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Well ID: 34-119-23602 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Falls Township | |
Operator Name: R C POLING CO INC | |
Well Pad ID: | |
Farm/Lease Name: DAVID MURRAY | |
License Status: Final Restoration | |
License Date: 2011-06-28 | |
Spud Date: 1976-04-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-05-27 | |
Well Total Depth: 3478.00 ft | |
Configuration: Vertical | |
Latitude: 39.990000 | |
Longitude: -82.050000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1975-12-29 | 28 CGAS EXPLORATION,INC GeoDate 12/29/75 |
Original Spud | 1976-04-26 | RE-ISSUE 12-31-75 / R.L. 4-21-76 |
Completed | 1976-05-20 | RE-ISSUE 12-31-75 / R.L. 4-21-76 |
Reached Total Depth | 1976-05-27 | RE-ISSUE 12-31-75 / R.L. 4-21-76 |
Change of Owner | 1999-09-07 | Operator changed from 28, CGAS EXPLORATION to 6295, KNOX ENERGY INC. |
Change of Owner | 2001-07-11 | Operator changed from 6295, KNOX ENERGY INC. to 236, POLING R C CO INC |
APP | 2006-08-04 | Proposed Formations:CLINTON, Issued Date:8/4/2006, Expired Date:8/4/2007 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
APP | 2007-10-25 | Proposed Formations:CLINTON, Issued Date:10/25/2007, Expired Date:10/24/2008 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
APP | 2009-04-13 | Proposed Formations:CLINTON, Issued Date:4/13/2009, Expired Date:4/13/2010 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
APP | 2010-06-16 | Proposed Formations:CLINTON, Issued Date:6/16/2010, Expired Date:6/16/2011 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
APP | 2011-06-28 | Proposed Formations:CLINTON, Issued Date:6/28/2011, Expired Date:6/27/2013 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2011-08-31 | RE-ISSUE 12-31-75 / R.L. 4-21-76 |
Construction Permit Expires | 2013-06-27 | RE-ISSUE 12-31-75 / R.L. 4-21-76 |
Record Last Modified | 2017-02-15 | RE-ISSUE 12-31-75 / R.L. 4-21-76 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 90000 Gal | 40000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | AMEX ENERGY CONSULTS INC | 13338.00 | 181.00 | 0 |
1985 | AMEX ENERGY CONSULTS INC | 9229.00 | 100.00 | 0 |
1986 | AMEX ENERGY CONSULTS INC | 6953.00 | 146.00 | 365 |
1987 | AMEX ENERGY CONSULTS INC | 5713.00 | 92.00 | 365 |
1988 | AMEX ENERGY CONSULTS INC | 4866.00 | 0.00 | 365 |
1989 | CGAS EXPLORATION | 4157.00 | 183.00 | 365 |
1990 | CGAS EXPLORATION | 3798.00 | 79.00 | 365 |
1991 | CGAS EXPLORATION | 3767.00 | 81.00 | 365 |
1992 | CGAS EXPLORATION | 3225.00 | 0.00 | 366 |
1993 | CGAS EXPLORATION | 3073.00 | 74.00 | 366 |
1994 | CGAS EXPLORATION | 2013.00 | 0.00 | 365 |
1995 | CGAS EXPLORATION | 1058.00 | 0.00 | 365 |
1996 | CGAS EXPLORATION | 1490.00 | 74.00 | 365 |
1997 | CGAS EXPLORATION | 1647.00 | 78.00 | 365 |
1998 | CGAS EXPLORATION | 1868.00 | 0.00 | 365 |
1999 | CGAS EXPLORATION | 746.00 | 0.00 | 365 |
2000 | KNOX ENERGY INC. | 53.00 | 0.00 | 30 |
2001 | KNOX ENERGY INC. | 0.00 | 0.00 | 365 |
2002 | KNOX ENERGY INC. | 0.00 | 0.00 | 365 |
2003 | R C POLING CO INC | 0.00 | 0.00 | 365 |
2004 | R C POLING CO INC | 0.00 | 0.00 | 365 |
2005 | R C POLING CO INC | 0.00 | 0.00 | 1 |
2007 | R C POLING CO INC | 0.00 | 0.00 | 365 |
2008 | R C POLING CO INC | 0.00 | 0.00 | 365 |
2009 | R C POLING CO INC | 0.00 | 0.00 | 365 |
2010 | R C POLING CO INC | 0.00 | 0.00 | 365 |
2011 | R C POLING CO INC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | AMEX ENERGY CONSULTS INC | Brine | 0 | 0 |
1985 | AMEX ENERGY CONSULTS INC | Brine | 0 | 0 |
