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Well ID: 34-115-23847 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Deerfield Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: DINGEY | |
License Status: Producing | |
License Date: 1985-05-08 | |
Spud Date: 1985-08-28 | |
Spud Drilling Contractor: DUSTY DRILLING | |
Final Drill Date: 1985-09-17 | |
Well Total Depth: 1372.00 ft | |
Configuration: Vertical | |
Latitude: 39.660000 | |
Longitude: -81.940000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1985-05-08 | Issued Date 5/8/85 Expired Date 11/4/85 Acres 0010000 Tool Type CT Proposed Formation BEREA Proposed Depth 01372 Proposed Drill Depth 01372 |
Original Spud | 1985-08-28 | |
Completed | 1985-09-17 | |
Reached Total Depth | 1985-09-17 | |
CO | 1985-10-04 | 1868 DUSTY DRILL & PRO CORP GeoDate 5/8/85 |
Completion Report Received | 1985-10-21 | |
Construction Permit Expires | 1985-11-04 | |
Change of Owner | 2003-09-24 | Operator changed from 1868, DUSTY DRILL & PRO CORP to 2867, DNL OIL CORP |
Change of Owner | 2007-07-11 | Operator changed from 2867, DNL OIL CORP to 8227, DEEP RESOURCES LLC |
Change of Owner | 2011-10-13 | Operator changed from 8227, DEEP RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 1322 | 1340 | 0 |
1322 | 1340 | 0 | |
2006-09-11 | 1336 | 1338 | 1 |
1336 | 1338 | 1 | |
1322 | 1340 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1025 Bbl | 20000 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | DUSTY DRILLING & PRODUCING COR | 179.00 | 341.00 | 182 |
1986 | DUSTY DRILLING & PRODUCING COR | 1292.00 | 648.00 | 365 |
1987 | DUSTY DRILLING & PRODUCING COR | 710.00 | 232.00 | 365 |
1988 | DUSTY DRILLING & PRODUCING COR | 672.00 | 209.00 | 323 |
1989 | DUSTY DRILLING & PRODUCING COR | 652.00 | 109.00 | 330 |
1990 | DUSTY DRILLING & PRODUCING COR | 601.00 | 117.00 | 351 |
1991 | DUSTY DRILLING & PRODUCING COR | 675.00 | 179.00 | 351 |
1992 | DUSTY DRILLING & PRODUCING COR | 747.00 | 119.00 | 365 |
1994 | DUSTY DRILLING & PRODUCING COR | 696.00 | 186.00 | 365 |
1995 | DUSTY DRILLING & PRODUCING COR | 37.00 | 176.00 | 365 |
2005 | DNL OIL CORP | 619.00 | 147.00 | 365 |
2006 | DNL OIL CORP | 595.00 | 145.00 | 365 |
2007 | DNL OIL CORP | 72.00 | 62.00 | 183 |
2010 | DEEP RESOURCES LLC | 154.00 | 157.00 | 365 |
2011 | DEEP RESOURCES LLC | 134.00 | 38.00 | 90 |
2012 | M & R INVESTMENTS OHIO LLC | 70.00 | 0.00 | 366 |
2013 | M & R INVESTMENTS OHIO LLC | 0.00 | 64.00 | 365 |
2014 | M & R INVESTMENTS OHIO LLC | 0.00 | 140.00 | 365 |
2015 | M & R INVESTMENTS OHIO LLC | 10.00 | 0.00 | 365 |
2016 | M & R INVESTMENTS OHIO LLC | 10.00 | 0.00 | 0 |
2017 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1154157541 | 2015-5-20 0:00: | PW | No Violations | 1.00 |
-1273868557 | 2014-2-27 0:00: | PW | No Violations | 2.80 |
-1440672697 | 2014-3-28 0:00: | PW | No Violations | 1.30 |
0000PL9411 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0029116408 | 2014-03-21 | Production Wells | No Violations | Compliance Follow-up -1273868557: The pumpjack horse head and bridle have been re-attached to the pumpjack and Andy Corp has repaired the stuffing box. Andy will have the contamination cleaned up by next Thursday and will restore vegetative growth in the next few months. |
0506240713 | 2015-02-09 | Production Wells | Violations Noted | Upon inspection, I found that the 1500 gallon tank was full and leaking in several areas. There were signs that the dike was holding brine. There is evidence of brine outside of the dike around the drain pipe. Quantabs revealed over 600 ppm of chlorides all around the outside and inside of the dike. I called and left messages with field supervisor, Jody Jasper, and Manager Rusty Hutson. I talked to well tender, Andy Corp and explained the issues. Operator needs to remove leaking tank and all contamination in and outside of the dike. |
