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Well ID: 34-115-24076 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Deerfield Township | |
Operator Name: J V ALTIER GAS & OIL INC | |
Well Pad ID: | |
Farm/Lease Name: HIVNOR RAYMOND & GLENNA | |
License Status: Producing | |
License Date: 1988-01-25 | |
Spud Date: 1988-02-25 | |
Spud Drilling Contractor: R WOLFE DRLG | |
Final Drill Date: 1988-02-26 | |
Well Total Depth: 1565.00 ft | |
Configuration: Vertical | |
Latitude: 39.710000 | |
Longitude: -81.920000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1988-01-25 | Issued Date 1/25/88 Expired Date 1/24/89 Acres 0023000 Tool Type RTA Proposed Formation BEREA Proposed Depth 01565 Proposed Drill Depth 01565 |
Original Spud | 1988-02-25 | PF=1ST BEREA |
Completed | 1988-02-26 | PF=1ST BEREA |
Reached Total Depth | 1988-02-26 | PF=1ST BEREA |
CO | 1988-05-10 | 302 STEWART DRILLING CO. INC GeoDate 1/25/88 |
Construction Permit Expires | 1989-01-24 | PF=1ST BEREA |
Completion Report Received | 1990-07-12 | PF=1ST BEREA |
CO | 1992-02-03 | 4074 OIL ENTERPRISES GeoDate 1/25/88 |
Change of Owner | 1998-04-16 | Operator changed from 4074, OIL ENTERPRISES to 1868, DUSTY DRILL & PRO CORP |
Change of Owner | 2010-07-22 | Operator changed from 1868, DUSTY DRILL & PRO CORP to 482, ALTIER J V GAS & OIL |
Last Compliance Report | 2013-10-09 | PF=1ST BEREA |
Record Last Modified | 2017-02-15 | PF=1ST BEREA |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 1439 | 1463 | 0 |
1439 | 1463 | 0 | |
2006-09-11 | 1454 | 1461 | 8 |
1454 | 1461 | 8 | |
1439 | 1463 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 809 Bbl | 20000 | FRAC:WATER/SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | STEWART DRILLING CO. INC | 1660.00 | 1614.00 | 194 |
1989 | STEWART DRILLING CO. INC | 3704.00 | 1324.00 | 365 |
1990 | STEWART DRILLING CO. INC | 3762.00 | 1200.00 | 365 |
1993 | OIL ENTERPRISES | 2506.00 | 0.00 | 365 |
1994 | OIL ENTERPRISES | 2029.00 | 386.00 | 365 |
1995 | OIL ENTERPRISES | 1420.00 | 216.00 | 365 |
1996 | OIL ENTERPRISES | 0.00 | 0.00 | 0 |
1998 | OIL ENTERPRISES | 0.00 | 0.00 | 0 |
2001 | J V ALTIER GAS & OIL INC | 1083.00 | 152.00 | 365 |
2002 | J V ALTIER GAS & OIL INC | 1291.00 | 327.00 | 290 |
2003 | J V ALTIER GAS & OIL INC | 988.00 | 210.00 | 275 |
2004 | J V ALTIER GAS & OIL INC | 1084.00 | 298.00 | 290 |
2005 | J V ALTIER GAS & OIL INC | 497.00 | 204.00 | 311 |
2006 | J V ALTIER GAS & OIL INC | 575.00 | 503.00 | 326 |
2007 | J V ALTIER GAS & OIL INC | 605.00 | 453.00 | 331 |
2008 | J V ALTIER GAS & OIL INC | 724.00 | 368.00 | 360 |
2009 | J V ALTIER GAS & OIL INC | 666.00 | 442.00 | 365 |
2010 | J V ALTIER GAS & OIL INC | 2134.00 | 432.00 | 365 |
2011 | J V ALTIER GAS & OIL INC | 996.00 | 153.00 | 365 |
2012 | J V ALTIER GAS & OIL INC | 665.00 | 202.00 | 366 |
2013 | J V ALTIER GAS & OIL INC | 417.00 | 217.00 | 365 |
2014 | J V ALTIER GAS & OIL INC | 380.00 | 146.00 | 365 |
2015 | J V ALTIER GAS & OIL INC | 297.00 | 103.00 | 365 |
2016 | J V ALTIER GAS & OIL INC | 293.00 | 230.00 | 365 |
2017 | J V ALTIER GAS & OIL INC | 315.00 | 191.00 | 365 |
2018 | J V ALTIER GAS & OIL INC | 342.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1075278129 | 2019-6-5 0:00:0 | PW | No Violations | 1.00 |
-114238751 | 2020-5-21 0:00: | PW | No Violations | |
-1262785125 | 2012-10-10 0:00 | PW | No Violations | 1.00 |
-127798218 | 2018-5-25 0:00: | TD | No Violations | 0.50 |
-151702270 | 2013-7-3 0:00:0 | PW | No Violations | 1.00 |
-1672813555 | 2008-5-2 0:00:0 | AD | No Violations | |
-1796271004 | 2019-6-18 0:00: | PW | No Violations | 0.60 |
-2099781883 | 2009-11-17 0:00 | AD | No Violations | |
-2131216568 | 2013-6-12 0:00: | PW | No Violations | 2.50 |
-2131253285 | 2004-3-2 0:00:0 | PW | No Violations | 3.00 |
-223977329 | 2012-10-10 0:00 | PW | No Violations | 3.00 |
-463516732 | 2019-6-25 0:00: | PW | No Violations | 0.50 |
-548047134 | 2013-8-30 0:00: | AM | No Violations | |
-637492555 | 2015-8-24 0:00: | PW | No Violations | 0.50 |
-712113106 | 2019-6-17 0:00: | PW | No Violations | 1.00 |
0000PL9282 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0127798218 | 2018-05-25 | Temporary Abandoned Annular Disposal | No Violations | I was on location today to check the annular disposal for Columbus. The annular disposal is not hooked up on this well. |
