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| Well ID: 34-115-23875 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Washington | |
| Municipality: Waterford Township | |
| Operator Name: GENESIS RESOURCES LLC | |
| Well Pad ID: | |
| Farm/Lease Name: KUTSCHERENKO | |
| License Status: Producing | |
| License Date: 1985-11-01 | |
| Spud Date: 1985-11-17 | |
| Spud Drilling Contractor: PERKINS DRLG | |
| Final Drill Date: 1985-11-20 | |
| Well Total Depth: 5172.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.580000 | |
| Longitude: -81.700000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1985-11-01 | 471 EAGLE MOUNTAIN ENERGY GeoDate 11/1/85 |
| Oil and Gas | 1985-11-01 | Issued Date 11/1/85 Expired Date 11/1/86 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05172 Proposed Drill Depth 05172 |
| Original Spud | 1985-11-17 | LOG TYPE=QUICKLOOK |
| Completed | 1985-11-20 | LOG TYPE=QUICKLOOK |
| Reached Total Depth | 1985-11-20 | LOG TYPE=QUICKLOOK |
| Completion Report Received | 1985-12-10 | LOG TYPE=QUICKLOOK |
| Construction Permit Expires | 1986-11-01 | LOG TYPE=QUICKLOOK |
| CO | 1996-07-24 | 4801 BANCEQUITY PETROLEUM CORP GeoDate 11/1/85 |
| Last Compliance Report | 2012-04-14 | LOG TYPE=QUICKLOOK |
| Change of Owner | 2018-05-04 | Operator changed from 4801, BANCEQUITY PETROLEUM CORP to 9086, GENESIS RESOURCES LLC |
| Record Last Modified | 2018-05-04 | LOG TYPE=QUICKLOOK |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 4910 | 5002 | 0 |
| 4910 | 5002 | 0 | |
| 2006-09-11 | 4972 | 5059 | 30 |
| 4972 | 5059 | 30 | |
| 4910 | 5002 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| GEL | 0 | 80000 Gal | 90000 | FRAC: H2O,SAND,CO2 | ||
| CO2 | 0 | 20 Tons | 0 |
For data sources see[4]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1242525956 | 2006-3-31 0:00: | AD | No Violations | |
| -1560449868 | 2015-12-28 0:00 | PW | No Violations | 1.00 |
| -81149378 | 2017-3-1 0:00:0 | PW | No Violations | 1.00 |
| 0000PL9394 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0081149378 | 2017-03-01 | Production Wells | No Violations | The inspection this day revealed that this well is equipped with a plunger lift system, a 4 1/2 inch diameter wellhead, and 1 1/2 inch diameter production tubing. The valves on the wellhead are open at the time of inspection. The tank battery for this well is equipped with a 100 barrel steel tank and a horizontal separator. There are no issues to report at this time and this well is in production at the time of inspection. |
| 0256885615 | 2003-05-19 | Production Wells | No Violations | well was recently put back into production,all production equiptment in place.
600psi on tubing on the day of my inspection. |
| 0625954772 | 2011-12-08 | Production Wells | No Violations | Inspection this day found well is equipped with a plunger lift system and in production. The tank battery needs proper identification posted and repairs made to the dike. I will notify the pumper of these issues. Annual production records are current in the DNR database. |
| 1242525956 | 2006-03-31 | Annular Disposal | No Violations | A.D. not in use,well is equipped with 4.5casing and 2.875 tubing with packer in place small amount of H2S odor detected,1-100 bbl,separator will need dike work preformed when SPCC rules go into effect. |
| 1523278123 | 2018-04-09 | Temporary Abandoned Annular Disposal | No Violations | I was on location today to check the annular disposal for Columbus. The annular disposal is not hooked up on this well. |
| 1560449868 | 2015-12-28 | Production Wells | No Violations | On my inspection today I found this well to be a rabbit well equipped with a 4 1/2 inch well head and 2 inch tubing equipped with 2 inch ball valves. The tank battery is equipped with a compressor station and one 100 bbl tank. Upon my inspection it appeared that the well head had been shut in at the valves and that H2S might be possibly leaking from it. I called Traci the pumper and he informed me that the valves were only pinched in but were still slightly open which I can confirm as I heard fluid moving through the pipes. He said the slight H2S smell was sulfur prep that they put down the hole to try to control the H2S from leaking out and getting to be too much. I could only smell the H2S when I was right up to the pipes and I heard no leaking sounds. No violations to report at this time and well is in production. |
| 256885615 | 2003-5-19 0:00: | PW | No Violations | |
| 625954772 | 2011-12-8 0:00: | PW | No Violations | 0.50 |
| PL9394 | PL | No Violations |
For data sources see[9]