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Well ID: 34-115-23857 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Deerfield Township | |
Operator Name: TEMPLE OIL & GAS CO | |
Well Pad ID: | |
Farm/Lease Name: WEAVER JAMES | |
License Status: Producing | |
License Date: 2008-04-24 | |
Spud Date: 1985-09-13 | |
Spud Drilling Contractor: TEMPLE OIL & GAS | |
Final Drill Date: 1985-11-04 | |
Well Total Depth: 4118.00 ft | |
Configuration: Vertical | |
Latitude: 39.720000 | |
Longitude: -82.010000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-07-03 | 79 OXFORD OIL CO GeoDate 7/3/85 |
Oil and Gas | 1985-07-03 | Issued Date 7/3/85 Expired Date 12/30/85 Acres 0185000 Tool Type CT Proposed Formation CLINTON Proposed Depth 04118 Proposed Drill Depth 04118 |
Original Spud | 1985-09-13 | |
Completed | 1985-11-04 | |
Reached Total Depth | 1985-11-04 | |
Completion Report Received | 1985-11-12 | |
Unknown | 1997-04-14 | Issued Date 4/14/97 Expired Date 4/14/98 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Change of Owner | 1997-06-23 | Operator changed from 79, OXFORD OIL CO to 384, TEMPLE OIL & GAS CO |
APP | 2008-04-24 | Proposed Formations:BEREA, Issued Date:4/24/2008, Expired Date:4/24/2009 6:00:00 AM, Drilling unit acres:185, Proposed Well Type:HAD, Proposed Well Class:POOL |
Construction Permit Expires | 2009-04-24 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4001 | 4026 | 0 |
4001 | 4026 | 0 | |
2006-09-11 | 4002 | 4026 | 22 |
4002 | 4026 | 22 | |
4001 | 4026 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1476 Bbl | 14000 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | TEMPLE OIL & GAS CO | 0.00 | 0.00 | 0 |
1987 | TEMPLE OIL & GAS CO | 24919.00 | 0.00 | 365 |
1990 | TEMPLE OIL & GAS CO | 20981.00 | 0.00 | 365 |
1992 | OXFORD OIL | 7514.00 | 0.00 | 365 |
1993 | OXFORD OIL | 5408.00 | 0.00 | 365 |
1994 | OXFORD OIL | 2317.00 | 0.00 | 365 |
1995 | OXFORD OIL | 1551.00 | 13.00 | 365 |
1996 | OXFORD OIL | 171.00 | 0.00 | 366 |
1997 | OXFORD OIL | 111.00 | 0.00 | 163 |
1998 | TEMPLE OIL & GAS CO | 232.00 | 0.00 | 241 |
1999 | TEMPLE OIL & GAS CO | 241.00 | 0.00 | 243 |
2000 | TEMPLE OIL & GAS CO | 320.00 | 0.00 | 261 |
2001 | TEMPLE OIL & GAS CO | 310.00 | 0.00 | 337 |
2002 | TEMPLE OIL & GAS CO | 106.00 | 0.00 | 257 |
2003 | TEMPLE OIL & GAS CO | 139.00 | 0.00 | 365 |
2004 | TEMPLE OIL & GAS CO | 147.00 | 0.00 | 253 |
2005 | TEMPLE OIL & GAS CO | 116.00 | 0.00 | 261 |
2006 | TEMPLE OIL & GAS CO | 48.00 | 0.00 | 244 |
2007 | TEMPLE OIL & GAS CO | 79.00 | 0.00 | 313 |
2008 | TEMPLE OIL & GAS CO | 36.00 | 0.00 | 365 |
2009 | TEMPLE OIL & GAS CO | 97.00 | 0.00 | 261 |
2010 | TEMPLE OIL & GAS CO | 70.00 | 0.00 | 313 |
2011 | TEMPLE OIL & GAS CO | 0.00 | 205.00 | 365 |
2012 | TEMPLE OIL & GAS CO | 0.00 | 0.00 | 366 |
2013 | TEMPLE OIL & GAS CO | 86.00 | 0.00 | 365 |
2014 | TEMPLE OIL & GAS CO | 1.00 | 0.00 | 365 |
2015 | TEMPLE OIL & GAS CO | 56.00 | 0.00 | 365 |
2016 | TEMPLE OIL & GAS CO | 14.00 | 0.00 | 365 |
2017 | TEMPLE OIL & GAS CO | 91.00 | 0.00 | 365 |
2018 | TEMPLE OIL & GAS CO | 3.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | TEMPLE OIL & GAS CO | Brine | 0 | 0 |
1987 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
1990 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
1992 | OXFORD OIL | Brine | 225 | 365 |
1993 | OXFORD OIL | Brine | 293 | 365 |
1994 | OXFORD OIL | Brine | 145 | 365 |
1995 | OXFORD OIL | Brine | 118 | 365 |
1996 | OXFORD OIL | Brine | 0 | 366 |
1997 | OXFORD OIL | Brine | 0 | 163 |
1998 | TEMPLE OIL & GAS CO | Brine | 83 | 241 |
1999 | TEMPLE OIL & GAS CO | Brine | 100 | 243 |
