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| Well ID: 34-117-20998 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Morrow | |
| Municipality: Cardington Township | |
| Operator Name: FISHBURN PRODUCING INC | |
| Well Pad ID: | |
| Farm/Lease Name: CLINGER C R | |
| License Status: Plugged and Abandoned | |
| License Date: 2016-04-15 | |
| Spud Date: 1964-02-29 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1964-03-08 | |
| Well Total Depth: 3114.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.540000 | |
| Longitude: -82.910000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1801-01-02 | 176 ASHLAND EXPLORATION INC |
| Original Spud | 1964-02-29 | COMPANY INSPECTION REPORT RECV'D 07/12/2013. LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE. |
| Completed | 1964-03-08 | COMPANY INSPECTION REPORT RECV'D 07/12/2013. LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE. |
| Reached Total Depth | 1964-03-08 | COMPANY INSPECTION REPORT RECV'D 07/12/2013. LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE. |
| CO | 1991-08-21 | 3941 FISHBURN PRODUCING INC GeoDate |
| APP | 2010-08-24 | Proposed Formations:TREMPEALEAU, Issued Date:8/24/2010, Expired Date:8/23/2012 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2012-12-19 | Proposed Formations:TREMPEALEAU, Issued Date:12/19/2012, Expired Date:12/19/2014 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2014-05-09 | Proposed Formations:TREMPEALEAU, Issued Date:5/9/2014, Expired Date:5/8/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2016-04-15 | Proposed Formations:TREMPEALEAU, Issued Date:4/15/2016, Expired Date:4/15/2018 12:00:00 PM, Drilling unit acres:104, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2018-04-13 | COMPANY INSPECTION REPORT RECV'D 07/12/2013. LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE. |
| Construction Permit Expires | 2018-04-15 | COMPANY INSPECTION REPORT RECV'D 07/12/2013. LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE. |
| Record Last Modified | 2018-07-11 | COMPANY INSPECTION REPORT RECV'D 07/12/2013. LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE. |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 2914 | 2928 | 28 |
| 2006-09-11 | 2956 | 2974 | 0 |
| 2914 | 2928 | 28 | |
| 2914 | 2928 | 28 |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | ASHLAND EXPLORATION INC | 0.00 | 756.00 | 365 |
| 1985 | ASHLAND EXPLORATION INC | 0.00 | 555.00 | 0 |
| 1986 | ASHLAND EXPLORATION INC | 0.00 | 564.00 | 365 |
| 1991 | FISHBURN PRODUCING INC | 0.00 | 822.00 | 150 |
| 1992 | FISHBURN PRODUCING INC | 0.00 | 901.00 | 365 |
| 1993 | FISHBURN PRODUCING INC | 0.00 | 348.00 | 180 |
| 1994 | FISHBURN PRODUCING INC | 0.00 | 378.00 | 270 |
| 1995 | FISHBURN PRODUCING INC | 0.00 | 300.00 | 350 |
| 1996 | FISHBURN PRODUCING INC | 0.00 | 161.00 | 120 |
| 1997 | FISHBURN PRODUCING INC | 0.00 | 262.00 | 300 |
| 1998 | FISHBURN PRODUCING INC | 0.00 | 139.00 | 105 |
| 1999 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2000 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 10 |
| 2001 | FISHBURN PRODUCING INC | 0.00 | 271.00 | 30 |
| 2002 | FISHBURN PRODUCING INC | 0.00 | 173.00 | 100 |
| 2003 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2004 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2005 | FISHBURN PRODUCING INC | 0.00 | 540.00 | 0 |
| 2006 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2007 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2008 | FISHBURN PRODUCING INC | 0.00 | 179.00 | 0 |
| 2009 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2010 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2011 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2012 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2013 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2014 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2015 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2016 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2017 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| 2018 | FISHBURN PRODUCING INC | 0.00 | 0.00 | 0 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1696562514 | 2018-5-4 0:00:0 | PB | No Violations | |
| -2031553958 | 2019-1-11 0:00: | PB | No Violations | |
| -2098685300 | 2013-2-4 0:00:0 | PW | No Violations | |
| -2126656365 | 2018-4-12 0:00: | PB | No Violations | |
| -745179336 | 2018-4-20 0:00: | PB | No Violations | |
| -76165408 | 2012-11-8 0:00: | AM | No Violations | |
