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34-115-24641

Well Details

Well ID: 34-115-24641
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Country: United States
State: Ohio
County: Morgan
Municipality: Deerfield Township
Operator Name: J T PLUS WELL SERVICE LLC
Well Pad ID:
Farm/Lease Name: CLEMENS
License Status: Producing
License Date: 2008-11-03
Spud Date: 2008-11-13
Spud Drilling Contractor: JAM OIL & GAS
Final Drill Date: 2008-12-12
Well Total Depth: 1280.00 ft
Configuration: Vertical
Latitude: 39.670000
Longitude: -81.990000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-11-03 Proposed Formations:BEREA, Issued Date:11/3/2008, Expired Date:11/3/2009 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2008-12-12
Construction Permit Expires 2009-11-03
Completion Report Received 2010-12-14
Change of Owner 2015-01-09 Operator changed from 1512, ALTIER H L SERVICE CO INC to 8699, J T PLUS WELL SERVICE LLC
Record Last Modified 2017-10-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2011-03-31 1224 1228 4
2011-03-31 1236 1242 14
1224 1228 4
1236 1242 14
1224 1228 4

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2009-06-22 H2O 15 29910 Gal 20000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2009 H L ALTIER SERVICE CO INC 0.00 0.00 0
2010 H L ALTIER SERVICE CO INC 426.00 0.00 30
2011 H L ALTIER SERVICE CO INC 3166.00 76.00 365
2012 H L ALTIER SERVICE CO INC 1962.00 0.00 180
2013 H L ALTIER SERVICE CO INC 349.00 0.00 122
2015 J T PLUS WELL SERVICE LLC 776.00 0.00 365
2016 J T PLUS WELL SERVICE LLC 655.00 76.00 365
2017 J T PLUS WELL SERVICE LLC 786.00 0.00 365
2018 J T PLUS WELL SERVICE LLC 761.00 66.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2009 H L ALTIER SERVICE CO INC Brine 0 0
2010 H L ALTIER SERVICE CO INC Brine 0 30
2011 H L ALTIER SERVICE CO INC Brine 80 365
2012 H L ALTIER SERVICE CO INC Brine 0 180
2013 H L ALTIER SERVICE CO INC Brine 0 122
2015 J T PLUS WELL SERVICE LLC Brine 0 365
2016 J T PLUS WELL SERVICE LLC Brine 70 365
2017 J T PLUS WELL SERVICE LLC Brine 0 365
2018 J T PLUS WELL SERVICE LLC Brine 140 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1057553113 2014-10-15 0:00 PW No Violations
-1191861871 2014-6-23 0:00: PW No Violations
-1726386468 2018-9-28 0:00: PW No Violations 0.50
-1743896654 2010-5-13 0:00: DD No Violations 1.00
-194364511 2013-9-9 0:00:0 PW No Violations 1.00
-20641406 2009-10-29 0:00 PL No Violations
-356908776 2010-8-5 0:00:0 PW No Violations 1.00
0020641406 2009-10-29 Preliminary Restoration No Violations FOLLOW UP TO NOV # 1522904713 An inspection of the well revealed Preliminary Restoration not completed, well site and lease road needs graded, then seed and mulch. Spud date 11-13-08. No ID at well head or tank battery.
0194364511 2013-09-09 Production Wells Violations Noted The pumpjack was pumping when I arrived on location. The wellhead has a stuffing box leak which is causing oil contamination down into the conductor pipe and all over the wellhead. There are two 100 bbl tanks in the dike and at the base of the brine tank there is a puddle of brine contamination as a result of a disconnected steel line. It appears as if someone unscrewed the bull plug. There was also a disconnected steel elbow piece laying at the opening. There is a large kill area 15x 60 leading from the dike and drain pipe downhill to the gate. There is a creek just next to the area, however there is no evidence of the contamination reaching the waters. It appears as if someone released the tubing inside the dike to allow the brine contaminated water to drain downhill. It also appears that the dike was overflowing and seeping the contamination in certain areas. The operator must repair or replace any faulty equipment at the wellhead and in the dike. The operator must remove all contamination at the wellhead and in and around the dike. The operator must lime, seed and mulch the area in order to restore vegetative growth. I talked to Tim Altier and he is going to try and get a hold of his brother Sean Altier, who pumps the wells, in order to take care of the issues. Sean Altier retuned my call and didnt know anything about the issues and will head out there tonight to take a look and get things cleaned up this week.
0356908776 2010-08-05 Production Wells No Violations Follow-up on NOV, In-Compliance.
0576642741 2010-04-13 Drill / Deepen / Reopen No Violations Follow-up inspection revealed no action taken to comply with NOV. Preliminary Restoration has not been completed. Well site and tank pad is bare, no vegetation and starting to erode. Grade well site and place water diversions in as needed, seed, lime and mulch well site and tank pad in accordance with 1509.072(A). Will notify company by letter again, spoke with company about violation during winter.
