the dike and hauled it off location and had begun spreading new limestone gravel in and outside of the dike. The field crew also spread Black River High Calcium Hydrated Lime on all of the areas outside of the dike. Jody Jasper stated they were going to try and correct the line across the stream today as well.
1424186606 2015-02-17 Production Wells No Violations Compliance follow-up -1273868557: I arrived to find that the rest of the gravel has been spread and the new tank is in place and is set up to be used for storing brine. There are several inches of snow on the ground therefore it makes it difficult to review the area outside of the dike. I will continue to monitor this location.
1440672697 2014-03-28 Production Wells No Violations Compliance Follow-up -1273868557: Andy has cleaned up the contamination from around the wellhead. Once the weather dries out the ground he will begin work on the flow and electric lines.
29116408 2014-3-21 0:00: PW No Violations 4.50
506240713 2015-2-9 0:00:0 PW No Violations 1.50
692506244 2014-12-23 0:00 PW No Violations 0.80
891078853 2015-3-10 0:00: PW No Violations 0.80
PL9411 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0506240713 US-OH-125524 2015-07-20 Well operation causing pollution and contamination
1273868557 US-OH-107608 2015-07-20 Well operation causing pollution and contamination
1273868557 US-OH-107609 2015-07-20 General Safety
1273868557 US-OH-107610 2015-07-20 Equipment pressure rated below operating pressure

For data sources see[9]

References