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34-119-23215

Well Details

Well ID: 34-119-23215
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Country: United States
State: Ohio
County: Muskingum
Municipality: Muskingum Township
Operator Name: MOCK PHILIP & DARLISS
Well Pad ID:
Farm/Lease Name: MOCK
License Status: Final Restoration
License Date: 2011-06-07
Spud Date: 1973-11-06
Spud Drilling Contractor:
Final Drill Date: 1973-12-03
Well Total Depth: 3430.00 ft
Configuration: Vertical
Latitude: 40.080000
Longitude: -82.090000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1973-10-25 107 PREMIER ENERGY CORP GeoDate 10/25/73
Original Spud 1973-11-06 IP. A.F. 1.1MMCFG
Completed 1973-12-03 IP. A.F. 1.1MMCFG
Reached Total Depth 1973-12-03 IP. A.F. 1.1MMCFG
Completion Report Received 1975-01-21 IP. A.F. 1.1MMCFG
Change of Owner 2011-05-24 Operator changed from 107, PREMIER ENERGY CORP to 8848, MOCK PHILIP & DARLISS. WELL TRANSFERRED PER OWNERSHIP AFFIDAVIT AND INSPECTOR REPORTS. WELL IS TO BE PLUGGED. SEE OWNER FILE FOR MORE INFO.
APP 2011-06-07 Proposed Formations:CLINTON, Issued Date:6/7/2011, Expired Date:6/6/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2011-06-15 IP. A.F. 1.1MMCFG
Record Last Modified 2013-03-14 IP. A.F. 1.1MMCFG
Construction Permit Expires 2013-06-06 IP. A.F. 1.1MMCFG

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3347 3401 16
3347 3401 16
3347 3401 16

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 68000 Gal 40000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 LIGHTHIZER CHARLES O 3215.00 31.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 LIGHTHIZER CHARLES O Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1018970821 2011-6-7 0:00:0 PB No Violations
-1302238893 2011-6-9 0:00:0 PB No Violations 5.00
-1772794337 2011-6-2 0:00:0 PB No Violations 3.00
-1875108265 2012-4-16 0:00: FR No Violations 1.00
-688673907 2003-12-17 0:00 PW No Violations
0027533652 2005-02-10 Production Wells No Violations
0688673907 2003-12-17 Production Wells No Violations Landowner bought well some 30 years ago. Says he probably still has the bill of sale somewhere. House gas only.
1018970821 2011-06-07 Plug / Plug Back No Violations Jet Wireline shot off 4.5 casing at 2340.
1302238893 2011-06-09 Plug / Plug Back No Violations On day of inspection Altier swabbed 30 barrels of crude oil from this well. They set cast plug on a 7 seat and then ran 4 tons of clay in on seat.
1307546070 2011-06-03 Plug / Plug Back No Violations Altier Brothers set bottom plug with 4 tons of clay. We started to rip pipe and it pulled apart. Will get mandrel and spear for Tuesday.
1559632370 2011-06-15 Plug / Plug Back No Violations Alteir was not at the rig. Piping was still on the trailer.
1772794337 2011-06-02 Plug / Plug Back No Violations On day of inspection alteirs rig was pulling tubing and cutting rods because of salt lock up.
1875108265 2012-04-16 Final Restoration No Violations Final Restoration has passed on 4-16-12 by Patrick Shreve.
27533652 2005-2-10 0:00: PW No Violations

For data sources see[9]

References