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34-117-22216

Well Details

Well ID: 34-117-22216
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Country: United States
State: Ohio
County: Morrow
Municipality: Gilead Township
Operator Name: GEOPETRO LLC
Well Pad ID:
Farm/Lease Name: SALISBURY (GOODMAN)
License Status: Plugged and Abandoned
License Date: 2017-11-28
Spud Date: 2006-09-06
Spud Drilling Contractor: MARIC DRILLING CO.
Final Drill Date: 2006-09-09
Well Total Depth: 3485.00 ft
Configuration: Vertical
Latitude: 40.510000
Longitude: -82.800000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1964-10-27
Completed 1964-11-09
APP 2006-08-16 Proposed Formations:TRENTON THRU TREMPEALEAU, Issued Date:8/16/2006, Expired Date:8/16/2007 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2006-09-09
Completion Report Received 2006-12-04
Change of Owner 2016-02-23 Operator changed from 6227, HOUGHTON INVESTMENTS LLC to 5677, GEOPETRO LLC
APP 2017-11-28 Proposed Formations:BLACK RIVER, Issued Date:11/28/2017, Expired Date:11/28/2019 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-07-13
Record Last Modified 2019-05-10
Construction Permit Expires 2019-11-28

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2007-02-01 3164 3170 25
3164 3170 25
3164 3170 25

