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34-117-23767

Well Details

Well ID: 34-117-23767
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Country: United States
State: Ohio
County: Morrow
Municipality: Franklin Township
Operator Name: PATSY S LAW TRUST
Well Pad ID:
Farm/Lease Name: EARL & SHERRILL VANHORN
License Status: Final Restoration
License Date: 2012-10-05
Spud Date: 1987-04-07
Spud Drilling Contractor: CAMPHIRE DRILLING
Final Drill Date: 1987-05-28
Well Total Depth: 3780.00 ft
Configuration: Vertical
Latitude: 40.550000
Longitude: -82.730000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1987-02-25 Issued Date 2/25/87 Expired Date 2/25/88 Acres 0020000 Tool Type CT Proposed Formation TREMPEALEAU Proposed Depth 03780 Proposed Drill Depth 03780
Original Spud 1987-04-07
Completed 1987-05-28
Reached Total Depth 1987-05-28
CO 1987-06-10 259 SPARKS HAROLD GeoDate 2/25/87
Completion Report Received 1987-09-04
CO 1992-08-18 2794 TENEYCK K/KRISTOFER O&G GeoDate 2/25/87
CO 1994-10-12 4943 LAW PATSY S TRUST GeoDate 2/25/87
APP 2012-10-05 Proposed Formations:, Issued Date:10/5/2012, Expired Date:10/5/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-04-22
Construction Permit Expires 2014-10-05
Record Last Modified 2019-06-14

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3756 0
3756 0
3756 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 1500 Gal 0 ACIDIZED W/1500 GAL

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 SPARKS HAROLD 0.00 565.00 90

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 SPARKS HAROLD Brine 200 90

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1901002902 2007-4-24 0:00: PW No Violations
-2135095240 2010-4-12 0:00: AM No Violations
-746132006 2012-10-10 0:00 PW No Violations
0000PL9022 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0746132006 2012-10-10 Production Wells No Violations The operator has applied for a plugging permit issued 10/5/2012, expires 10/5/2014.
1177936936 2007-04-24 Production Wells Violations Noted Well has pump jack but is not capable due to pulley half of motor missing. Well appears not to have been pumped recently. Well operates off of propane. Plastic lead line has been cut from land owner mowing and will need to be repaired before well can pump. Digital photos taken. Landowner called on line and wants well operated or plugged.
1208788027 2008-04-17 Production Wells No Violations Follow up on NOV issued by Jeff Fry. The well is still incapable of production at this time due to the gas line not being hooked to the motor. No Identification posted.
1256571892 2009-10-26 Production Wells No Violations NOV resolved the well is equipped to produce
1365615048 2013-04-10 Plug / Plug Back No Violations On-site with George Camphire to begin plugging of the Vanhorn #3. 12:15 pm begin washing in clay for the bottom hole plug. 3:20 pm 710 shovels washed-in, run in check for bridges. Shut down for day.
1365694219 2013-04-11 Plug / Plug Back No Violations No one working due to heavy rains and flooding.
1366731517 2013-04-22 Plug / Plug Back No Violations ODNR was not notified for completion of the plugging of the Vanhorn #3. Gave plugging affidavit George Camphire to complete. Clay tickets received.
1366737274 2013-04-23 Final Restoration No Violations George Camphire has begun the final restoration and is removing the storage.
1369331167 2013-05-23 Final Restoration No Violations Received request by Mr. George Camphire to inspect the storage area restoration as part of the final restoration. Mr. Camphire has removed all the storage most of the gravel and graded the area with a bulldozer. He states that the farmer is fine with the grading and will be able to plant the area. Waivers needed for the flow lines and access road before the final restoration is complete. Status: will continue to monitor restoration.
1380732845 2013-10-02 Final Restoration No Violations Final restoration is not complete, waiver needed for road and flow lines. Status: contacted operator.
1389018491 2014-01-06 Final Restoration No Violations Signed landowner waiver received for the access road. Final restoration complete.
1901002902 2007-04-24 Production Wells No Violations FOLLOW UP TO NOV # 1177936936 Well has pump jack but is not capable due to pulley half of motor missing. Well appears not to have been pumped recently. Well operates off of propane. Plastic lead line has been cut from land owner mowing and will need to be repaired before well can pum
2135095240 2010-04-12 Administrative Inspection No Violations Resolve NOV. Inspection Report 10-26-09 per Inspector Faust, well capable.
PL9022 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1177936936 US-OH-104728 2007-04-30 Well shall be plugged

For data sources see[9]

References