| 0000PL9194 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 001287i540 | 2002-01-24 | Production Wells | No Violations | |
| 0076165408 | 2012-11-08 | Administrative Inspection | No Violations | Inspected the Clinger #1 (#998) as a request from the Columbus office for a Temporary Inactive permit application. No pump jack or storage. The well remains with tubing and rods removed and the well bore with 4.5 casing is open to the environment. There is no identification posted. |
| 0745179336 | 2018-04-20 | Plug / Plug Back | No Violations | Visit location with Health Physicist Mr. Paul Carder on location for testing. |
| 1020801948 | 2018-02-23 | Production Wells | No Violations | Inspected the Clinger #1 (#998) as part of a standard production well status check. No leaks noted. Status: ok, waiting on plugging. |
| 1287i540 | 2002-1-24 0:00: | PW | No Violations | |
| 1400506682 | 2014-05-19 | Production Wells | No Violations | Temporary Inactive Well Status second year permit received: Issued 5/9/2014 Expires 5/9/2015 |
| 1441132212 | 2015-09-01 | Production Wells | No Violations | The temporary inactive status year two permit has expired and was not renewed. Status: contacted operator for its plans for the well. |
| 1441294691 | 2015-09-01 | Production Wells | No Violations | Location Information for the Clinger #1 (#998). WELL HEAD: Lat. 40.54836 Long. -82.91660 / CENTER-OF-STORAGE PAD: Lat. 40.54836 Long. -82.91921 / ENTRANCE: Lat. 40.54844 Long. -82.91936. |
| 1445262460 | 2015-10-16 | Production Wells | No Violations | Received email from the operator stating that they are planning on applying for a plug permit. |
| 1462286051 | 2016-05-03 | Production Wells | No Violations | Permit to plug and abandon received: issued 4/15/2016 expires 4/15/2018. |
| 1523644956 | 2018-04-13 | Plug / Plug Back | No Violations | 4/13/18 Fishburn ran-in-hole and tagged plug #1 top at 2675 feet. Ripped 4.5 inch casing at 1110 feet and laid down casing. 9:28 am Cemenco hooked-up, broke circulation to clear casing and mixed and displaced straight Class A (15# weighed) cement plug #3 (Newburg 1050-750), Plug Down: 9:46 am. Fishburn laid down casing and shut down to wait-on-cement. 10:50 am Cemenco hooked-up, broke circulation and swept surface casing clean with 21 bbls fresh water at 3/5 bbls/min. Mixed and displaced Class A cement plug #3 (surface 480-154) Plug Down: 11:08 am. Fishburn laid down casing. 11:25 am Cemenco hooked-up and circulated cement plug #4 (top of surface) to surface, Plug Down: 11:30 am. Fishburn laid down casing, Cemenco topped off hole. Plugging operations co-witnessed by Fishburn service rig operator Mr. Tony Matthews. **The Clinger C.R. #1 (#998) Trempealeau well is officially plugged and abandoned** |
| 1523899807 | 2018-04-11 | Plug / Plug Back | No Violations | Fishburn finished running tubing for plugging, workover pit is lined and Cemenco pump truck is parked on location. No one working. |
| 1696562514 | 2018-05-04 | Plug / Plug Back | No Violations | Check workover pit and cement top after plugging. Status: cement top 28 feet from surface, workover pit 12 inches from top. Contacted operator with status update. |
| 1806740452 | 2017-09-20 | Production Wells | No Violations | Inspected the Clinger #1 (#998) as part of a standard production well status check. Inspect well, storage and identification. Status: ok, the plug permit expires 4/15/2018. |
| 2031553958 | 2019-01-11 | Plug / Plug Back | No Violations | Ellis Brother ready mix truck topped off the surface casing with 9 sack grout. Firshburn excavated around the well head and cut off the casing 4 feet below ground level and welded on a steel identification plate. Photo-documented. Status: Fishburn to get landowner waiver to complete restoration. |
| 2098685300 | 2013-02-04 | Production Wells | No Violations | The Clinger #1 (#998) has been placed into temporary inactive status, expires first year 12/19/2013. No change in status, the well lacks production equipment and well identification. |
| 2126656365 | 2018-04-12 | Plug / Plug Back | No Violations | Fishburn finished running 2.375 inch upset tubing to 3075 feet. 8:26 am Cemenco hooked-up, broke circulation with 21 bbls fresh water, mixed and displaced 30 sacks, straight Class A cement Plug #1 (Trempealeau, 3075-2675), inside the 4.5 inch casing: Plug down 8:45 am. Fishburn laid down tubing string and hooked onto the 4.5 inch casing and pulled 4 inches of stretch to check for integrity (ok). Shut-down for the day. |
| PL9194 | PL | No Violations |
For data sources see[8]