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34-115-23869

Well Details

Well ID: 34-115-23869
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Country: United States
State: Ohio
County: Morgan
Municipality: Center Township
Operator Name: BANCEQUITY PETROLEUM CORPORATI
Well Pad ID:
Farm/Lease Name: HUPP
License Status: Final Restoration
License Date: 2007-07-11
Spud Date: 1989-11-20
Spud Drilling Contractor: R WOLFE DRLG
Final Drill Date: 1989-11-21
Well Total Depth: 1875.00 ft
Configuration: Vertical
Latitude: 39.600000
Longitude: -81.600000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Change of Owner 1985-10-18 500 SHANAHAN DONALD P GeoDate 10/18/85
CO 1985-10-18 500 SHANAHAN DONALD P GeoDate 10/18/85
Oil and Gas 1985-10-18 Issued Date 10/18/85 Expired Date 10/18/86 Acres 0010000 Tool Type CRAF Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000
Change of Owner 1989-11-09 500 SHANAHAN DONALD P GeoDate 11/9/89
CO 1989-11-09 500 SHANAHAN DONALD P GeoDate 11/9/89
Oil and Gas 1989-11-09 Issued Date 11/9/89 Expired Date 11/9/90 Acres 0010000 Tool Type CRAF Proposed Formation BEREA Proposed Depth 01875 Proposed Drill Depth 01875
Original Spud 1989-11-20 R.I. 11-11-89 PERMIT EXPIRED.
Completed 1989-11-21 R.I. 11-11-89 PERMIT EXPIRED.
Reached Total Depth 1989-11-21 R.I. 11-11-89 PERMIT EXPIRED.
Completion Report Received 1990-01-18 R.I. 11-11-89 PERMIT EXPIRED.
CO 1991-12-13 28 CGAS EXPLORATION,INC GeoDate 11/9/89
Change of Owner 1999-04-30 Operator changed from 28, CGAS EXPLORATION to 4801, BANCEQUITY PETROLEUM CORP
APP 2007-07-11 4801 BANCEQUITY PETROLEUM CORP Proposed Formation BEREA Issued Date 7/11/2007 Expired Date 7/10/2008 6:00:00 AM
Plugged/Abandoned 2008-05-08 R.I. 11-11-89 PERMIT EXPIRED.
Construction Permit Expires 2008-07-10 R.I. 11-11-89 PERMIT EXPIRED.
Record Last Modified 2017-02-15 R.I. 11-11-89 PERMIT EXPIRED.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1795 1814 0
1795 1814 0
2006-09-11 1796 1799 6
1796 1799 6
1795 1814 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 600 Bbl 20000 FRAC:WATER/SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1990 SHANAHAN DONALD P 126.00 0.00 365
1992 CGAS EXPLORATION 586.00 0.00 366
1995 CGAS EXPLORATION 0.00 0.00 365
1996 CGAS EXPLORATION 0.00 0.00 365
1997 CGAS EXPLORATION 0.00 0.00 365
1998 CGAS EXPLORATION 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1990 SHANAHAN DONALD P Brine 0 365
1992 CGAS EXPLORATION Brine 140 366
1995 CGAS EXPLORATION Brine 0 365
1996 CGAS EXPLORATION Brine 0 365
1997 CGAS EXPLORATION Brine 0 365
1998 CGAS EXPLORATION Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL9399 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0457223080 2006-11-16 Production Wells Violations Noted Well has been placed back into production resolving previous NOV.
0933492392 2006-07-27 Production Wells Violations Noted No change in status of well(still idle)called and left messages with company with no response.

Recommend Chiefs Order to plug said well and also place company on permit hold list.

1146321984 2006-04-27 Production Wells Violations Noted Upon receiving complaint of idle well on property by Alva Heiss found well to be idle,well is equipped with 7 4.5 casing 2 tubing&rods,pump jack has been removed and all valves@wellhead are shut no I.D. posted,last production reported on well was back in 1998.Photos taken.
1159046918 2006-09-21 Production Wells No Violations Upon inspecting well site for compliance too previous NOV,found operator has placed pumping unit on said well and is preparing to place well back into production.

Called well owner and discussed when he might get well into production he stated that well tender was buying motor for unit this week,also informed him that Icouldnt clear violations until wel was in production and properly IDed and dike constructed around tanks.

1210371232 2008-05-08 Production Wells Violations Noted Well has been plugged resolving previous NOV.
1220048623 2008-08-29 Final Restoration No Violations Final restoration work at site satisfactory,pit has been filled in and site restored, site currently has corn growing on it
457223080 2006-11-16 0:00 PW No Violations
933492392 2006-7-27 0:00: PW No Violations
PL9399 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0457223080 US-OH-124950 2006-04-29 Failure to legibly identify well
0457223080 US-OH-124951 2006-04-29 Well shall be plugged
0933492392 US-OH-130669 2006-04-29 Failure to legibly identify well
0933492392 US-OH-130670 2006-04-29 Well shall be plugged
1146321984 US-OH-103786 2006-04-29 Failure to legibly identify well
1146321984 US-OH-103787 2006-04-29 Well shall be plugged
1210371232 US-OH-105483 2006-04-29 Failure to legibly identify well
1210371232 US-OH-105484 2006-04-29 Well shall be plugged

For data sources see[9]

References