0919337494 2009-10-29 Preliminary Restoration No Violations FOLLOW UP TO NOV # -20641406 FOLLOW UP TO NOV # 1522904713 An inspection of the well revealed Preliminary Restoration not completed, well site and lease road needs graded, then seed and mulch. Spud date 11-13-08. No ID at well head or tank battery.
1057553113 2014-10-15 Production Wells No Violations The well is now in compliance.
1111257861 2014-04-07 Production Wells No Violations Compliance Action Follow-up -194364511: The side slope of the dike still has not been restored from previous contamination. I called and talked to Sean Altier and he said once the weather improves and the ground is dry he will till and seed the dike.
1191861871 2014-06-23 Production Wells No Violations Compliance Action Follow-up -194364511: The side slope of the dike still has not been restored from previous contamination. I spoke with Sean Altier and he said he will get his son down there to till area and plant seed.
1229636807 2008-12-18 Drill / Deepen / Reopen No Violations Stopped by drilling rig for update they were preparing to move rig to new drill site,TD on this well was 1280 and operator ran 1265 of used 4.5 casing in hole and cemented in place with 30 sk cement.
1240870998 2009-04-27 Drill / Deepen / Reopen No Violations Drlg pit emptied and filled in, restoration work not done on well site or lease road. Spud date 11/13/08, due date 8/13/09
1248376767 2009-12-09 Drill / Deepen / Reopen No Violations Follow-up inspection revealed Preliminary Restoration not completed, no vegetation growing on well site. Spoke with Tim Altier (owner) about violation, Tim will have violation corrected in a couple weeks.
1382369266 2013-10-21 Production Wells No Violations Compliance Action Follow-up -194364511: Sean Altier has repaired the stuffing box and fixed the steel line in the dike. He has cleaned up around the wellhead but still needs to clean up scald area outside of the dike, which he stated would be in the next few weeks. He thinks someone was up there messing with the equipment.
1418683446 2014-01-13 Production Wells No Violations Compliance Action Follow-up -194364511: The side slope of the dike still has not been restored from previous contamination. I will return when there is better weather and work with Sean to restore vegetative growth.
1522904713 2009-10-29 Preliminary Restoration Violations Noted An inspection of the well revealed Preliminary Restoration not completed, well site and lease road needs graded, then seed and mulch. Spud date 11-13-08. No ID at well head or tank battery. Preliminary Restoration needs done, well site and lease road needs graded, seed, lime and mulched. Need full and legible ID at well head and tank battery. Failure to comply may result in a Forfeiture of Bond.
1726386468 2018-09-28 Production Wells No Violations I was on location today to do a field inspection on this well. At this time the well appears to be capable of production. The well has a pumping unit on it with rods and tubing in it. There are 2-100 barrel storage tank on location for this well. There are no violations at this time.
1743896654 2010-05-13 Drill / Deepen / Reopen No Violations Follow-up on NOV, Non-Compliance, no action has been taken to complete Preliminary Restoration. Rob Stonerock called company and explained that restoration was past due and if not complied with a forfeiture of Bond may be issued.
576642741 2010-4-13 0:00: DD No Violations 1.00
919337494 2009-10-29 0:00 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0194364511 US-OH-119570 2014-10-28 Well operation causing pollution and contamination
0194364511 US-OH-119571 2014-10-28 Equipment pressure rated below operating pressure
0194364511 US-OH-119572 2014-10-28 No SPCC dike/or failure to keep dike free of water or oil
0194364511 US-OH-119573 2014-10-28 Failure to have required locks, bull plugs
0194364511 US-OH-119574 2014-10-28 Dike or pit not able to prevent escape of brine or other wastes
0194364511 US-OH-119575 2014-10-28 Failure to keep dike or pit free of brine or other wastes
1522904713 US-OH-114508 2009-11-02 Failure to reimburse for costs of a corrective action
1522904713 US-OH-114509 2009-11-02 Failure to restore land surface within 9 mos. (CHANGE) (REPLACE)
1522904713 US-OH-114510 2009-11-02 Failure to legibly identify well

For data sources see[9]

References