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Well ID: 34-115-24247 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Deerfield Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: WOODARD J | |
License Status: Producing | |
License Date: 1997-09-18 | |
Spud Date: 1992-09-09 | |
Spud Drilling Contractor: UNGER DRILLING | |
Final Drill Date: 1992-09-13 | |
Well Total Depth: 4430.00 ft | |
Configuration: Vertical | |
Latitude: 39.640000 | |
Longitude: -81.990000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1992-01-06 | 2867 DNL OIL CORP GeoDate 1/6/92 |
Oil and Gas | 1992-01-06 | Issued Date 1/6/92 Expired Date 1/5/93 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04430 Proposed Drill Depth 04430 |
Original Spud | 1992-09-09 | |
Completed | 1992-09-13 | |
Reached Total Depth | 1992-09-13 | |
Completion Report Received | 1992-12-23 | |
Construction Permit Expires | 1993-01-05 | |
CO | 1994-11-25 | 1868 DUSTY DRILL & PRO CORP GeoDate 1/6/92 |
Annular Disposal Well | 1997-09-18 | |
Change of Owner | 2003-09-24 | Operator changed from 1868, DUSTY DRILL & PRO CORP to 2867, DNL OIL CORP |
Change of Owner | 2007-07-11 | Operator changed from 2867, DNL OIL CORP to 8227, DEEP RESOURCES LLC |
Revocation | 2008-06-01 | |
Change of Owner | 2011-10-13 | Operator changed from 8227, DEEP RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC |
Last Compliance Report | 2018-04-18 | |
Record Last Modified | 2018-04-18 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1998-02-13 | 4238 | 4248 | 20 |
4238 | 4248 | 20 | |
4238 | 4248 | 20 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1800 Bbl | 40000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1992 | DNL OIL CORP | 306.00 | 0.00 | 90 |
1993 | DNL OIL CORP | 39473.00 | 0.00 | 130 |
1994 | DUSTY DRILLING & PRODUCING COR | 36381.00 | 0.00 | 365 |
1995 | DUSTY DRILLING & PRODUCING COR | 26218.00 | 0.00 | 365 |
1996 | DUSTY DRILLING & PRODUCING COR | 23799.00 | 0.00 | 365 |
1997 | DUSTY DRILLING & PRODUCING COR | 22739.00 | 0.00 | 365 |
1998 | DUSTY DRILLING & PRODUCING COR | 23111.00 | 0.00 | 330 |
1999 | DUSTY DRILLING & PRODUCING COR | 24329.00 | 0.00 | 365 |
2000 | DUSTY DRILLING & PRODUCING COR | 17107.00 | 0.00 | 365 |
2001 | DUSTY DRILLING & PRODUCING COR | 20762.00 | 0.00 | 365 |
2002 | DUSTY DRILLING & PRODUCING COR | 21363.00 | 0.00 | 365 |
2003 | DUSTY DRILLING & PRODUCING COR | 20703.00 | 0.00 | 365 |
2004 | DNL OIL CORP | 18612.00 | 0.00 | 360 |
2005 | DNL OIL CORP | 13865.00 | 0.00 | 365 |
2006 | DNL OIL CORP | 12368.00 | 0.00 | 365 |
2007 | DEEP RESOURCES LLC | 2010.00 | 0.00 | 180 |
2008 | DEEP RESOURCES LLC | 1473.00 | 0.00 | 365 |
2009 | DEEP RESOURCES LLC | 8014.00 | 0.00 | 365 |
2010 | DEEP RESOURCES LLC | 15867.00 | 0.00 | 365 |
2011 | DEEP RESOURCES LLC | 8025.00 | 0.00 | 90 |
2012 | M & R INVESTMENTS OHIO LLC | 6916.00 | 0.00 | 366 |
2013 | M & R INVESTMENTS OHIO LLC | 10595.00 | 0.00 | 365 |
2014 | M & R INVESTMENTS OHIO LLC | 1063.00 | 0.00 | 365 |
2015 | M & R INVESTMENTS OHIO LLC | 1818.00 | 0.00 | 365 |
2016 | M & R INVESTMENTS OHIO LLC | 5.00 | 0.00 | 365 |
2017 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-318364231 | 2013-1-28 0:00: | AD | No Violations | |
-482919837 | 2018-3-22 0:00: | TD | No Violations | 0.50 |
-848497577 | 2011-10-28 0:00 | PW | No Violations | 0.50 |
0000000882 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 11/6/92 INSPECTOR TED DOBBIN DATE 11/0619/92 DATA FROM OLD VAX INFO | |
0318364231 | 2013-01-28 | Annular Disposal | No Violations | Well is not equipped or being used for annular disposal. The well was currently being pumped during inspection. There are no issues at well location. |
0482919837 | 2018-03-22 | Temporary Abandoned Annular Disposal | No Violations | I was on location today to check the annular disposal for Columbus. The annular disposal is not hooked up on this well. |
0848497577 | 2011-10-28 | Production Wells | No Violations | Records show this a very good Medina well. Jack pumping this day on well, tanks have good IDs, good dike, current chart in meter. |
1767730826 | 2017-11-13 | Production Wells | No Violations | This well appears to be capable of production at this time. The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The production valves at the wellhead are open to the production tanks. The identification for this well is located on the pumping unit and the production tank. There are no violations at this time. |
2089632258 | 2008-07-14 | Annular Disposal | No Violations | A.D. not hooked up,owner attempted to test A.D but could not bring it up to required pressure decision was made to install larger storage tank and produce well and haul brine to their injection well,test compressor has been removed from site and all annular fittings on wellhead have been removed. |
882 | PL | No Violations |
For data sources see[9]