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Well ID: 34-119-22499 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Wayne Township | |
Operator Name: CAMERON PRODUCTION CO INC | |
Well Pad ID: | |
Farm/Lease Name: BOETCHER | |
License Status: Final Restoration | |
License Date: 2014-04-17 | |
Spud Date: 1972-04-30 | |
Spud Drilling Contractor: | |
Final Drill Date: 1972-05-07 | |
Well Total Depth: 4205.00 ft | |
Configuration: Vertical | |
Latitude: 39.900000 | |
Longitude: -81.910000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1972-04-30 | RE-ISSUED 4-27-72 RE-ISSUED 04/27/1972 |
Completed | 1972-05-07 | RE-ISSUED 4-27-72 RE-ISSUED 04/27/1972 |
Reached Total Depth | 1972-05-07 | RE-ISSUED 4-27-72 RE-ISSUED 04/27/1972 |
CO | 1984-10-31 | 1146 ENNEY OILFIELD COMPANY |
Change of Owner | 1998-01-27 | Operator changed from 1146, SCION ENERGY, Inc. to 2409, RANDELL OIL CO |
Change of Owner | 1998-08-05 | Operator changed from 2409, RANDELL OIL CO to 1720, CAMERON PROD CO INC |
APP | 2014-04-17 | Proposed Formations:, Issued Date:4/17/2014, Expired Date:4/16/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-08-01 | RE-ISSUED 4-27-72 RE-ISSUED 04/27/1972 |
Construction Permit Expires | 2016-04-16 | RE-ISSUED 4-27-72 RE-ISSUED 04/27/1972 |
Record Last Modified | 2019-06-14 | RE-ISSUED 4-27-72 RE-ISSUED 04/27/1972 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4077 | 4102 | 0 |
4077 | 4102 | 0 | |
4077 | 4102 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 3000 Bbl | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | SCION ENERGY INC | 1154.00 | 243.00 | 0 |
1985 | SCION ENERGY INC | 1567.00 | 286.00 | 365 |
1986 | SCION ENERGY INC | 2222.00 | 379.00 | 365 |
1987 | SCION ENERGY INC | 1883.00 | 197.00 | 365 |
1988 | SCION ENERGY INC | 1715.00 | 186.00 | 365 |
1989 | SCION ENERGY INC | 1587.00 | 237.00 | 365 |
1990 | SCION ENERGY INC | 1251.00 | 166.00 | 365 |
1991 | SCION ENERGY INC | 1264.00 | 151.00 | 365 |
1992 | SCION ENERGY INC | 984.00 | 197.00 | 365 |
1993 | SCION ENERGY INC | 696.00 | 125.00 | 365 |
1994 | SCION ENERGY INC | 1686.00 | 112.00 | 365 |
1995 | SCION ENERGY INC | 421.00 | 0.00 | 365 |
1996 | SCION ENERGY INC | 394.00 | 0.00 | 365 |
1997 | SCION ENERGY INC | 443.00 | 0.00 | 365 |
1998 | RANDELL OIL CO | 49.00 | 0.00 | 90 |
1999 | CAMERON PRODUCTION CO INC | 985.00 | 121.00 | 0 |
2000 | CAMERON PRODUCTION CO INC | 887.00 | 61.00 | 365 |
2001 | CAMERON PRODUCTION CO INC | 342.00 | 120.00 | 365 |
2002 | CAMERON PRODUCTION CO INC | 513.00 | 58.00 | 365 |
2003 | CAMERON PRODUCTION CO INC | 816.00 | 58.00 | 365 |
2004 | CAMERON PRODUCTION CO INC | 165.00 | 108.00 | 365 |
2005 | CAMERON PRODUCTION CO INC | 390.00 | 0.00 | 365 |
2006 | CAMERON PRODUCTION CO INC | 263.00 | 117.00 | 365 |
2007 | CAMERON PRODUCTION CO INC | 163.00 | 56.00 | 365 |
2008 | CAMERON PRODUCTION CO INC | 263.00 | 117.00 | 365 |
2009 | CAMERON PRODUCTION CO INC | 132.00 | 0.00 | 365 |
2010 | CAMERON PRODUCTION CO INC | 293.00 | 49.00 | 365 |
2011 | CAMERON PRODUCTION CO INC | 108.00 | 0.00 | 0 |
2012 | CAMERON PRODUCTION CO INC | 62.00 | 26.00 | 366 |
2013 | CAMERON PRODUCTION CO INC | 10.00 | 0.00 | 365 |
2014 | CAMERON PRODUCTION CO INC | 103.00 | 0.00 | 365 |
2015 | CAMERON PRODUCTION CO INC | 0.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-544068229 | 2016-2-1 0:00:0 | FR | No Violations | 1.00 |
-623002636 | 2014-8-1 0:00:0 | PB | No Violations | 7.00 |
0265955152 | 2010-02-09 | Production Wells | No Violations | Producing, no problems noted at time of inspection. |
0544068229 | 2016-02-01 | Final Restoration | No Violations | 119-22499 well owned by Cameron Producing Inc. has been plugged. Final Restoration passed on 2-1-16 by Patrick Shreve. Well was plugged in compliance OAC 1501-9-11. The land was restored back under ORC 1509.072. |
0623002636 | 2014-08-01 | Plug / Plug Back | No Violations | Berrys well service ran 2 10 round tubing in the 4.5casing to the depth of 2995. The lime plug was set at 2995-2395. The Berea plug was set at 1226-826. The 4.5 casing was ripped off at 662. Set Plug at 615-365. Set surface plug 200-0. All plugs circulated. |
0928485281 | 2004-03-09 | Production Wells | No Violations | |
1194988755 | 2007-11-13 | Production Wells | No Violations | Producing, no problems noted. |
1406816920 | 2014-07-31 | Plug / Plug Back | No Violations | Berrys well service is over well. The pulled 2.375tubing 10 round and pulled mud anchor. They ran tubing back in. Cemenco is spotting the cement plug in the bottom at 4132-3742 of 30 sacks of regular class A cement. Well did not circulate. |
1406901919 | 2014-07-31 | Administrative Inspection | No Violations | Berrys well service called and stated that they could not get telegraph up until 682. Two years ago the company had washed clay down the backside to fix holes in the pipe. There was about 16-20-ton of clay on back side. The decision was made to spot the cement plugs thru the 2 tubing inside the 4.5casing. The big lime and the Berea were the only two plugs in the pipe. |
265955152 | 2010-2-9 0:00:0 | PW | No Violations | |
928485281 | 2004-3-9 0:00:0 | PW | No Violations |
For data sources see[9]