0151702270 | 2013-07-03 | Production Wells | No Violations | Joe Altier has asked me to come out to the tank battery to witness that he has replaced the leaking nipple. I arrived on location and found that he has in fact replaced the nipple and replumbed the lines to the plastic tank underneath the knock out tank. There are no other issues at this time. |
0223977329 | 2012-10-10 | Production Wells | No Violations | I accompanied Cindy VanDyke on the inspection of well. Well is capable of producing and there is a current chart in the meter. There were 2//100 barrel tanks and a 25 barrel separator above a plastic water tank. ID was posted on tank and dike is in good condition. |
0319664747 | 2015-03-16 | Administrative Inspection | No Violations | Joe Altier and Debbie Hivnor both called today and stated there was a small leak from a bad union and a heater tube on one of the tanks. He has his well tender out on location repairing the issues this morning. |
0533072304 | 2009-07-08 | Annular Disposal | No Violations | Follow-up on NOV, In-Compliance, company not using water knock out, has been unhooked. |
0548047134 | 2013-08-30 | Administrative Inspection | No Violations | Joe Altier called me and said they changed out the tank and contamination. The replaced the gravel with fresh stone. I will head out next week to check the location. |
0598822018 | 2011-04-26 | Production Wells | No Violations | Inspection this day found well producing with jack, tank has good IDs, good dike, current chart in meter. Looks very nice. |
0610655976 | 2015-02-09 | Production Wells | No Violations | This was a tank battery inspection. There are no issues to report at this time. |
0637492555 | 2015-08-24 | Production Wells | No Violations | This well is equipped with an electric motor powered pump jack. Two 100 bbl. tanks, one vertical separator, one salt water knockout, and one 250 gallon brine poly tank. The well was properly identified with the identification located on the tank. No violations at the time of inspection. |
0818118948 | 2012-08-01 | Production Wells | No Violations | I received call from Debbie Hivnor at 6:30 AM on 7/30 that Joe had released brine inside the dike area - said they had called him after discovering it at 10 PM - he said he would be out in morning. Also stated that there was still an oily spot down in woods from his last oil spill. I called Joe and he said they had been out and flushed brine with clean water and removed from inside dike. Very little - less than a bbl - had spilled out of tank. Joe said he had a trac-hoe coming on Wed. to finish laying the new flowline that he continues to have leaks in. He had received information for couplers that stop the corrosion that is causing his leaks. Joe plans to have line replaced and restoration done by the end of the week. He plans to removed contaminated soil, seed, mulch and fertilize the area in question and remove all brine from inside the dike. No violation wrote at this time but instructed Joe what to do. |
1144738512 | 2019-06-05 | Production Wells | Violations Noted | I was on location this morning after receiving a phone call from landowner Debbie Hivnor last night stating that the well had oil around it on the ground and was covered up with fresh gravel instead of removed from location. Debbie also stated that she put some absorbent on it because it is suppose to rain and she does not want it to get in her spring. When I got to the well I saw the absorbent she put down and I could see the oil coming through the fresh gravel. The company will need to remove all contaminated soil from location. |
1262785125 | 2012-10-10 | Production Wells | No Violations | My inspection this day with Jake Glascock to show him well, inform him of the numerous complaints he may receive. I gave Jake a history of the problems and we did a visual inspection of the recent reclamation, finding it satisfactory. The tank battery looked satisfactory and found no violations. |
1325071346 | 2013-08-06 | Production Wells | No Violations | Debbie Hivnor called and said she believes the tank is leaking from the bottom. She said they have been digging away the gravel from under the nipple and it accumulates water. It had just rained so it was hard to tell if it was from the tank. I called Joe and he stated they have shut in well and recorded the levels and found no loss in the fluid. Joe does not believe the tank is leaking and we will have to wait until there is a long period of dry weather in order to tell if there is an issue. |
