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34-117-23775

Well Details

Well ID: 34-117-23775
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Country: United States
State: Ohio
County: Morrow
Municipality: Perry Township
Operator Name: PETRO EVALUATION SERVICES INC
Well Pad ID:
Farm/Lease Name: MORRISON-HOWARD UNIT
License Status: Final Restoration
License Date: 2010-04-12
Spud Date: 1987-06-22
Spud Drilling Contractor: KIDD DRILLING
Final Drill Date: 1987-06-25
Well Total Depth: 1577.00 ft
Configuration: Vertical
Latitude: 40.600000
Longitude: -82.680000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1987-06-08 164 PETRO EVALUATION SERV INC GeoDate 6/8/87
Oil and Gas 1987-06-08 Issued Date 6/8/87 Expired Date 6/7/88 Acres 0040000 Tool Type CRA Proposed Formation TREMPEALEAU Proposed Depth 01577 Proposed Drill Depth 01577
Original Spud 1987-06-22
Completed 1987-06-25
Reached Total Depth 1987-06-25
Completion Report Received 1989-09-19
APP 2010-04-12 Proposed Formations:TREMPEALEAU, Issued Date:4/12/2010, Expired Date:4/12/2011 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged/Abandoned 2010-05-21
Construction Permit Expires 2011-04-12
Record Last Modified 2015-09-24

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NATURAL PRODUCER

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1306802555 2010-11-16 0:00 FR No Violations
0000PL9019 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1268745511 2010-03-15 Production Wells Violations Noted On site with Landowner Bob Morrison. Mr. Morrison stated that the well has not been in production for appox 20 years and that he would like to see the well get plugged. The well is incapable of production due to the lack of a sailes line for the gas. The well head is leaking at this time around the 4.5 inch casing. Petro Evaluation Serv Inc its agents,assignees and sucsseccors shall plug the well or put it into production.
1274814028 2010-05-21 Plug / Plug Back No Violations On site to plug with cement. NOV plug or produce resolved.
1306802555 2010-11-16 Final Restoration No Violations Final restoration done. Casing cut off site graded and seeded with an agricultural crop ( winter wheat)
PL9019 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1268745511 US-OH-107213 2010-03-16 Well shall be plugged

For data sources see[4]

References