0692506244 | 2014-12-23 | Production Wells | No Violations | Compliance Follow-up -1273868557: Andy Corp, of M & R, has replaced the flow line and secured it up above the stream in one area but has yet to do the same to the area that had the main concern. The original issues concerning the electric and flow lines tangled up and lying in the streams still has no resolution. Andy said he would finish the job this week. |
0891078853 | 2015-03-10 | Production Wells | No Violations | Compliance follow-up -1273868557: Operator has removed the flow line from the creekbed and chained it to a tree. They have also severed the electric line but there are no signs they have reconnected it anywhere else. |
1154157541 | 2015-05-20 | Production Wells | No Violations | I was at this well to do a follow-up inspection on it. The violations have been resolved at this time. The well is in production and there are no violations. |
1273868557 | 2014-02-27 | Production Wells | Violations Noted | I met the landowner Jim Flynn out at his property to inspect three wells. This well is equipped with a pumpjack with it head disconnected and laying on the ground. It was still attached to the rods. There is contamination from the stuffing box all around the wellhead. The valves were open and the landowner stated Andy Corp was out there in October repairing the leaking stuffing box. The flow line and electric line run through the creek down below and both are exposed in the water and in danger of breaking from debris. I talked with the field supervisor Jody Jasper and he said they would get on all of these problems this week. Operator must remove and properly dispose of all contamination and repair or replace any faulty equipment. |
1415229812 | 2014-11-05 | Production Wells | No Violations | Compliance Follow-up -1273868557: I was on location with Diversified/M & R Investments field manager, Rusty Hutson. He stated that they will order two rolls of plastic flow line to replace and re-route the old, bent lines in the stream. They will also re-route the electric line. |
1423758806 | 2015-02-12 | Production Wells | No Violations | Compliance follow-up -1273868557: I was on location to witness operator replace the plastic tank with a 50 bbl steel tank. Yesterday they had removed all of the material from inside the dike and hauled it off location and had begun spreading new limestone gravel in and outside of the dike. The field crew also spread Black River High Calcium Hydrated Lime on all of the areas outside of the dike. Jody Jasper stated they were going to try and correct the line across the stream today as well. |
1424186606 | 2015-02-17 | Production Wells | No Violations | Compliance follow-up -1273868557: I arrived to find that the rest of the gravel has been spread and the new tank is in place and is set up to be used for storing brine. There are several inches of snow on the ground therefore it makes it difficult to review the area outside of the dike. I will continue to monitor this location. |
1440672697 | 2014-03-28 | Production Wells | No Violations | Compliance Follow-up -1273868557: Andy has cleaned up the contamination from around the wellhead. Once the weather dries out the ground he will begin work on the flow and electric lines. |
29116408 | 2014-3-21 0:00: | PW | No Violations | 4.50 |
506240713 | 2015-2-9 0:00:0 | PW | No Violations | 1.50 |
692506244 | 2014-12-23 0:00 | PW | No Violations | 0.80 |
891078853 | 2015-3-10 0:00: | PW | No Violations | 0.80 |
PL9411 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0506240713 | US-OH-125524 | 2015-07-20 | Well operation causing pollution and contamination | |
1273868557 | US-OH-107608 | 2015-07-20 | Well operation causing pollution and contamination | |
1273868557 | US-OH-107609 | 2015-07-20 | General Safety | |
1273868557 | US-OH-107610 | 2015-07-20 | Equipment pressure rated below operating pressure |
For data sources see[9]