1986 | AMEX ENERGY CONSULTS INC | Brine | 0 | 365 |
1987 | AMEX ENERGY CONSULTS INC | Brine | 0 | 365 |
1988 | AMEX ENERGY CONSULTS INC | Brine | 2 | 365 |
1989 | CGAS EXPLORATION | Brine | 13 | 365 |
1990 | CGAS EXPLORATION | Brine | 14 | 365 |
1991 | CGAS EXPLORATION | Brine | 0 | 365 |
1992 | CGAS EXPLORATION | Brine | 15 | 366 |
1993 | CGAS EXPLORATION | Brine | 0 | 366 |
1994 | CGAS EXPLORATION | Brine | 0 | 365 |
1995 | CGAS EXPLORATION | Brine | 15 | 365 |
1996 | CGAS EXPLORATION | Brine | 0 | 365 |
1997 | CGAS EXPLORATION | Brine | 14 | 365 |
1998 | CGAS EXPLORATION | Brine | 0 | 365 |
1999 | CGAS EXPLORATION | Brine | 0 | 365 |
2000 | KNOX ENERGY INC. | Brine | 0 | 30 |
2001 | R C POLING CO INC | Brine | 0 | 365 |
2002 | R C POLING CO INC | Brine | 0 | 365 |
2003 | R C POLING CO INC | Brine | 0 | 365 |
2004 | R C POLING CO INC | Brine | 0 | 365 |
2005 | R C POLING CO INC | Brine | 75 | 1 |
2007 | R C POLING CO INC | Brine | 0 | 365 |
2008 | R C POLING CO INC | Brine | 0 | 365 |
2009 | R C POLING CO INC | Brine | 0 | 365 |
2010 | R C POLING CO INC | Brine | 0 | 365 |
2011 | R C POLING CO INC | Brine | 30 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1060912495 | 2011-8-15 0:00: | PB | No Violations | 4.00 |
-1480436667 | 2012-8-6 0:00:0 | FR | No Violations | 1.00 |
-670099489 | 2011-8-16 0:00: | PB | No Violations | 2.50 |
-95581699 | 2011-8-18 0:00: | PB | No Violations | 6.00 |
0030487516 | 2011-08-22 | Plug / Plug Back | No Violations | Rig ripped and pulled 8casing. |
0095581699 | 2011-08-18 | Plug / Plug Back | No Violations | Appalachian Surveys shot tubing at 2360. There was cave in and could not get passed this point. We also shot casing and set a 200 cement plug using Formation Cementing. Wright removed all tubing. |
0653036139 | 2011-08-11 | Plug / Plug Back | No Violations | Cemenco pumped on tubing. Tubing is plugged with paraffin. Will pump solvent down tubing. |
0670099489 | 2011-08-16 | Plug / Plug Back | No Violations | Kenny Wright is knifing paraffin out of the tubing. Has only reached 700. Total depth is 3400. |
1060912495 | 2011-08-15 | Plug / Plug Back | No Violations | Wire line truck is trying to shoot tubing off but cannot get down hole. Solvent truck coming in to treat tubing. |
1067945767 | 2011-08-19 | Plug / Plug Back | No Violations | Wright Well Service ripped the 4.5 casing at 1975. Set 200 rip plug with cement. Set a cast plug on 7 seat and placed 200 of clay on cast plug. |
1289i39059 | 2002-05-14 | Production Wells | No Violations | STATUS CHECK |
1289i39059270 | 2002-5-14 0:00: | PW | No Violations | |
1313593973 | 2011-08-17 | Plug / Plug Back | No Violations | Wrights Well Service is still pulling parafin out of well using solvent and swab cups. They are at a depth of 1760. Broke thru and was able to go to bottom of tubing. Appalachain Well Surveys will be out tomarrow to shoot off tubing. |
1480436667 | 2012-08-06 | Final Restoration | No Violations | On day of inspection the Final Inspection passed by Patrick Shreve on 8-6-12. All production material has been removed and regraded and vegetated back. |
2073403232 | 2011-08-23 | Plug / Plug Back | No Violations | Wright Well Service brought a steel dye nipple to screw on the down hole joint of 8 5/8casing. Screwed together with power tongs, pulled stretch and it started to rip. The pipe unseated and all 470 of 8 5/8casing came out. |
30487516 | 2011-8-22 0:00: | PB | No Violations | 4.00 |
653036139 | 2011-8-11 0:00: | PB | No Violations | 2.00 |
For data sources see[8]