2000 | TEMPLE OIL & GAS CO | Brine | 265 | 261 |
2001 | TEMPLE OIL & GAS CO | Brine | 0 | 337 |
2002 | TEMPLE OIL & GAS CO | Brine | 0 | 257 |
2003 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
2004 | TEMPLE OIL & GAS CO | Brine | 0 | 253 |
2005 | TEMPLE OIL & GAS CO | Brine | 0 | 261 |
2006 | TEMPLE OIL & GAS CO | Brine | 0 | 244 |
2007 | TEMPLE OIL & GAS CO | Brine | 0 | 313 |
2008 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
2009 | TEMPLE OIL & GAS CO | Brine | 0 | 261 |
2010 | TEMPLE OIL & GAS CO | Brine | 0 | 313 |
2011 | TEMPLE OIL & GAS CO | Brine | 1092 | 365 |
2012 | TEMPLE OIL & GAS CO | Brine | 0 | 366 |
2013 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
2014 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
2015 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
2016 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
2017 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
2018 | TEMPLE OIL & GAS CO | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1014631995 | 2017-7-11 0:00: | PW | No Violations | 1.00 |
-181859232 | 2015-12-30 0:00 | PW | No Violations | 2.00 |
-1984526856 | 2016-6-20 0:00: | PW | No Violations | 1.00 |
-2136108203 | 2020-2-19 0:00: | PW | No Violations | 1.00 |
-380797446 | 2009-4-24 0:00: | PB | No Violations | |
0000PL9405 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0181859232 | 2015-12-30 | Production Wells | No Violations | Follow up on previous NOV found that nothing had been done to comply with the notice issued. Well still had no conspicuous ID posted, the lease road was still eroded/washed out and the production records submitted to the State of Ohio are still below the minimum requirements set for a well to stay in production. |
0283781083 | 2015-10-05 | Production Wells | Violations Noted | The lease road in a low spot was eroded or washed out. There was no identification posted at the well site. Valves were open and production line connected to the well via a 4x2 swedge nipple.
Lease road shall be restored and culvert put in if necessary to prevent future erosion. Proper Identification shall be posted at the well head. Production records submitted to the State for this well are less than the State minimum requirement for a well to stay in production. Land owner met me at my truck and is concerned with multiple wells feeding into one meter. |
0380797446 | 2009-04-24 | Plug / Plug Back | No Violations | PLUGBACK PERMIT EXPIRED 4/24/09. |
1014631995 | 2017-07-11 | Production Wells | No Violations | I was on location today to do a follow-up inspection on this well today. Both violations have been corrected and the well is now incompliance. The well is no longer in violation. |
1301673029 | 2016-05-11 | Production Wells | No Violations | Upon my inspection today I found there to be no resolution to any of the issues at the time. Compliance ha not been resolved. |
1984526856 | 2016-06-20 | Production Wells | No Violations | Upon my inpection I found this well to have production reports to be up to date and prodction to have been reported. The well is capable of production and is in compliance at this time. The lease road is still eroded away and is still a safety hazard at the time of inspection. |
283781083 | 2015-10-5 0:00: | PW | No Violations | 2.50 |
PL9405 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0283781083 | US-OH-122941 | 2015-10-26 | General Safety | |
0283781083 | US-OH-122942 | 2015-10-26 | Failure to legibly identify well | |
0283781083 | US-OH-122943 | 2015-10-26 | Statement of annual production not filed |
For data sources see[9]