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 1000 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2006 HOUGHTON INVESTMENTS LLC 0.00 59.00 365
2007 HOUGHTON INVESTMENTS LLC 0.00 59.00 365
2008 HOUGHTON INVESTMENTS LLC 0.00 86.00 365
2009 HOUGHTON INVESTMENTS LLC 0.00 58.00 365
2010 HOUGHTON INVESTMENTS LLC 0.00 40.00 365
2011 HOUGHTON INVESTMENTS LLC 0.00 44.00 365
2012 HOUGHTON INVESTMENTS LLC 0.00 28.00 366
2013 HOUGHTON INVESTMENTS LLC 0.00 19.00 365
2014 HOUGHTON INVESTMENTS LLC 0.00 0.00 365
2015 HOUGHTON INVESTMENTS LLC 0.00 0.00 365
2016 GEOPETRO LLC 0.00 0.00 0
2017 GEOPETRO LLC 0.00 0.00 0
2018 GEOPETRO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2006 HOUGHTON INVESTMENTS LLC Brine 800 365
2007 HOUGHTON INVESTMENTS LLC Brine 0 365
2008 HOUGHTON INVESTMENTS LLC Brine 0 365
2009 HOUGHTON INVESTMENTS LLC Brine 60 365
2010 HOUGHTON INVESTMENTS LLC Brine 0 365
2011 HOUGHTON INVESTMENTS LLC Brine 0 365
2012 HOUGHTON INVESTMENTS LLC Brine 0 366
2013 HOUGHTON INVESTMENTS LLC Brine 0 365
2014 HOUGHTON INVESTMENTS LLC Brine 0 365
2015 HOUGHTON INVESTMENTS LLC Brine 0 365
2016 GEOPETRO LLC Brine 0 0
2017 GEOPETRO LLC Brine 0 0
2018 GEOPETRO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1300912188 2016-3-2 0:00:0 PW No Violations
-1918794722 2018-7-13 0:00: PB No Violations
-1954839424 2017-12-13 0:00 PB No Violations
-2080430596 2015-1-23 0:00: PW No Violations
-945395702 2018-7-16 0:00: PB No Violations
0049943885 2015-01-23 Production Wells No Violations Inspected the Salisbury #1 (#2216) as part of a standard production well status check. Inspect well, storage and identification. Status: not in production.
0945395702 2018-07-16 Plug / Plug Back No Violations Check status of top plug after weekend. Ran depth counter into casing, plug top at 5 feet from ground level. Contacted operator who planned on topping off with bagged cement after cutting off the casing 36 inches below ground level.
1190398564 2007-09-21 Preliminary Restoration No Violations Preliminary restoration done.
1300912188 2016-03-02 Production Wells No Violations Change-of-operator noted: Houghton Investments to Geopetro LLC 2/23/2016.
1367511343 2013-05-02 Production Wells No Violations Inspected the Salisbury (Goodman) #1 (#2216) as part of a standard productive well status check. The well is equipped with a Churchill gas powered pumpjack and the well pad is clean and free of excess contamination. The storage consists of two tanks (#138951) and a brine tank set in a gravel, fully lined dike. The well identification and emergency contact information is marked at the storage. This is an old Trempealeau well reopened and completed in the Black River. Status: ok.
1531853745 2018-07-12 Plug / Plug Back No Violations 4:18 pm Berry Well Service finished laying down tubing, hooked-up swab tool and made two runs and swabbed the fluid level down to the top of the perfs at 3164 (Black River). 5:18 pm Cemenco hooked-up to the 4.5 inch casing and mixed 30 sacks Class A cement plug #1 (3164-2764) and displaced with 44.5 bbls of water at a rate of 5 bbls per minute. 5:33 pm plug landed at 200 psi-bumped to 700 psi and shut down for the night.
1532538226 2018-07-18 Plug / Plug Back No Violations Check status of restoration. The well was cut-off approximately 36 inches below ground level and was identified by Mr. Kenny Smith who welded on an identification plate (photo-documented) and buried by Mr. Kevin Mullins. The workover pits have been closed, flowline removed and cut up, storage dike and gravel removed. 2 storage tanks, pump jack and 3 piles of gravel remain on location. The landowner plans to use the gravel for personal use. Status: will continue to monitor restoration.
1918794722 2018-07-13 Plug / Plug Back No Violations Berry Well Service ran-in-hole and confirmed cement top (plug #1) at 2752. Rigged up ripping tool and began looking for soundings at 2500 feet. No sounding until 1472 (bottom of the Big Lime). Achieved rip and laid down one range 3 joint. 10:11 am Cemenco hooked-up broke circulation and mixed 75 (*planned 85) sacks Class A plug #2 (1430-1160) at 10:18 am the return water turned gray from clear. *Initially thought cement slurry had return to surface-displaced plug as mixed: plug down 10:28 am. Pulled casing up to next plug depth and evaluated. Testing on the fluid were negative for cement and the pulled casing had integrity (no holes or ruptures seen), added the unused 10 sacks of cement to the subsequent plug #3 (Big Lime). 11:00 am Mullins Energy Service dug and lined an additional workover pit. 11:50 am Cemenco hooked-up broke circulation and mixed 52 sacks Class A cement plug #3 (860-678), plug down 12:00 pm. Berry Well Service laid down casing and shut down to wait on additional fresh water. 1:05 pm Cemenco hooked-up to casing and displaced 30 bbls tested fresh water at 3 bbls per minute to flush surface casing. 1:15 pm mixed 58 sacks Class A plug #4 (500-300) plug down 1:24 pm. Berry Well Service finished laying down casing, fluid level at 120. Cemenco mixed 36 sacks Class A cement and displaced with gravity plug #5 (120-0) to the surface which held, plug down: 1:47 pm. Plugging operations co-witnessed by Geopetro LLC. Representative Mr. Eric Brown and Mr. Kevin Mullins. **The Salisbury (Goodman) #1 (#2160) Black River Well (reopen), is Officially Plugged and Abandoned**
1954839424 2017-12-13 Plug / Plug Back No Violations Plugging permit received: issued 11/28/2017 expires 11/28/2019
2080430596 2015-01-23 Production Wells No Violations Location Information for the Salisbury #1 (#2216). WELL HEAD: Lat. 40.51871 Long. -82.80772 / CENTER-OF-STORAGE: Lat. 40.51915 Long. -82.80763 / ENTRANCE: Lat. 40.51947 Long. -82.81669.
49943885 2015-1-23 0:00: PW No Violations

For data sources see[9]

References