1344366223 | 2012-08-06 | Production Wells | No Violations | My inspection this day with Joe Altier found area with brine and oil kill has been reclaimed - contaminated soil removed, Joe says - smoothed ground seeded, fertilized, and mulched - good rain the last day or 2 and should be sprouting very soon. Joe has replaced the steel flowline with plastic and corrosion inhibitor couplings and this should prevent any further problems. The dike area was inspected and, due to rains the night before, was found to contain fresh rain water - was no indication of brine and Joe and I discussed the possibility that the hose could have popped out of the hole in the top and released brine inside the dike area. The hose is now tied down and cant possiby slip out. Joe opened valve on outside of dike and drained the inside of the fresh water. Identification is complete. All violations have been resolved. |
1346358722 | 2012-08-30 | Production Wells | No Violations | I received a complaint from Debbie Hivnor that grass has not grown back where Joey had reseeded and that there were still bare patches. I went out and looked with Joey Altier and found there were a couple 2 squares of ground that still did not have a sufficient stand of grass - the big majority of it did. Considering that he only reseeded about 3 weeks ago and that we did not have rain until the last week, I felt it looked very good. I know that if another month passed, all the ground would be covered. Joe said he would go ahead and put more seed down in those patches and also address another area where she felt was too bare. This 2nd spot is where her cows root around and is understandable that grass has trouble growing. Joe said he would also plant more there. I called Debbie and told her that while I did not see a problem with the reclamation the way it was and that if she had waited a month, it would be taken care of, that Joe was going to re-seed the areas for her. |
1367765004 | 2013-05-05 | Production Wells | Violations Noted | Well equipped with a pumping unit with electric motor. The stuffing box had developed a leak and released a small amount of crude oil at the well head. The tank battery was equipped with two 100 barrel (Bbl) steel tanks, a 30 Bbl water knock-out not in use, a separator, and a 100 gallon poly tank being used for the annular disposal on another well on the lease. This well is not set up for annular disposal. The nipple on one of the 100 Bbl tanks had corroded and allowed a small amount of salt water to leach into the dike. There was a band clamp temporarily wrapped around the nipple. The dike was equipped with a drain to release fresh water. There was no sign of contaminated soils near the end of the drain outside of the dike. The water in the dike was field tested with a Quan-tab and found to have greater than 6508 ppm Chloride content. All leaking equipment shall be repaired or replaced. Any contaminated soils shall be removed, and disposed of properly. |
1369842852 | 2013-05-29 | Production Wells | No Violations | The stuffing box has been repaired and the operator cleaned up the oil contamination. Well is in compliance. |
1377539066 | 2013-08-26 | Production Wells | No Violations | Alan Hivnor called and stated that the tank was leaking and he was concerned about his spring water. He said there was standing water in the dike. Upon inspection, I found a puddle with around a quart or less of brine water which appeared to be emanating from the bottom of the tank. I called Joe Altier and told him the only way to know for sure whether or not the brine source is from the tank or trapped in the dike gravel is to remove both. He said he would get a new tank and remove the contamination. |
1378322624 | 2013-09-04 | Production Wells | No Violations | Joe has cahnged out the tank, removed the old gravel, and replaced with new gravel. There are no issues at this time. |
