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Well ID: 34-119-23215 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Muskingum Township | |
Operator Name: MOCK PHILIP & DARLISS | |
Well Pad ID: | |
Farm/Lease Name: MOCK | |
License Status: Final Restoration | |
License Date: 2011-06-07 | |
Spud Date: 1973-11-06 | |
Spud Drilling Contractor: | |
Final Drill Date: 1973-12-03 | |
Well Total Depth: 3430.00 ft | |
Configuration: Vertical | |
Latitude: 40.080000 | |
Longitude: -82.090000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1973-10-25 | 107 PREMIER ENERGY CORP GeoDate 10/25/73 |
Original Spud | 1973-11-06 | IP. A.F. 1.1MMCFG |
Completed | 1973-12-03 | IP. A.F. 1.1MMCFG |
Reached Total Depth | 1973-12-03 | IP. A.F. 1.1MMCFG |
Completion Report Received | 1975-01-21 | IP. A.F. 1.1MMCFG |
Change of Owner | 2011-05-24 | Operator changed from 107, PREMIER ENERGY CORP to 8848, MOCK PHILIP & DARLISS. WELL TRANSFERRED PER OWNERSHIP AFFIDAVIT AND INSPECTOR REPORTS. WELL IS TO BE PLUGGED. SEE OWNER FILE FOR MORE INFO. |
APP | 2011-06-07 | Proposed Formations:CLINTON, Issued Date:6/7/2011, Expired Date:6/6/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2011-06-15 | IP. A.F. 1.1MMCFG |
Record Last Modified | 2013-03-14 | IP. A.F. 1.1MMCFG |
Construction Permit Expires | 2013-06-06 | IP. A.F. 1.1MMCFG |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3347 | 3401 | 16 |
3347 | 3401 | 16 | |
3347 | 3401 | 16 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 68000 Gal | 40000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | LIGHTHIZER CHARLES O | 3215.00 | 31.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | LIGHTHIZER CHARLES O | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1018970821 | 2011-6-7 0:00:0 | PB | No Violations | |
-1302238893 | 2011-6-9 0:00:0 | PB | No Violations | 5.00 |
-1772794337 | 2011-6-2 0:00:0 | PB | No Violations | 3.00 |
-1875108265 | 2012-4-16 0:00: | FR | No Violations | 1.00 |
-688673907 | 2003-12-17 0:00 | PW | No Violations | |
0027533652 | 2005-02-10 | Production Wells | No Violations | |
0688673907 | 2003-12-17 | Production Wells | No Violations | Landowner bought well some 30 years ago. Says he probably still has the bill of sale somewhere. House gas only. |
1018970821 | 2011-06-07 | Plug / Plug Back | No Violations | Jet Wireline shot off 4.5 casing at 2340. |
1302238893 | 2011-06-09 | Plug / Plug Back | No Violations | On day of inspection Altier swabbed 30 barrels of crude oil from this well. They set cast plug on a 7 seat and then ran 4 tons of clay in on seat. |
1307546070 | 2011-06-03 | Plug / Plug Back | No Violations | Altier Brothers set bottom plug with 4 tons of clay. We started to rip pipe and it pulled apart. Will get mandrel and spear for Tuesday. |
1559632370 | 2011-06-15 | Plug / Plug Back | No Violations | Alteir was not at the rig. Piping was still on the trailer. |
1772794337 | 2011-06-02 | Plug / Plug Back | No Violations | On day of inspection alteirs rig was pulling tubing and cutting rods because of salt lock up. |
1875108265 | 2012-04-16 | Final Restoration | No Violations | Final Restoration has passed on 4-16-12 by Patrick Shreve. |
27533652 | 2005-2-10 0:00: | PW | No Violations |
For data sources see[9]