1381801607 | 2008-05-01 | Production Wells | No Violations | Complaint received from Allen Hivnor @10:30 pm of oil within dike area at tank site located on his property, he claims that tank is leaking only when owner heats oil in preparation for shipping, inspected site and found small amount of oil residue located within dike area called well owner J.V. Altier and requested he meet me at site and discuss plans for possibly removing tank and replacing it with a new tank and also replacing stone that is located beneath present tank,decision was made to replace tank and stone at site owner stated job would be complete by 5/2/08.Photos taken of site 4. |
1556543123 | 2019-04-29 | Production Wells | No Violations | My inspection on this day revealed that the well has allowed oil to leak onto the ground surface and flow approximately 40 feet from the wellhead. The contamination was approximately 15 feet at its widest point just before it flowed over a bank where it then took a more narrow course for approximately 10 feet. The oil did not impact any bodies of water. The well was equipped with a pumping unit and motor. It was not pumping during the inspection. An observation of the pumping unit revealed that the pumping unit may need to be adjusted as the polish rod did not appear to be centered in the stuffing box. This may have caused the stuffing box to leak and allow oil to leak onto the ground. During my inspection I did not observe identification at the well or tank battery. I contacted the well owner Joey Altier during my inspection and advised him of the leak. Mr. Altier said he would have it cleaned up today. The well owner shall clean up oil within 5 days and post identification within 10 days. I took several photos during the inspection. Time of inspection: 8:30 AM. Weather: 44 degrees F, Sunny |
1561722442 | 2019-6-28 0:00: | PW | No Violations | 0.50 |
1672813555 | 2008-05-02 | Annular Disposal | No Violations | Upon inspecting tank site again for compliance of inspectors request too change out tank and removal of stone beneath tank,job was completed as requested!with no spillage of brine/oil within dike area. |
1978283313 | 2009-05-15 | Production Wells | Violations Noted | An inspection of the well revealed water knock out starting to leak in several places. Oily and brine materials will need cleaned up from water knock out leaking. Rob Stonerock and landowner along on inspection. |
2099781883 | 2009-11-17 | Annular Disposal | No Violations | Follow-up on NOV, In-Compliance. |
2131216568 | 2013-06-12 | Production Wells | No Violations | Mrs. Hivnor called and stated the nipple on the tank was leaking brine. When I arrived I found that there was a very small leak coming from the nipple which already had a clamp. Josh Garland was recently at location for the same complaint and had issued a compliance action. I told Joe Altier that they needed to repair or replace the equipment and clean up the contamination. I witnessed the well tender tighten the clamp and clean up the area. Joe said if the nipple still leaks he will replace the part. I will return in a few weeks for a follow-up inspection. |
2131253285 | 2004-03-02 | Production Wells | No Violations | Complaint called in by Deb HIV nor stated there was oil/brine within dike area wanted it cleaned up A.SA.P.arrived on location to meet with well owner Joe Artier to witness cleanup, dike area was flushed with fresh water and loaded in vacuum truck owned by Steve AltierUIC-154photos taken of before and after cleanup.Mr. Hivinor called @8:40 pm and stated approximatly 1qt. Of iol still remained within dike area wants it cleaned up .3-3-04 went by site and took additional photos of clean up. |
319664747 | 2015-3-16 0:00: | AM | No Violations | |
407284248 | 2019-6-11 0:00: | PW | No Violations | 0.70 |
533072304 | 2009-7-8 0:00:0 | AD | No Violations | |
598822018 | 2011-4-26 0:00: | PW | No Violations | 0.50 |
610655976 | 2015-2-9 0:00:0 | PW | No Violations | 0.80 |
818118948 | 2012-8-1 0:00:0 | PW | No Violations | 1.00 |
PL9282 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1144738512 | US-OH-103717 | 2019-06-10 | 9-1-07 | Well operation causing pollution and contamination |
1367765004 | US-OH-110840 | 2013-06-10 | Equipment pressure rated below operating pressure | |
1978283313 | US-OH-120006 | 2009-05-18 | Well operation causing pollution and contamination | |
1978283313 | US-OH-120007 | 2009-05-18 | Equipment pressure rated below operating pressure | |
1978283313 | US-OH-120008 | 2009-05-18 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[9]